Implementing Six Sigma Quality at Better Body Manufacturing D M A I Define Measure Analyze C Improve Control D M A I Overview Define Measure Analyze C Improve Control ABC Incorporated (ABC) is not achieving Six Sigma quality levels for all critical Body-Side Sub-Assembly dimensions as requested by their customers. 200000 DPM 150000 DPM 0 ASM_9Y 3874 ASM_10Y 776 ASM_6Y 4 ASM_6Y 50000 19786 ASM_10Y 85824 ASM_3Y ASM_9Y ASM_8Y ASM_3Y 172475 ASM_8Y 100000 ASM_7Y ASM_7Y Dimension Ensure that all critical body-side subassembly dimensions are within Six Sigma quality levels of < 3.4 DPM. Cp 2.0 and Cpk 1.67. • Determined the correlation between body side and assembly dimensions. • Evaluated the significance of Tonnage > 935 for ASM_7Y & ASM_8Y. • Conducted a DOE for Clamp position for ASM_9Y & ASM_10Y. • Change tonnage to > 935 to correct ASM_7Y and ASM_8Y • Set clamp position to location 2 for ASM_9Y and ASM_10Y • Re-machine A-pillar die to correct A_3Y and ASM_3Y 2 Problem Statement & The Goal D M A I Define Measure Analyze C Improve Control ABC Incorporated’s customer wants ABC to apply Six Sigma problem solving methodology to insure that the body side subassembly is achieving Six Sigma quality levels of less than 3.4 defects per million for all critical body side subassembly dimensions. ABC needs an improvement strategy that minimizes the rework costs while achieving the desired quality objective. ABC’s goal is to produce module subassemblies that meet the customer requirements and not necessarily to insure that every individual stamped component within the assembly meets it original print specifications – sub-system optimizations vs. local optimization. A-Pillar Reinforcement B-Pillar Reinforcement Body Side Outer + + 3 D M A I Measure Phase Define Measure Analyze C Improve Control Key Variables: Assembly process variables: Weld Pattern (density), Clamp Location, and Clamp Weld Pressure Stamping process variables (body side): Press Tonnage, Die Cushion Pressure, Material Thickness Body Assembly Dimensions ASM_1Y through ASM_10Y Assembly Dimensions with Highest Defects 200000 172475 DPM 150000 100000 85824 50000 19786 3874 776 4 0 ASM_7Y ASM_8Y ASM_3Y ASM_9Y ASM_10Y ASM_6Y 4 Analyze Phase D M A I Define Measure Analyze C Improve Control Resolution alternatives (based upon past experience): 1. Make adjustments to assembly process settings 2. Reduce variation of components through better control of stamping process input variables 3. Rework stamping dies to shift component mean deviation that is off target and causing assembly defects Target Performance Level: All ten critical assembly dimensions at Six Sigma quality level of 3.4 DPM. Cp 2.0 and Cpk 1.67 Fish Bone and P-Diagrams: Understanding potential causes of defects. From this we pick the assembly and component dimensions that require further analysis 5 D M A I Analyze Phase Define Measure Analyze C Improve Control Environment Quality Component Variability Inspection Process Clamp Weld Pressure Clamp Location Methods For our analysis we will do a DOE to check for levels that contribute to better quality product. Material Thickness Humidity Gage R&R Weld Pattern (density) Inputs Temperature Operator Training Body Assembly Yield Strength Material Thickness Die Cushion Pressure Elastic Limit Materials Press Tonnage Machine Control Variables Clamp Location Press Tonnage Weld Density Die Pressure Clamp Pressure Body Side Sub-Assembly Stamping Process Yield Strength Outputs Body Side Sub-Assemblies at Six Sigma quality levels Noise Variables Environment Inherent Variation Error States Dimensional defects 6 D M A I Analyze Phase Define Measure Analyze C Improve Control Analysis of ASM_7Y and ASM_8Y Run Chart for ASM_7Y Run Chart for ASM_8Y 1.0 ASM_8Y ASM_7Y 1.0 0.5 0.5 0.0 0.0 2 7 2 12 4.00000 7.00000 5.00000 0.03464 0.96536 Number of runs up or down: Expected number of runs: Longest run up or down: Approx P-Value for