Chapter 135 Published : PROCEEDINGS OF THE 7TH INTERNATIONAL MINE VENTILATION CONGRESS, June 17-22, Crakow, Poland CONTROL OF FIRE IN A LONGWALL PANEL UNDER SHALLOW COVER WITH CHAMBER METHOD OF VENTILATION AND HIGH PRESSURE HIGH STABILITY NITROGEN FOAM - A CASE STUDY N. Sahay Scientist Central Mining Research Institute, Dhanbad, India B.C. Bhowmick N.K. Varma S.K. Ray S.M. Verma Scientist Central Mining Research Institute, Dhanbad, India P.K. Mandal General Manager Jhanjra Area Eastern Coalfields Limited, India ABSTRACT Fire in a powered support longwall panel (AW 1 ) in RVIIA seam of 1 & 2 Incline mine of Jhanjra Project in Raniganj Coalfields, India was successfully brought under control using a novel ventilation technique and infusion of high pressure high stability nitrogen foam from surface through boreholes. A few years ago in 1994, a similar fire in Kottadih colliery about 10 km away from this mine was successfully tackled with pressure balancing and infusion of gaseous and liquid nitrogen from PSA type nitrogen generator and LN2 from tanker/reservoir (1). Due to complex geomining situations at AW1 panel the above method had to be supplemented by Chamber method of ventilation and infusion of high pressure high stability nitrogen foam. The panel had to be sealed three times within a period of six months due to recurrence of fire after reopening. Finally, Chamber method of ventilation was adopted for making the pressure of affected panel positive with respect to surface atmosphere and caved & sealed longwall panel (W1) in RVII seam which was about 40 m above the fire affected panel. Further high pressure high stability nitrogen foam procured from TECHNOVENT Czech Republic was injected through a number of boreholes in a systematic manner. For this purpose a foam generator of 9.6 m3/ min capacity coupled with trolley mounted PSA type nitrogen generator of 300 Nm 3/h capacity was put into service. Foaming agent having an expansion factor of 80 - 160 times and foam stability of about 72 hours was used. In addition to above, to meet any emergency situation LN2 in tanker and a reservoir filled with LN2 were kept in readiness. Above measures supported by thorough monitoring of status of fire by drawing gas samples from goaf through a number of boreholes and its analysis in the field laboratory ultimately led to control of fire in the panel. The panel is running smoothly with an average production of about 3000 tonnes of coal per day. The paper briefly discusses the genesis of the problem, chronological order of the events and action taken, results obtained, principle & practices of Chamber method of ventilation and high pressure high stability nitrogen foam technology coupled with a trolley mounted PSA type nitrogen generator. The method seems to be promising and cost effective for controlling fire in a running longwall panel with complex geo-mining conditions. This technique is general enough for successful application in other mine under similar situation. KEYWORDS Longwall technology, nitrogen infusion, chamber method of ventilation, dynamic balancing of pressure, sealed off area, foam infusion, goaf INTRODUCTION In 21st century powered support longwall technology has bright future in Indian coal mines. It has been successfully adopted in 1 & 2 Incline mine, Jhanjra Area of Raniganj Coalfields about 200 km from Kolkata, India. The mine has the reputation of successful completion of 10 (ten) longwall panels at 972 PROCEEDINGS OF THE 7TH INTERNATIONAL MINE VENTILATION CONGRESS shallow depth (about 40 m). The success at Jhanjra brightened the prospect of Longwall technology in Indian coal mine. However, fire in AW1 longwall panel, RVIIA seam not only crippled the Jhanjra mine by bringing all production activities to a halt but also had a much greater suppressive impact in the entire mining industry of the country as the story of Longwall technology in the country seemed to be leading to a sad end. It was, therefore, imperative to pool the collective wisdom and expertise of CMRI and mine management to work out innovative measures to tackle this fire, reopen the sealed off panel to save the costly equipment like powered support, shearer, AFC etc. and resume production at an early date. A similar type of fire in a longwall panel of Kottadih colliery(1), a neighbouring mine about 10 km from Jhanjra project was successfully controlled by application of pressure balancing and nitrogen infusion. However, the difficult geo-mining conditions at Jhanjra, explained later in the