1996 Pollution Prevention Internship Final Project Report Intern: Jeff LeBlanc P.O. Box 216 Oxford, MA 01540 Home: 508-987-5036 Work: 603-898-8010 Ext 2343 Fax: 603-898-0526 E-Mail: jjlb@hopper.unh.edu Facility: HADCO Corporation Tech Center One 7 Manor Parkway Salem, NH. 03079 Contact Person: Lee Wilmot Corporate Safety, Health & Environmental Manager Phone: 603-896-2424 E-mail: lwilmot @hadco.com Marc Duquette Senior Safety & Environmental Engineer Phone: 603-896-2699 E-mail: mduquette@hadco.com 1 Table Of Contents I. Introduction.................................................................................................. 3 II. Executive Summary..................................................................................... 4 a. Water Recycling.................................................................................... 4 b. Mecer Filtration...................................................................................... 4 c. Mister......................................................................................................5 d. Diffusion Dialysis................................................................................... 5 III. Objective...................................................................................................... 6 IV. Water Recycling........................................................................................... 7 V. Mecer Filtration............................................................................................ 20 VI. Mister........................................................................................................... 26 VII. Diffusion Dialysis......................................................................................... 29 VIII. Appendix..................................................................................................... 31 I. Introduction 2 Hadco Corporation has a long history in pollution prevention techniques and environmental concern. Over the past thirty years, Hadco has strived to increase production while maintaining a perspective on environmental awareness. As a producer of printed circuit boards, the demand for chemical and water usage is high. Through pollution prevention techniques, Hadco has taken steps to limit these demands. This summer the goal was to further help Hadco in their effort to reduce waste. Specifically I concentrated on reducing water usage to limit the amount of waste water generated. By reducing Hadco’s water usage while maintaining their high record of quality, great savings as a result of reduced waster consumption could be achieved. A second area for waste reduction that was explored over the course of this internship was the recycling of spent nitric acid. Nitric acid is used in the solder stripper to strip any excess tin/lead solder left on the board. At the present time Hadco ships any spent solder strip off-site for disposal. By looking to reduce this waste, Hadco is now considering the implementation of new technology that would recycle this waste, thus reducing the amount of off-site shipments. By implementing new technology, and evaluating existing technology, Hadco has been able to reduce waste over the past few years. From water reduction to chemical reduction, Hadco has set unprecedented records in waste reduction. II. Executive Summary IIa. Water Recycling: 3 As a PCB Corporation, the requirement for water consumption is relatively demanding. Water is required for both industrial process as well as domestic usage. Hadco Corporation has preset limits for water consumption, mandated by Greater Lawrence Sanitary District (GLSD). With an increase in production, Hadco Corp. must now evaluate new technology and present process consumption to maintain operation within these set parameters. Process equipment was evaluated based on flow rates, and general cleanliness of the water. This value was determined from water analysis. Once flow rates and water data was known, suggestions could be made for water reduction techniques. In conjunction with in house water reduction techniques, vendors were contacted to make recommendations for the equipment that would be required by Hadco, to recycle current waste water. The final objective for this project was to perform cost analysis on all recommendations submitted by vendors. This allowed for a cost comparison. IIb. Mecer Filtration System. The Mecer filtration system is an on site etchant recycling system. The Mecer is designed specifically to handle ammoniacal etchant. Hadco Corp. Implemented this system in February of 1995 in their Salem Tech Center One facility. Due to the many problems experienced with the system over a period of 6 months, Hadco has since removed the Mecer system. However due to the tremendous cost of purchasing and disposing of ammoniacal etchant, Hadco now desires to evaluate the feasibility of re-implementation of a Mecer system. In order to perform this evaluation, original problems with the system had to be reviewed. Engineers and operators that worked on the original system had to be contacted and alarm logs had to be reviewed. In addition to evaluating past performance at TCI, other companies that have installed this system were contacted. These companies could then be compared to Hadco based upon process performance. IIc. Mister The ammonia etcher at Hadco is used to strip copper off the inner and outter layers of the printed circuit boards. Fumes exiting the front of the etcher pose a 4 