Trends: Approx P-Value for Oscillation: 12 Subgroup Number Subgroup Number Number of runs about median: Expected number of runs: Longest run about median: Approx P-Value for Clustering: Approx P-Value for Mixtures: 7 6.00000 7.66667 3.00000 0.10778 0.89222 Number of runs about median: Expected number of runs: Longest run about median: Approx P-Value for Clustering: Approx P-Value for Mixtures: 4.00000 7.00000 5.00000 0.03464 0.96536 Number of runs up or down: Expected number of runs: Longest run up or down: Approx P-Value for Trends: Approx P-Value for Oscillation: 8.00000 7.66667 2.00000 0.59781 0.40219 XY Plot of ASM_8Y and ASM_7Y 1.0 ASM_7Y Conclusion: BS_7Y and ASM_7Y are following a similar trend. A correlation chart to study this further shows high correlation. (Pearson correlation, R of 0.701). 0.5 0.0 0.0 0.5 1.0 ASM_8Y 7 D M A I Analyze Phase Define Capability Analysis of B_7Y Capability of B_7Y USL 0 DPM Within Overall Potential (Within) Capability Cp 2.96 CPU 2.50 CPL 3.43 Cpk 2.50 Cpm * Overall Capability Pp PPU PPL Ppk 2.95 2.49 3.41 2.49 Improve Control Capability Analysis of BS_7Y Capability of BS_7Y LSL Process Data USL 0.70 Target * LSL -0.70 Mean 0.11 Sample N 36 StDev (Within) 0.0788122 StDev (Overall) 0.0791215 Measure Analyze C LSL Process Data USL 0.700000 Target * LSL -0.700000 Mean 0.899444 Sample N 36 StDev (Within) 0.149640 StDev (Overall) 0.383691 USL 698416 DPM Within Overall Potential (Within) Capability Cp 1.56 CPU -0.44 CPL 3.56 Cpk -0.44 -0.8 -0.6 -0.4 Observed Performance PPM < LSL 0.00 PPM > USL 0.00 PPM Total 0.00 -0.2 0.0 0.2 0.4 Exp. "Within" Performance PPM < LSL 0.00 PPM > USL 0.00 PPM Total 0.00 0.6 0.8 Exp. "Overall" Performance PPM < LSL 0.00 PPM > USL 0.00 PPM Total 0.00 Cpm * Overall Capability Pp PPU PPL Ppk 0.61 -0.17 1.39 -0.17 -1.0 -0.5 0.0 Observed Performance PPM < LSL 0.00 PPM > USL 666666.67 PPM Total 666666.67 0.5 1.0 Exp. "Within" Performance PPM < LSL 0.00 PPM > USL 908706.09 PPM Total 908706.09 1.5 2.0 Exp. "Overall" Performance PPM < LSL 15.33 PPM > USL 698400.06 PPM Total 698415.39 XY Plot of ASM_7Y and BS_7Y 1.3 Furthermore, BS_7Y shows strong correlation on dimension ASM_7Y. (Pearson correlation, R of 0.786). 1.2 1.1 1.0 BS_7Y Conclusion: B_7Y has 0 ppm compared to ~700K DPM in BS_7Y. 0.9 0.8 0.7 0.6 0.5 0.4 0.3 0.5 1.0 1.5 ASM_7Y 8 D M A I Analyze Phase Define Measure Analyze C Improve Control XY Plot of Tonnage vs. BS_7Y XY Plot of Tonnage vs. BS_7Y BS_7Y 1.5 1.0 0.5 905 915 925 935 945 Tonnage Conclusion: Tonnage values above 935 greatly improves BS_7Y and brings it closer to the mean. Let’s see what impact this has on ASM dimensions 7Y, 8Y, 9Y, and 10Y by creating a subset of the data looking only at Tonnage > 935. 9 D M A I Analyze Phase Define Measure Analyze C Improve Control Impact this has on ASM dimensions 7Y, 8Y, 9Y & 10Y on Tonnage Capability Analysis of ASM_8Y at Tonnage > 935 Capability Analysis of ASM_7Y at Tonnage > 935 Process Data USL 1.00 Target * LSL -1.00 Mean 0.09 Sample N 12 StDev (Within) 0.163174 StDev (Overall) 0.147855 LSL USL Within Overall * Overall Capability Pp PPU PPL Ppk 2.25 2.05 2.46 2.05 LSL Within Overall -1.0 -0.5 Observed Performance PPM < LSL 0.00 PPM > USL 0.00 PPM Total 0.00 0.0 0.5 Exp. "Within" Performance PPM < LSL 0.00 PPM > USL 0.01 PPM Total 0.01 1.0 Cpm Exp. "Overall" Performance PPM < LSL 0.00 PPM > USL 0.00 PPM Total 0.00 * Overall Capability Pp PPU PPL Ppk 3.74 4.22 3.26 3.26 -1.0 LSL * Overall Capability Pp PPU PPL Ppk 1.88 0.90 2.86 0.90 0.0 0.5 Exp. "Within" Performance PPM < LSL 0.00 PPM > USL 0.00 PPM Total 0.00 1.0 Exp. "Overall" Performance PPM < LSL 0.00 PPM > USL 0.00 PPM Total 0.00 Capability Analysis of ASM_10Y at Tonnage > 935 USL Within Overall Potential (Within) Capability Cp 1.62 CPU 0.78 CPL 2.46 Cpk 0.78 Cpm -0.5 Observed Performance PPM < LSL 0.00 PPM > USL 0.00 PPM Total 0.00 Capability Analysis of ASM_9Y at Tonnage > 935 Process Data