paper, made the fire problem more complicated and the technique of pressure balancing with nitrogen infusion was found effective in controlling fire in the longwall panel as long as it remained sealed. However, on reopening the panel the fire would erupt again. It was obvious that an improved technique of fire control was needed for this mine which led to introduction of chamber method of ventilation along with high pressure nitrogen foam technology that ultimately proved successful in keeping the fire under control not only when the panel was sealed but also when the panel was reopened and put under normal operation. The paper briefly deals with the problem, various measures taken to control the fire, their impact on status of fire and highlight the important lessons learnt which would be beneficial to other mines. In RVII seam a manual section is in operation and ten longwall panels have already been successfully completed, whereas in RVIIA seam developments by Road header machine in east and west sides of the property are in progress and one longwall panel (AW 1) in west side of the mine has just started. Layout of panels and developments in RVII and RVIIA seams are shown in Figure 1. Entries into the mine are through Incline 1 & 2 and ‘D’ shaft sunk upto RVII seam. No 1 & 2 Incline mine was producing about 3500 tonnes of coal per day deploying 1200 personnel before the onset of fire in AW1 panel. INCLINE 1 INCLINE 2 MANUEL DIST 1D 2D W4 AW2 AW2 AE1 AW1 AE1 W1 D S D Shaft PARTICULARS OF THE MINE RVII seam circuit RVIIA seam circuit Jhanjra Area extends to about 12 Sq km which is encircled by faults with throws varying from 10 to 30 m. Jhanjra block has nine viable seams with total extractable reserves of 212 million tonnes of coal. It is being extracted by two mines viz 1&2 Inclined mine and Main Industrial Complex. Depth of the seams varies from 38 to 380 m. Details of thickness and depth of the five top seams are given in Table below: S.No 1. 2. 3. 4. 5. Seam number RVII RVIIA RVI RV RIV Thickness, m 1.27 - 4.23 0.45 - 4.11 2.15 - 5.60 2.90 - 6.64 3.75 - 11.27 Depth, m 76 109 201 231 257 The seams are degree II gassy. In Incline 1 & 2 mine workings are spread in two seams viz. RVII and RVIIA. Figure 1. Schematic diagram of 1 & 2 Incline mine, Jhanjra area Ventilation circuit General Ventilation layout of the mine is shown in Figure 1. The mine is being ventilated by an Axial flow fan (make - Voltas, Model - VF 2500) installed at Incline No 1. The fresh air reaches the mine through Incline No. 2 and Shaft ‘D’ situated at extreme boundary of the property. Development of the mine is between these openings viz. No 2 Incline and ‘D’ shaft along RVII and RVII A seams. No 1 dip having conveyor belt installations all along its length is connected with incline no. 1 serving the purpose of main return airways and transportation of coal of the total mine. The air flowing down through incline no. 2 is mostly utilised for ventilation of workings of RVII CONTROL OF FIRE IN A LONGWALL PANEL UNDER SHALLOW COVER HISTORY OF FIRE IN THE MINE Presence of CO to the extent of 80 PPM was noticed in the tail gate during extraction of W1 panel in 1990 91 which ultimately vanished after 400 m progress of the face. The measure taken was only dozing on the surface above W1 panel . 115.0 m BH 1 C B BH 4 B A B BH 12 BH 3 B BH 2 C BH 13 BH 5 BH 11 C Figure 2: Conceptual model of the goaf Figure 2. Conceptual of the goaf BH 14 Installation Chamber Some details of AW1 panel AW1 longwall panel with single entries, retreat and U-system of ventilation is the first panel in RVIIA seam. This panel is located below the caved and sealed longwall panels W1 & W2 in RVII seam. Details of the panel are given below. Name of the Panel : AW1 Name of seam : RVIIA Seam Thickness : 3.2 m Length of panel : 850 m Depth from surface : 97 m Parting between RVII : 40 m & RVIIA seams Length of face : 120 m No. of chocks : 82 Chock resistance : (4 × 550) tonnes Distance of installations chamber between : 40 m AW1 & W1 panels Date of Starting of : 08.06.1999 the panel Thickness of RVIIA seam at installation chamber is 3.2 m, but due to limitation in support resistance (4 x 550 tonnes) only 2.4 m height of the seam could be extracted along the floor. About 0.8 m thick coal layer along the roof was left in the goaf. After progress of 40 m of the face it was observed that there was no periodic weighting and goaf was not even half filled. Apprehending the danger of air blast, Induced blasting was resorted to after every 10.0 