hazard to both the operator and other plant personnel working in the area of the etcher. To minimize this exposure factor, a water spray mister has been utilized to diminish the ammonia fumes. A second purpose for this mister is to remove any residual etch that may accumulate on the rollers. However the water effluent contains high concentration of chelated copper. This concentration poses problems with waste water treatment. Such high concentrations are difficult to treat. It was the goal of this project to find a new manner in which the ammonia fumes could be treated so as to minimize the risk to workers and minimize concentration levels at waste treatment. IId. Diffusion Dialysis Diffusion dialysis is the process used to recover spent acid for reuse. This technology can be used in a PCB manufacturing environment to reclaim acid from spent baths. With a predicted reclaim of 85-90% of spent acid, this technology could pose a large savings to Hadco. At the present time Hadco Corp. is considering the use of this technology on their solder stripper to reclaim spent nitric acid. Hadco presently uses 2090 gallons of solder strip a year. This corresponds to a $27207 annual cost for purchase and disposal. By implementing diffusion dialysis technology, there is the potential for a $24486/yr savings. III Objective The main objectives presented at Hadco TCI this summer were: 5 1. Evaluate present process parameters and make suggestions for water reduction. 2. Contact vendors and evaluate their suggestions for technology required for water reduction. 3. Evaluate the Mecer system and evaluate the feasibility of re-implementation of the system to the TCI facility. 4. Develop a way in which the ammonia fumes from the mister can be treated while at the same time limiting copper sent to waste treatment. IV. Water Recycling Due to increases in production, Hadco Corp. now finds that it must evaluate present process parameters to maintain operation within GLSD set parameters for water usage. This project started by recording all flow rates for each process 6 within the TCI facility. Since some of the process machinery was not equipped with flow meters, in many cases this required entering the trench, following pipes, and measuring flow rates with a bucket. Also noted for each process were counter flow measures, flow restrictors, board sensors, conductivity controllers (where applicable) and the type of water (i.e. DI or city water). This information was added to a database created for water consumption. Samples were taken from each rinse tank every week and tested for conductivity (s), pH, totally dissolved solids (mg/l), copper(mg/l), and lead (mg/l). These tests were repeated over a seven week duration. The reason for seven weeks of testing was to develop a spectrum of data that would allow for true maximum and minimum values to be seen. During the seven weeks of testing, all disposition streams were verified by entering the trench and following the piping. Upon completion of the sampling and testing, averages were calculated for each rinse tank. Two databases were then developed from this information. One database contained the average values, while the second database contained the maximum observed values. A copy of these two databases can be seen in the appendix section IA. of this report. By observing the recorded data, changes to the process could then be suggested. Suggestion were based upon cleanliness of the water, determined by conductivity and TDS. After reviewing the collected data, it was found that much water could be conserved at the TCI facility. The following graph shows the processes and the amount of water that could be conserved. 7 Potential For Water Savings 6000 5000 Gallons / Day 4000 3000 2000 1000 0 Final Clean Dep/Des O/L Strip Oxide 8 Ni/Gold Solder Strip I/L Strip One area in which water consumption was able to be reduced was the black oxide line. From the collected data, it was found that the effluent from the DI rinse was cleaner than the feed to the city water rinse. Therefore the suggestion was made to counter-flow of the DI effluent to the city water rinse tank. Below you can see the original setup followed by the changes made as a result of the data testing. These changes yielded a savings of 3.25 gpm with a cost savings of $ 8640.64/yr. The additional 0.75 gpm was added to rinse #18 to improve rinse quality after the entek bath. After evaluating the collected data, it was determined that the flow rate could be lowered from 3 to 1.5 gpm. Water quality was monitored daily for a two week duration following these changes to insure quality. The rinse water in stations 15 and 14 were found to improve due to DI water addition. 9 A second area in which water reduction was targeted pertained to the Nickel/Gold line. By reviewing the collected data, once again counter flow options were suggested. Below you can see the previous and new setup. Caution had to be taken so as not to contaminate any of the baths on this line. By working with the process engineer an estimated 2.5 gpm of rinse water was saved. This resulted in an annual savings of $1767.33. Again, the rinse water quality will be analyzed daily for a two week duration to insure the quality of the water. Another area in which it was found possible to conserve water was the solder stripper. After the board goes through the nitric acid bath, it then moves through two rinse stages. The first rinse stage is a feed and bleed recirculating rinse tank with a flow rate of 3 gpm. The second rinse consists of two spray rinses. The water enters the stripper via a direct line and is used for the second spray rinse. It is then collected in a basin at the bottom of the stripper. From there it is pumped back to the top of the machine and used in the first spray rinse. 