Natural Gas Pipeline Accident Investigations – Perspectives and Recommendations John B. Vorderbrueggen, PE Chief, Pipeline and Hazardous Materials Investigations 1 WRGC August 20, 2013 A Short NTSB Overview How old is the NTSB? A. 30 years B. 39 years C. 73 years D. 87 years E. 95 years 2 Origin of the NTSB • Air Commerce Act of 1926 U.S. Department of Commerce shall investigate aircraft accidents • 1940 - Investigations assigned to the Civil Aeronautics Board Bureau of Aviation Safety 3 Origin of the NTSB • 1967 - NTSB embedded in the U.S. Department of Transportation • 1974 - NTSB reestablished as an independent, Executive Branch agency • U.S. Code Title 49, Chapter 11 4 NTSB Improvements • 1996 – Coordinate assistance to families of aviation accident victims • 2000 – Created the NTSB Training Academy (NTSB Training Center) − GW University Campus in Ashburn, VA − Improve employee technical skills − Provide investigation expertise to industry 5 NTSB Features • Independent Federal Agency • Does not regulate transportation equipment, personnel, or operations • No official role in establishing and enforcing industry regulations • Does not initiate enforcement action • Issues and tracks Recommendations 6 NTSB Transportation Modes • Aviation • Marine • Highway • Railroad • Pipeline and Hazardous Materials 7 Other NTSB Offices • Research and Engineering − Safety Research and Satirical Analysis − Vehicle performance − Vehicle recorders − Materials laboratory − Medical Investigations 8 Other NTSB Offices • Administrative Law Judges − “Court of appeal" for airmen, mechanics or mariners for certificate actions − Hear, consider, and issue initial decisions on appeals − Adjudicate claims for fees and expenses from FAA certificate and civil penalty actions 9 The NTSB Board Members August 2013 Hon. Deborah A. P. Hersman Acting Chairman Hon. Robert L. Sumwalt Hon. Christopher A. Hart Hon. Mark R. Rosekind Hon. Earl F. Weener 10 Natural Gas Transmission Pipeline Accidents San Bruno, California Palm City, Florida 11 Pacific Gas and Electric Company Natural Gas Transmission Pipeline Rupture and Fire San Bruno, California September 9, 2010 12 Pipe Segment Crater 14 Claremont Drive Earl Avenue RUPTURE Glenview Drive Accident Consequences • Eight fatalities • Dozens injured • 38 homes destroyed • More than 70 homes damaged 16 17 Ruptured Pipeline Details • 30-inch diameter, 0.375-inch wall • Installed in 1956 • API Grade X42, carbon steel • Documents listed seamless pipe • Other inaccurate fabrication records 18 Events Prior to the Rupture • Electrical maintenance work at Milpitas Terminal • Power supply units interrupted • Line discharge pressure climbed 19 Accident Event Timeline • 5:45 p.m. pressure rose above 375 psi • 6:11 p.m. pipeline ruptured when pressure reached 386 psi • 7:30 p.m. upstream valve closed • 7:46 p.m. downstream valves closed 20 Undocumented Configuration North joint Pup 6 Pup 5 Pup 4 Pup 3 4½ feet Pup 2 Pup 1 3½ - 4 feet each South joint Rupture initiation 21 Comparison of Pipe Attributes Section South joint DSAW seam weld Rolling direction Yield strength Weld hardness Pup 1 Pup 2 Pup 3 Pup 4 Pup 5 Pup 6 North joint No record of material supplier, material pedigree, or fabrication records 22 Typical DSAW Seam Weld Raised weld reinforcement Outer wall Weld metal (first pass) Weld metal Inner wall (second pass) Raised weld reinforcement 23 Incomplete Pup 1 Seam Weld No weld reinforcement Outer wall Fracture through weld Unwelded region Inner wall 24 Fit-up angle Identified Safety Issues • Multiple deficiencies in PG&E operations practices • Federal and state regulatory oversight weakness • Deficient federal pipeline safety rules 25 Other Shortcomings • PG&E integrity management, threat identification, record keeping, dispatch procedures • CPUC hydrotest exemption for pre-1961 pipelines • DOT grandfather hydrotest exemption for pre-1970 pipelines 26 Probable Cause Inadequate quality assurance and quality control in 1956 pipe relocation − Substandard longitudinal pipe joint with a visible weld flaw that grew to a critical size − Pipeline ruptured when poorly planned electrical work at the Milpitas Terminal caused an unplanned pressure increase 27 Probable Cause (cont.) Inadequate pipeline integrity management program − PG&E failed to detect and repair, or remove the defective pipe 28 Probable Cause (cont.) Contributing to the accident • CPUC failed to detect the inadequacies of the PG&E pipeline integrity management program 29 Probable Cause (cont.) • California Public Utilities Commission and the U.S. DOT exemptions from pipeline pressure testing of existing pipelines − Hydrotest would likely have identified the