m mark to fill up the goaf. After 40.5 m progress of the face local fall occurred on 27.7.99 and as a result the goaf was filled to about 90%. Main fall occurred after 80.5 m progress of the face on 18.8.99. After occurrence of main fall water from upper seam goaf started percolating down at the rate of about 200 GPM, although a borehole was drilled earlier from lower seam to upper seam for dewatering purpose. On 28.8.99 traces of CO gas at top gate of AW 1 panel in RVIIA seam was noticed after ocurrence of main fall which increased gradually to 400 PPM even after further progress of the face by 30 m. Finally, the panel was sealed on 8.9.99 by erecting stoppings at top and bottom gates. At this juncture CMRI was called for scientific support for assessment of status of fire and extinguishment of fire quickly. A team of scientists of CMRI visited the mine. Details of investigations2 carried out by the authors, approaches adopted for control of fire and result obtained are discussed briefly phase wise in the following paragraphs. The entire period of fighting the fire are divided into eight phases. List of the action taken and their results with observation are furnished in Table 1. From the account of action taken to control fire during the first seven phases of fire fighting operation and their results it is clear that: 1. The conventional model of packing of longwall goaf viz. free zone, critical zone and compact zone as propounded by various authors (3) are not applicable in this mine. 2. Location of seat of fire was not known. 3. Heat could not be dissipated even after keeping the panel in sealed condition more than 90 days and maintaining its temperature below 10°C by pouring LN2 through different boreholes. 4. Requirement of Nitrogen gas is very high to control fire in open longwall panel due to uncontrolled leakage of air . 5. Rate of emission of CO increased rapidly within a few days after getting an indication of its presence in the face. Finally, during 8th phase of fire fighting operation a new model for packing of goaf in this situation considering: bolted roof of top & bottom gate, panel located below caved panel of upper seam, shape of the goaf being almost square. was conceived. Conceptual model alogwith location of bore holes is shown in Figure 2. Face seam and developments of RVIIA seam whereas air entering through ‘D’ shaft is used for ventilation of isolation stoppings of sealed Longwall Panel of RVII seam and Longwall panel AW1 of RVIIA seam. Air enters through ‘D’ shaft into RVIIA seam flows along shaft level, 1 L north sump, 0 dip and reaches to bottom gate of AW1 longwall panel. Return air of AW1 flows along top gate, 0 rise and joins the main return flowing along 1st rise and No 1 incline. 973 974 PROCEEDINGS OF THE 7TH INTERNATIONAL MINE VENTILATION CONGRESS Table 1. Summary of results of action taken during different phases of controlling fire with observations Ph. No Period No of days/ panel condition I 01.09.99 to 10.09.99 9 Sealed II 11.09.99 to 12.09.99 2 Opened III 13.09.99 to 27.09.99 14 Sealed IV 27.09.99 to 09.10.99 V 10.09.99 to 28.11.99 14 Sealed 29.11.99 to 08.12.99 10 Opened VI VII 9.12.99 to 13.03.99 12 Opened 94 Sealed Bore Hole available Action taken 1, 2 & 3 Injection of LN2 through BH Nos. 1, 2 & 3 -do- - Injection of LN2 through 1, 2, 3 boreholes and Dynamic & 4 balancing of pressure around AW1 panel Chamber method of ventilation and Injection of LN2 through BH4 Dynamic balancing 1, 2, 3, around AW1 and 4 & 5 Injection of LN2 through bore-holes. Chamber method of ventilation and Injection -do- of LN2 through BH4 & 5 -do- Dynamic balancing of pressure and Injection of LN2 through boreholes selected on the basis of O2 in the borehole. Further LN2 inj. rate was controlled so as to keep the goaf only slightly positive with respect to atmosphere In the Figure the zone marked A is considered well compacted through which no or little leakage of air is possible. Hence it is not very risky from heating point of view. The area marked B is only partially compacted which may allow slight leakage of air. The area under C is by far least compacted zone allowing leakage of air which may lead to spontaneous heating The crushing along the boundary of this zone may further enhance the chances of heating. On the basis of this model a few additional bore holes viz. 11, 12, 13 & 14 were drilled in zone C to facilitate inertisation and plugging this highly sensitive area by injection of high pressure high stability nitrogen foam. IDENTIFICATION OF