10 Following this procedure the water is discarded to WWT. The flow rate for the second rinse is 5 gpm. From testing the water, it was found that the exiting water from the second rinse was clean to the point of acceptance for use as the feed for the first rinse. The flow rate for the second rinse could not be turned down to match the flow rate of the first rinse due to the fact that the high flow rate was required to maintain spray pressure. So by counter-flowing the second rinse to the first, 3 gpm will be saved resulting in a savings of $1595.19/yr. This should also improve the quality of the water in the first rinse due to the fact that water will be fed and bled off at a greater rate. A diagram of this change can be seen below. 11 By reviewing water data for the inner layer stripper, it was found that effluent water was not contaminated to the point of disuse. There were two options on what to do with the water at this point. The first option was to run the water through a filter and into a recirculation tank. This would close-loop the water for the inner layer stripper for a time interval to be determined. The second option was to simply decrease the flow rate to the stripper. By working with the process engineer, it was determined that the best choice would be to lower the flow rate to the system. By recirculating the rinses, chemistries within the solution would have concentrated to unacceptable quality levels. Therefore, the decision was made to turn down the flow rate from 3 gpm to 2 gpm. This produced a water savings of 600 gpd resulting in a $1292.91 annual savings. Again, the water quality was monitored daily over a two week interval to insure quality. The final clean was found to have effluent as pure as the feed water. I proposed adding a 20 micron filter and recirculating tank to this system to closeloop the water usage. The final clean presently runs at 4 gpm. However, due to new technology being implemented at Hadco, the final clean machine will be replaced in one month. For these reasons, this water reduction technique was deemed unnecessary. I am presently working with Technics, the vendor which implemented the software on the deposition line to establish a way in which water usage can be regulated on this line. At the present time, the deposition line is operated about 20 hours a day. During this time, the line is only utilized for work 12 out of the 20 hours. The remainder of the time, the line is left running to maintain the baths. Many times, the operators will leave the water to the rinses running, while no work is being processed for those 8 hours. Water regulation in this area will have a significant impact on water control at Hadco TCI. To control water consumption on this line, Technics is investigating the feasibility of implementing two photoelectric switches on the front of the deposition line. These switches will in turn send a beam through the racks in which the boards are placed. If the rack is found not to contain boards, then the beam will not be reflected. However, if there are boards in the rack and the beam is reflected, a signal will be sent to a timer and a motorized ball valve that will activate the rinses for the duration of the time it takes for the rack to pass through every stage. This technology would allow for a 5520 gpd savings, corresponding to a annual savings of $12229.83. To sum up all conservation measures recommended to Hadco, the table below shows the estimated water savings: 12 Process Deposition Etcher I/L Strip Nickel/Gold Oxide Solder Strip Old Flow (GPM) 11.50 220 GPD 3.00 5.50 10.75 8.00 New Flow (GPM) 11.50 50 GPD 2.00 3.00 7.50 5.00 TOTALS Savings (GPM) 0.00 0.00 1.00 2.50 3.25 3.00 Savings (GPD) 5520 150 600 600 3900 720 9.75 11490 This is a 17.6% savings in Hadco’s total daily water consumption. The savings from these expected changes can be seen in the table below: Amt. Water GPD 10890 (Cw) 600 (DI) TOTAL Cost Per Kgal $ 6.07 8.07 Total Savings $/Day 66.1023 4.842 70.9443 Total Savings $/Year 24127.33 1767.33 25894.66 After all in-house water conservation techniques had been exhausted, outside vendors were contacted to make suggestions to further help Hadco reduce water usage. The implementation of the above in-house water conservation measures will not guarantee that Hadco maintains water compliance during busy times. To insure future compliance vendors were asked to speculate on a 20-30 gpm water recycling system. Vendors that were contacted include: Kinetico Manchester Corp. Remco Engineering U.S. Filter Memtek Dynatec Selection was based upon reference from Hadco personnel. All vendors were supplied with the collected water data averages and maximums. Quotes from the vendors were then obtained for evaluation. Cost analysis was performed on all quotes received from the vendors. This entailed acquiring a current water bill from the town of Salem, a current electric 13 bill from Granite State Electrical, and the schematic breakdown for sludge pricing. Before a final decision on pilot testing can be made, the decision must be made whether to implement an IX or RO system at Hadco. Both systems offer various advantages and limitations in daily operation. Below