USL 1.00000 Target * LSL -1.00000 Mean 0.52083 Sample N 12 StDev (Within) 0.206010 StDev (Overall) 0.177098 USL Potential (Within) Capability Cp 3.27 CPU 3.69 CPL 2.85 Cpk 2.85 Potential (Within) Capability Cp 2.04 CPU 1.86 CPL 2.23 Cpk 1.86 Cpm Process Data USL 1.00000 Target * LSL -1.00000 Mean -0.12833 Sample N 12 StDev (Within) 0.101825 StDev (Overall) 0.089161 Process Data USL 1.00 Target * LSL -1.00 Mean 0.39 Sample N 12 StDev (Within) 0.215541 StDev (Overall) 0.187663 LSL USL Within Overall Potential (Within) Capability Cp 1.55 CPU 0.94 CPL 2.15 Cpk 0.94 -1.0 -0.5 Observed Performance PPM < LSL 0.00 PPM > USL 0.00 PPM Total 0.00 0.0 0.5 Exp. "Within" Performance PPM < LSL 0.00 PPM > USL 10010.77 PPM Total 10010.77 1.0 Exp. "Overall" Performance PPM < LSL 0.00 PPM > USL 3408.51 PPM Total 3408.51 Cpm * Overall Capability Pp PPU PPL Ppk 1.78 1.08 2.47 1.08 -1.0 -0.5 Observed Performance PPM < LSL 0.00 PPM > USL 0.00 PPM Total 0.00 0.0 0.5 Exp. "Within" Performance PPM < LSL 0.00 PPM > USL 2326.72 PPM Total 2326.72 1.0 Exp. "Overall" Performance PPM < LSL 0.00 PPM > USL 576.00 PPM Total 576.00 Conclusion: Setting Tonnage to greater than 935 resulted in ASM_7Y and ASM_8Y meeting the goal of <3.4 DPM. ASM_9Y and ASM_10Y require further analysis. 10 D M A I Analyze Phase Define Measure Analyze C Improve Control DOE for Response Variable ASM_9Y • DOE factorial analysis shows Clamp Position is the only significant factor in determining ASM_9Y dimension Input Variable Proposed ASM_9Y Setting Proposed ASM_10Y Setting DOE Response Optimization for ASM_9Y Clamp Location Location 2 Location 2 Weld Density (welds per X inches) 1.33 1.33 • Set Clamp Position to Location 2Clamp (level Pressure1) 2100 psi 2100 psi • Optimizer recommends setting Weld Density to 1.33 weld per inch (level 1), but this appears to be a robust parameter, which could be changed for the benefit of process without reducing quality if processing time or cost shows a benefit. • Optimizer recommends setting Clamp Pressure to 2100 psi (level 1), but this appears to be a robust parameter, which could be changed for the benefit of process without reducing quality if processing time or cost shows a benefit. • Run additional tests at recommended settings to confirm results • Weld Density and Clamp Pressure are robust parameters and can be set to optimize the process capability to maximum level and lowest cost. 11 Analyze Phase D M A I Define Measure Analyze C Improve Control DOE for Response Variable ASM_10Y • DOE factorial analysis shows Clamp Position is also the only significant factor in determining ASM_10Y dimension DOE Response Optimization for ASM_10Y • Setting clamp to location 2 also improves ASM_10Y • Recommend same settings used to improve ASM_9Y to improve process capability which also allows for no changes to machine setup and helps reduce possible process concerns • Run additional tests at recommended settings to confirm results • Weld Density and Clamp Pressure are robust parameters and can be set to optimize the process capability to maximum level and lowest cost. 12 Analyze Phase D M A I Define Measure Analyze C Improve Control DOE for Response Variable ASM_3Y • DOE factorial analysis shows that no factors are significant • Response Optimization shows no solution for response optimizer Observe Process Capability of A_3Y and BS_3Y • ASM_3Y and A_3Y have a similar mean shift in the -Y direction Correlation of Output Variables • No dimensional correlations appear to exist between ASM_3Y and A_3Y or BS_3Y Stepwise Regression Analysis of BS_3Y • Tonnage and Die Pressure appear to be significant in determining dimension BS_3Y • Tonnage values < 920 may improve BS_3Y • Die Pressure appears to have no clear correlation to BS_3Y 13 D M A I Analyze Phase Define Measure Analyze C Improve Control Process Capability of BS_ 3Y and ASM_3Y at Tonnage < 920 • Created subset of body data looking only at