LOCATION OF SEAT OF FIRE To deal with fire identification of its location is very important. However, in most cases identification of Goaf environment at end of the Day O2 % CO Tem. 0C ppm 12 Nil 26 19 400 - 1.9 30 26 - 1400 - 1.9 Nil 26 - 2200 - Amount of LN2 flushed, ltrs. 51,123 Observations Environment of goaf behind stoppings and bore holes i.e. only closed to the face could be assessed Ventilation of the face could not be controlled because face was abot 90% filled with water Environment of total goaf was monitored by using 1,05,915 number of bore holes 67,046 Ventilation sys-tem was disturbed on 7.10.99 and LN2 supply was intrupted. Environment of total goaf was monitored by using 2,31,965 number of bore holes 35,427 Chamber method of ventilation could be maintained upto 5.12.99 Environment of total goaf was monitored by using number of bore holes and consumption of LN2 was reduced 0.2 Nil <10 1,74,097 exact location of seat of fire is rather difficult. In case of fire in AW1 panel, due to geo-mining condition the problem become very complex. As per example the fire could be in the same (RVIIA) or in the upper seam(RVII). Fire in RVIIA seam may be due to: Spontaneous heating in the heap of broken coal lying in the goaf. Non dissipation of heat generated during induced blasting in the panel. Delay in main fall allowing free path for air in the goaf. But the possibility of heating in the upper seam (RVII) also could not be ruled out due to following reasons: 1. The W1 panel in RVII seam having a history of fire is just above the AW1 panel with a parting of only 40.0 m. Toxic gases and even smoke due to fire in this panel may easily leak to AW1 panel giving false indication of fire in the bottom seam. CONTROL OF FIRE IN A LONGWALL PANEL UNDER SHALLOW COVER The System requires 1. Ventilation Survey data in the mine 2. Conversion of an area into Chamber by closing cross connections. 3. Axial flow fan of desired capacity. 4. Two regulators of variable aperture, R1 & R2 as shown in Figure 3. The function of R1 is to create pressure difference across the face to achieve optimum flow of air at the face and minimum leakage of air into goaf. Similarly R2 is to raise the pressure of the chamber to desired level so that goaf pressure is slightly positive with respect to atmosphere. Before finalising the design of the arrangement for implementation of Chamber method of ventilation a limited ventilation survey was carried out in the mine from the mouth of Incline 2 to bottom gate of AW 1 panel along intake via drift. Results showed that the cumulative pressure drop upto bottom gate was 120 Pa. Accordingly, design of chamber method of ventilation was worked out and implemented around AW1 panel. In this system of ventilation a chamber is formed by closing cross cut connections between 0 rise and 1st rise as shown in Figure 3. 0 Rise 1 Rise R2 Top Gate BH 5 R1 Goaf Bottom Gate X D Keeping the above arguments in mind following strategies were worked out to control the fire and its quick suppression if it gets aggravated again after reopening on 14.03.2000. 1. Reduction in air leakage into goaf either from bottom gate side or from upper seam or surface with adequate air quantity at the face. Monitoring of status of fire through boreholes by maintaining pressure of the boreholes slightly positive by adoption of a ventilation arrangement called Chamber method of ventilation, which has been discussed in later chapter in the paper. 2. Plugging of air path from top and bottom gate sides particularly along the barrier and create N2 bank in the floor of the goaf. For this purpose High pressure high stability Nitrogen foam technology comprising foam generating machines and foaming agent from M/s Technovent PTY Ltd, Czech Republic was used. Another foaming solution from M/s Control system, Kolkata, India was also used when the foaming agent from Czech was exhausted. Details of high pressure high stability foam technology has been discussed in the later chapters. 