installation defects 30 Probable Cause (cont.) Contributing to the severity of the accident • Lack of automatic shutoff valves or remote controlled valves • Flawed PG&E emergency response procedures • Delay in isolating the rupture 31 Pre-report Recommendations • Pipeline and Hazardous Materials Safety Administration (2 Early, 1 Urgent) • California Public Utilities Commission (3 Urgent) • Pacific Gas and Electric Company (2 Early, 2 Urgent) 32 Final Report Recommendations • The U.S. Department of Transportation (4) • The Pipeline and Hazardous Materials Safety Administration (13) • The State of California (1) 33 Recommendations (cont.) • The California Public Utilities Commission (2) • The Pacific Gas and Electric Company (8) • The American Gas Association and the Interstate Natural Gas Association of America (1) 34 Florida Gas Transmission Company Pipeline Rupture Palm City, Florida May 4, 2009 35 36 Pipeline Details • 18-inch diameter carbon steel, 0.25-inch wall thickness, API 5LX, 1959 installation • Hydrotested at 1085 psig • 1971 hydrotested at 1320 psig - 866 psig MAOP 37 Pipeline Details • Polyethylene tape coated and cathodically protected • 2004 Magnetic flux leakage in-line inspection • Postaccident metallurgy identified replaced segments but no record of the change 38 39 40 41 Pipeline Configuration • Three parallel, interconnected lines • Dual pressure-reducing regulators protected lower MAOP on 18 inch line • Normal flow demand (pressure) fluxuations expected 42 43 System Response to the Rupture • Line break actuator closed upstream ASV within two minutes • Downstream actuator failed to activate • FGT crew closed valve two hours later 44 Post-Accident System Test • Downstream ASV operated as designed − Rate-of-pressure drop setpoint was most likely above the accident pressure decay rate − Pressure decay dependent on looped system interaction 45 SCADA System • No position indication on mainline valves or cross-connect regulators − Controllers were unaware of ASV closure and the full-open regulators • No alarms sounded − Pressure scan rate too low to detect short duration pressure drop 46 Postaccident Pipe Inspection • No internal corrosion • External corrosion pitting under damaged coating − 30 percent wall thinning along longseam, below minimum required • Magnetic particle inspection identified longitudinal cracks along longitudinal weld 47 Class Location • Ruptured pipe assigned Class 1, no HCA sites − Integrity management not required − Baseline in-line inspection was performed − Mainline valve spacing for Class 1 • Class 3 applied - school within 366 feet 48 49 Integrity Management Program • Stress corrosion cracking was not considered a significant risk • 2004 caliper tool and axial MFL in-line inspection – no repairs required in rupture area • Axial MFL does not accurately detect longitudinally oriented stress corrosion cracking 50 FGT Postaccident Actions • SCADA instrument upgrades on looped systems • Pressure transmitters installed at regulators and each parallel line • Valve position sensors installed on regulators and cross-connect valves • Remote control functionality added to the cross-connect valve 51 FGT Postaccident Actions • SCADA pressure rate-of-change alarm configuration revised • Conducted circumferential MFL inspection • Hydrostatic pressure tested the line – four failures on the 18-inch pipeline • Follow-up hydrostatic spike test 52 Probable Cause Pipeline failed due to environmentally assisted cracking under a disbonded polyethylene coating that remained undetected by the integrity management program The integrity management program incorrectly identified the pipe section as not a high consequence area 53 Probable Cause (cont.) Contributing to the prolonged gas release was the inability of the pipeline controller to detect the rupture due of limitations in the SCADA system and the configuration of the pipeline. 54 Ongoing Investigations • Cleburne, Texas Enterprise Products Operating, LTD June 7, 2010 One Fatality • Sissonville, West Virginia Columbia Gas Transmission December 11, 2012 55 The NTSB Perspective Most Wanted List – Pipeline Safety • PHMSA and State regulators must improve industry oversight − effective performance-based standards − adequacy of integrity management and inspection protocols − ensure deficiencies are promptly corrected Pipeline Safety (cont.) • Operators need to improve emergency response − Faster leak isolation using automatic and remote shutoff valves − Provide key information on pipelines to local jurisdictions and residents John B. Vorderbrueggen, PE Chief, Pipeline and Hazardous Materials Investigations 202-314-6467 John.vorderbrueggen@ntsb.gov 58