Sustainability practitioner Ross Greenhalgh Company : Tesco Stores Ltd Description of person (max 750 words) : I am submitting my nomination for this award because through my work I have demonstrated that through good operation of environmental assets, businesses can make profit as well as save carbon; true sustainability. Executive Summary Through my Lean Six Sigma Green Belt project work, I changed the way Tesco runs its CHP fleet, increasing profit and reducing our carbon footprint. By considering all factors and modelling the units, profitability increased by 20%-50%, far exceeding the target of 5% and making the company’s sustainable business strategy work at an operational level. Background In the current economy, it is more important than ever that sustainable business strategies are both financially and environmentally viable. As part of Tesco’s strategy it has been installing gas CHPs on major developments for the past few years. It was clear that we could operate and control our CHP systems better to make them more profitable, while maintaining the carbon benefits. We have: 158 gas CHPs Installed capacity of 20 MWe Two operators – Cogenco and EnerG. Until recently, we have operated our CHPs with one strategy applied across all sites, a simple and effective approach, but not sustainable for continued investment from the business. Planning I agreed a brief with my project’s sponsor to define the problem – we can control and operate our CHP systems better. I used a series of project management tools to understand the processes and then value stream mapped these to identify waste. Of utmost importance was the root cause of why we ran the engines the way we did. I used a fishbone approach to figure out the causes considering: Materials Machines Manpower Mother Nature Measurement Methods Through stakeholder engagement I gathered an understanding of what our customers were looking for, as well as what the business needed. The key issues were energy price, weather, budgeting approach and data. No capital was required, but changes to the revenue budgets involved needed agreement through the business. The proposed timelines for the project ran from November to April, with a target to improve profit by 5%. Innovation I started by looking at the short-term operation, but stakeholder feedback showed the longer term also needed to be tackled. Data was the first issue, which I resolved by working with EICT (our energy data supplier) to generate the right data in the right format. I also resolved budgeting issues by working with budget owners and our Finance teams to agree that the changes were the right thing to do overall, despite being more beneficial to some than others. The final element was an automated model to address the remaining issues. I created a model combining all the metrics that encompass running of gas CHP, including, but not limited to: Energy price Climate Change Levy (CCL) Carbon Weather Regional heat demand profiles Engine inputs and outputs (kWh and £) Maintenance This allowed me to create a full-year forecast alongside the short-term, tactical forecast. This helped to maximise the profitability in both respects while maintaining the carbon contribution to long-term targets. Efficiency improvements I achieved improvements by running the engines proactively rather than reactively - smarter, not harder. Running the engines at the right time of day, week and year established the profitability increase. Delivery The delivery of the project involved setting up a simple communication process with the operators to tell them when to run the engines. No disruption to operations was anticipated, because the CHPs are lead boilers - meaning the boilers pick up any heat demand when the CHP is off. As a precaution, I engaged our maintenance team and we agreed that any issues would be escalated back. One issue occurred at a site that had the boilers in manual override, but this was promptly resolved. Results No capital budget was required for the project, all changes to the revenue budgets were agreed through the correct processes. The analysis phase took longer than hoped, but ‘quick wins’ were implemented before the trial and the project got back on track before the end. The profitability improvements ranged from 20% to 50% depending on the engine, exceeding the target of 5 %. The key conclusion was that if environmental initiatives are not financially sustainable for businesses, then they are not truly sustainable. Correct operation of these assets can go a long way to turning around the perception that saving carbon costs money.