3. To keep good environment at face safe and to maintain CO level within permissible limit even when concentration of CO in the goaf became high, air from Chamber method of ventilation It is a ventilation arrangement which is superimposed on the main ventilation system to neutralise or reduce the cumulative pressure drop from desired area in the mine measured from surface. In case of a longwall panel at shallow depth or in multi seam working air leakage may take place in uncontrolled manner, depending upon size of cracks & fissures and suction pressure created by the fan. Continuos feeding of air either through bottom gate or surface in a place where rate of dissipation of heat is poor, may result in onset of spontaneous heating in the goaf. To overcome this problem Chamber method of ventilation may be adopted with benefit. D ACTION TAKEN DURING 8th PHASE goaf was discharged to atmosphere through boreholes close to the zone of high CO concentration. D 2. Leakage of air through surface cracks to the goaf due to suction pressure created by the main fan may lead to heating. 3. Huge amount of coal lying on the floor in the panels and its possible oxidation after dewatering of the goaf. Further, the panels W1 , W2 , W3 & W4 in RVII seam may be inter connected and migration of CO from any one of the panels to AW1 panel is possible. Presence of air leakage path from surface through cracks to any segment of the four panels stated earlier may extend upto AW1 panel and seat of fire may be any where in this path. Considering the possibilities and situations mentioned above in both the seams it was very difficult to decide the exact location of seat of fire. To locate the seat of fire further investigations were carried out with particular emphasis on following. 1. Study of concentration gradient of CO in RVII & RVIIA seams. All boreholes samples results showed that CO concentration was always higher in bottom seam than in top seam clearly indicating that location of fire was in bottom seam. 2. Study of pressure gradient along the panels in both the seams indicated favourable condition for flow of CO from lower to upper seam. The concentration of CO is lower in upper seam than that in lower seam is again a clear indication of existence of fire in the lower seam. The above analysis more or less confirmed that location of seat of fire was in AW 1 panel. Exact location of fire could be established only after assessment of results of foam infusion through different bore holes, discussed in later chapters. 975 Auxiliary Ventilation System 1 L North Chamber fan ‘D’ Shaft Figure 33. : Layout of Chamber system around AW1 Panel, RVIIA seam Figure Layount ofventilation Chamber ventilation system around AW1 Panel, RCIIA seam 976 PROCEEDINGS OF THE 7TH INTERNATIONAL MINE VENTILATION CONGRESS The chamber comprises top and bottom gates, 0 rise and the face. A forcing fan of suitable capacity is installed at 1L north on intake side of the chamber. The specification of the fan is worked out on the basis of requirement of the air quantity in the chamber considering pressure of the chamber to be maintained slightly higher with respect to atmosphere and to create pressure difference sufficient for optimum airflow rate at the face with minimum leakage of air into goaf. In this system there are two regulators namely R1 and R2 in 0 rise. Results of performance studies of chamber ventilation system are furnished below: Fan make : Voltas Fan type : PV-160 Fan pressure : 314.0 Pa Air quantity handled by fan : 41 m3/s Pressure of chamber measured at : (+) 98.0 Pa top gate Pressure drop across R1 : 8.0 pa Air quantity at face : 6.70 m3/s Air quantity at R1 : 20.0 m3/s Pressure of borehole No5 : (+) 20.0 Pa Air quantity at bottom gate : 7.43 m3/s Leakage of air into goaf : 0.76 m3/s Pressure developed by main fan : 785.0 pa Air quantity handled by main fan : 90.0 m3/s High pressure nitrogen foam Injection of N2 in liquid or gaseous form through borehole may not yield the desired result in open goaf because during injection, pressure at the bottom of borehole is high and N2 comes out from the goaf in a very short time following low resistance path, possibly along the roof. To reduce the requirement of Nitrogen and for plugging leakage path, injection of high pressure nitrogen foam was found very effective in controlling fire in AW1 longwall panel. Details of the foam technology are given in reference (4). Foam was generated with 3% solution of foaming agent using a Foam generator connected to a trolly mounted PSA type nitrogen generator having a capacity of 300 Nm3/hr at 98% purity. The arrangement is shown in Figure 4. The efficacy of this technology depends upon Location of borehole used for infusion of foam. Amount of foam injection To find the best results of foam injection, foam was injected through different bore holes located in different zones of the goaf. It has been stated earlier that on the basis of compaction, the goaf may be divided into three zones viz., A, B and C. A is compact zone, B is critical zone and C is free from roof fall. From Figure 2 it can be seen that bore holes No 1, 2, 3, 4 & 11 are all located in zone C and bore hole No 5 lies in zone B. Effect of foam injection through different bore holes are discussed below: Case I : Injection of foam through BH No. 1 Nitrogen foam generated from 3% solution of foaming agent with 98% pure N2 from PSA type nitrogen generator was injected through BH No. 1. 