dimensions with Tonnage < 935 • Tonnage < 920 appears to improve the mean of BS_3Y slightly, but has no impact on improving the mean of ASM_3Y. Capability Analysis of ASM_3Y Die remachined to move mean +0.80 Capability of A_3Y and ASM_3Y with +0.80 mm mean offset • Manipulate data for A_3Y and ASM_3Y by +0.80 mm to simulate re-machining Process Data USL 1 Target * LSL -1 Mean 0 Sample N 36 StDev (Within) 0.0851436 StDev (Overall) 0.0971725 USL Within Overall Potential (Within) Capability Cp 3.91 CPU 3.91 CPL 3.91 Cpk 3.91 Cpm • Process capability shows 0 defects for A_3Y and ASM_3Y with this mean offset LSL * Overall Capability Pp PPU PPL Ppk 3.43 3.43 3.43 3.43 -1.0 -0.5 Observed Performance PPM < LSL 0.00 PPM > USL 0.00 PPM Total 0.00 0.0 Exp. "Within" Performance PPM < LSL 0.00 PPM > USL 0.00 PPM Total 0.00 0.5 1.0 Exp. "Overall" Performance PPM < LSL 0.00 PPM > USL 0.00 PPM Total 0.00 14 Analyze Phase D M A I Define Measure Analyze C Improve Control Conclusions • From the analysis of ASM_7Y and ASM_8Y we can conclude that: • Setting tonnage > 935 results in ASM_7Y and ASM_8Y meeting the goal • Analyzing ASM_9Y and ASM_10Y helps determine that: • Setting clamp position to location 2, weld density to 1 weld every 1.33” and clamp pressure to 2000 psi helps with dimensions ASM_9Y and ASM_10Y • Analyzing ASM_3Y helps us conclude that: • Re-machine A-Pillar die to move A_3Y to nominal – which could cause BS_3Y to shift towards nominal – effectively shifting ASM_3Y to nominal 15 D M A I Analyze Phase Define Measure Analyze C Improve Control With the recommended changes the process performance will improve significantly Dimension Mean StDev Overall DPM_Obsv DPM_Within DPM_Exp Pp Ppk Cp Cpk ASM_1Y -0.035 0.165 0 0 0 2.01 1.94 2.47 2.39 ASM_2Y 0.259 0.152 0 0 1 2.20 1.63 2.31 1.71 ASM_3Y 0.000 0.097 0 0 0 ASM_4Y 0.009 0.115 0 0 0 2.90 2.87 3.53 3.50 ASM_5Y -0.330 0.145 0 0 2 2.30 1.54 3.72 2.50 ASM_6Y -0.284 0.160 0 1 4 2.08 1.49 2.24 1.60 ASM_7Y 0.090 0.148 0 0 0 2.25 2.05 2.04 1.86 ASM_8Y -0.128 0.089 0 0 0 3.74 3.26 3.27 2.85 ASM_9Y 0.521 0.180 0 0 0 ASM_10Y 0.395 0.191 0 0 0 16 Improve Phase D M A I Define Measure Analyze C Improve Control Recommendations for improving the process: • Set Tonnage to above 935 to improve ASM_7Y & ASM_8Y • Set Clamp to Location 2 to improve ASM_9Y & ASM_10Y • Re-machine the A-Pillar die to move the mean of A_3Y to nominal which in turn will move ASM_3Y to nominal Implement the above recommendations and run additional samples to verify results. 17 Control Phase D M A I Define Measure Analyze C Improve Control Recommended controls : • Implement a gauge on the body side component press to monitor tonnage • Implement an alarm and shut-off feature on the body side press if tonnage falls below 935 tons • Implement poke-yoke clamping fixture that ensures clamp is always in Position 2 • Establish an affordable control plan for ongoing monitoring of the 10 critical assembly dimensions. 18 Summary D M A I Define Measure Analyze C Improve Control ABC Incorporated is not achieving Six Sigma quality levels for all critical BodySide Sub-Assembly dimensions as requested by their customers. BBM needs to apply Six Sigma problem solving methodology to establish an improvement strategy that minimizes rework costs, yet achieves the desired quality objective. Bring the key process output variables within Six Sigma quality level of < 3.4 DPM. Cp 2.0 and Cpk 1.67 Set Tonnage to above 935 to improve ASM_7Y & ASM_8Y • Set Clamp to Location 2 to improve ASM_9Y & ASM_10Y • Re-machine the A-Pillar die to move the mean of A_3Y to nominal • Implement a gauge on the body side component press to monitor tonnage • Implement an alarm & shut-off feature on body side press if tonnage falls below 935 • Implement poke-yoke clamping fixture that ensures clamp is always in Position 2 • Establish control plan for ongoing monitoring of the 10 critical assembly dimensions. • 19