100 Kg of foaming agent which is equivalent to 200 m3 of foam was used. Environment inside goaf was monitored through boreholes by multi gas analyser. Results are furnished in Table below. Date 15.3.2k BH NO. 1 3 4 AFC, U/G Time hrs. 12.20 13.15 12.05 13.10 CO2, % 5.59 3.03 2.64 1.37 O 2, % 4.49 7.26 12.6 17.2 CO, ppm Nil Trace Nil Nil The table revealed that O2 % in BH 1 is 4.49% where as O2 % in BH 4 is 12.60%. Hence injection of foam through BH-1 does not plug air space which is extended up to installation chamber. Hence injection through BH-1 alone was not very effective. Figure 4. Arrangements for injection of foam through boreholes Case II: Injection of foam through BH Nos. 1 &2 On 17.3.2k foam was injected through Borehole Nos. 1 & 2. Foam generated from 100 Kg of foaming agent was injected into goaf through BH-1 and 300 Kg of CONTROL OF FIRE IN A LONGWALL PANEL UNDER SHALLOW COVER foam in similar concentration was injected through BH 2. Environmental condition of goaf was monitored through B H No. 1 & 4. Results are given below. Date 17.3.2k BH NO 1 4 Time hrs. 21.00 21.10 O2, % 3.97 16.9 CO, ppm Nil 38 From the result it is clear that percentage of O2 in BH 4 is increasing even after injection of foam through BH 1 & 2. It clearly indicated that injection of foam through these boreholes was also not very effective. of gas concentration seat of fire appears to be around BH 11 in AW1 panel, RVIIA seam and probably it is between BH11 and installation chamber. To investigate this problem further drilling of three boreholes around BH 11 connecting to installation chamber of AW1 panel were proposed. Boreholes viz., 12, 13 & 14 were drilled near junction of installation chamber of AW1 panel and top gate as shown in Figure 2 and gas sample drawn through these boreholes were analysed. Results are furnished in table below: Date 26.3.2k Case III: Injection of foam through BH Nos. 4, 5&11 On 18.03.2k foam generated from solution of 150 Kg, 75 Kg and 150 Kg was injected through borehole Nos. 4, 5 & 11 respectively and environmental condition of goaf was monitored before and after injection. The results are furnished in table below. Date 18.3.2k 19.3.2k 20.3.2k BH Time O2, % CO, Face NO. hrs. ppm 1 05.40 9.0 Nil Nil 5 05.45 12.9 62 Nil 11 06.20 13.6 110 Nil 1 10.15 10 Nil Nil 11 10.30 13.8 110 Nil 2 10.40 16.9 13 Nil No communication through borehole No. 4, 5 & 11 after foaming 1 23.30 1.5 8 Nil 2 23.45 17.8 19 Nil 5 00.00 17.0 133 18 From the table it can be seen that O2 concentration is high through out the goaf except near borehole No.1. Case IV : Injection of foam and LN2 through BH No. 11 On 21.3.2k, foam infusion was done through Bore hole No 11 200 Kg of foaming agent was used. Further, 10 K litres of LN2 was injected through borehole No. 5 and environmental condition of goaf was monitored through boreholes. Results of the monitoring are furnished in table below. Date 22.3.2k BH NO. 2 4 11 O2, % 7.7 12.1 6.8 CO, ppm 21 0 1200 The table reveales that CO in BH 11 is 1200 ppm and it was gradually rising even after injection through different boreholes in different quantity. From the study 977 01.4.2k BH NO 12 13 5 13 14 Time hrs. 10.00 10.30 18.30 18.45 18.50 O2, % 4 11.2 7.5 5.27 4.52 CO, ppm 201 1200 10800 10375 10900 From the above results location of fire was confirmed to be in the installation chamber of AW1 panel in top gate side between borehole No. 13 and 14. Discharging CO into atmosphere through borehole When CO at face increased from permissible limit, pressure of the chamber was increased by closing regulator R2 underground and boreholes 5, 2 & 3 were opened to allow discharge of goaf air to atmosphere. However, care was taken to see that fresh air from longwall face did not leak into goaf. For this purpose LN2 injection through borehole No 12 & 13 at the same rate of air discharge was maintained. This measure proved effective. Control of fire After confirmation of location of fire, Indian protein foam was injected through boreholes No. 12,13&14 alternately. Foam generated from 200 to 800 kg of protein base foaming chemical of Indian origin (procured from M/s Control system, Kolkata) was injected daily using trolly mounted PSA type nitrogen generator at the rate between 200 to 220Nm3/hr and purity 98%. This was supplemented with injection of about 150 liters/h of LN2 infusion through nearest to aforesaid borehole. Further, as stated earlier chamber method of ventilation was adopted around AW1 panel to make the chamber slightly positive with respect to atmosphere as well as the W1 & W2 panel in RVII seam and provided air quantity at face in the range of 6.0 to 12.0 m3/s at the pressure drop across the panel between 80 and 210 Pa. Environmental condition of the goaf was monitored by air sampling through borehole no. 1, 2, 3 & 5. Results of all these measures were very encouraging as can be seen from the Figure5. Fire was brought under control. The panel was finally reopened on 14th march 2000. Since then it is running smoothly and producing about 3000 tonnes of coal per day. 978 PROCEEDINGS OF THE 7TH INTERNATIONAL MINE VENTILATION CONGRESS 12000 1000 Injection of foam & LN2 through BH Nos. 1, 2, 4 & 11 Nitrogen Foam, Kg 900 Injection of foam & LN2 through BH Nos. 12, 13 & 14 10000 800 CO 700 8000 CO, ppm LN2, ltr/hr 6000 600 500 400 4000 300 200 2000 100 Series1 Series2 5/6/00 5/4/00 5/2/00 4/30/00 4/28/00 4/26/00 4/24/00 4/21/00 4/15/00 4/13/00 4/9/00 4/11/00 4/7/00 4/3/00 4/1/00 3/28/00 3/26/00 3/23/00 3/21/00 3/18/00 3/15/00 0 3/13/00 0 Series3 Figure 5 : Variation of CO in the goaf of AW1 panel of 1 & 2 Incline with injection of LN2 & Nitrogen foam Figure 5. Variation of CO in the goaf of AW1 panel of 1 & 2 Incline with injection of LN 2& Nitrogen foam CONCLUSIONS & RECOMMENDATIONS Conclusions that emerged during dealing with fire in AW 1 panel are as below: 1. Reduction in air leakage into goaf either from bottom gate side or from upper seam or surface even when adequate air quantity flows through the face by Application of Chamber method of ventilation around AW1 panel was very effective in control of fire. 2. Monitoring of status of fire through boreholes by maintaining pressure of the boreholes slightly positive and analysing the air samples by Multi-gas Analyser provided an accurate status of the fire affected area and helped in locating the actual seat of fire. 3. Plugging of air path from top and bottom gate side particularly along the barrier and creation of N2 bank in the floor of the goaf by injection of high pressure high stability N2 foam was found effective in eliminating/reducing leakage of air to seat of fire. 4. Method to check flow of CO from seat of fire to face by discharging of CO in the atmosphere through boreholes when concentration of CO at the face is exceeding the permissible limit was found quite effective however, it must be worked out and executed carefully and the amount of goaf air discharged must be replaced by infusion of same amount of N2 into goaf through bore hole. Finally, after the advancement of the face to about 240 m, fire was brought under complete control. The face is progressing smoothly and producing about 3000 tonnes of coal per day. ACKNOWLEDGMENT The authors express their sincere thanks to Director, Central Mining Research Institute, Dhanbad for granting permission to publish this paper, members of Ventilation & Special Projects Discipline of CMRI and Mine management for sincere cooperation in field investigations and execution of the measures in controlling fire. Further special thanks to Sri A. Ansari of CMRI for field investigation and compilation of data. Thanks are also due to Dr. V.Voracek., Czech Republic, for valuable suggestions during Injection of foam. The opinion express in this paper are those of authors and not necessarily of CMRI. REFERENCES Bhowmick, B.C., Sahay, N., Ahamad, I. and Verma, S.M., 2000, “Significant improvement in effectiveness of nitrogen infusion technology for control of fire by dynamic balancing of pressure - a case study of powered support longwall face”, The Canadian Mining and Metallurgical Bulletin, Vol. 93, No. 1038, March, pp. 74-80 CMRI report on “Quick control of spontaneous heating and early reopening of aw 1 longwall panel in 1 & 2 incline mine, jhanjra area, ECL”, 2000 McPherson, M. J., 1993, Subsurface ventilation and environmental engineering. Chapman & Hall, London Voracek V., 1994, “Usage of nitrogen foam for both prevention and suppression of spontaneous combustion of coal in Ostrava-Karvina coalfields”, Proceeding of Workshop on Occupational safety and environment protection in underground coal mining Industry, Sczyrk, poland, October