is a list for the advantages and disadvantages for each system. IX system Advantages: Quality of recycled water would abolish need for DI resin columns Recycled water could be used for bath make ups High metal removal efficiency Recycled water would have a TDS level of 1 ppm. High reclaim ratio (in %) Lead/Lag setup allowing for zero down time while cleaning/performing maintenance. Possibility for metal recovery through Electrowinning IX system Disadvantages: Limited feed streams Potential for resin fouling High initial cost Lower TDS feed limit Poor organic removal RO system Advantages: Lower cost High metal and organics removal Consistent water quality Higher TDS feed streams RO system Disadvantages: 14 Reclaim ratio (around 65-70% w/out more expensive membranes) Potential for membrane fouling More expensive in annual maintenance Lower quality in recycled water (usually 10% of TDS fed) Potential hazard when using water for bath make ups Water must be treated with DI resin columns to produce DI water Cleaning Time may incur unacceptable down time for permit levels. A schematic for each system can be seen as follows: 15 It is recommended that vendors be sent a second copy of water data with the updated technology. This will have to include the data on the PAL line, data on the new developer, and data on the new chem clean system. Based upon the initial proposals from the vendors, I would recommend that Hadco consider a treatability study followed by the pilot testing of a Kinetico IX system. This recommendation is based upon many researched findings. The first thing to consider was the company background. As large manufactures in water recycling, Kinetico has over twenty years of knowledge in water recycling technology and how it relates to a PCB manufacturing environment. The company has over 300 systems installed in this type of manufacturing background. The most important point considered was the quality of the effluent water proposed by Kinetico. Kinetico has proposed an Ion Exchange system which will recycle water to DI quality. With the regenerated water being of DI quality, there would no longer be a need for present resin columns used to generate DI water. Recycled water could be used in all plating baths and rinses without concern of chemical reaction and/or contamination. Secondly, by using the ion exchange system, the possibility for metal recovery also exists. This would produce a revenue stream to help offset the initial costs for the equipment. The Kinetico design proposes a 90 to 95 percent reclaim ratio on the spent water. This was the highest reclaim ratio proposed out of all the vendors. Other vendors, while proposing quality systems were excluded based upon the following reasons. Dynatec: Dynatec proposed the use of an RO system for the TCI facility. However without Hadco putting up the initial cost for a treatability study, Dynatec was reluctant to specify possible recycle streams, size of the required RO, and cost for the system. It was also stated in the information packet received from Dynatec that even after passing through the membrane columns, it is possible that the recycled water would not be acceptable for all rinse applications. To further treat the water the use of DI resin columns would be required. It is possible that the recycled water from this system would cause chemical reaction and therefore could not be used for concentrated bath make ups. Remco Engineering: Remco Engineering was found to be an “off the shelf” distributor of water recycling technology. Based upon the proposal received from Remco, it was determined that this company would not be able to provide the knowledge required to service the unit. US Filter: 16 While a quote has yet to be received from US Filter, it was the feeling of their sales representative that US Filter would suggest the use of an RO system for Hadco. Since there was no proposal available for review, I could only review the experience of the company. It was discovered during review that while US filter has much experience in water purification, their experience with how this relates to a PCB manufacturing environment was limited. To further investigate this factor, I visited Elexsys Corp. located in Nashua, NH. The company is using a US Filter RO system to recycle spent waste water. What I found at Elexsys was that while the system was working to acceptable levels, the company was only able to achieve a reclaim ratio of 65%. Secondly, the effluent water was found to have a TDS of typically 10% of the feed to the unit. This produced water that while Elexsys claimed was pure, they were not using for concentrated bath make ups. Manchester Corp: Manchester Corp. was the company that designed the existing conventional waste treatment system (CWTS) in the TCI facility. Manchester proposed an RO system for Hadco to consider for water recycling. Manchester’s design for this system did have a few drawbacks. First, the maximum expected reclaim ratio was 80%. With such a low reclaim ratio, the quality of the reclaimed was expected to be of DI quality. However, this was not found to be true. The system that Manchester designed would require the use of resin columns to further treat the water to obtain DI quality. Another drawback to the Manchester system was the cost. This system was priced roughly equal to the Kinetico system while the water quality proved to be poorer. Also due to the nature of the RO system, no metal recovery could be utilized to offset the initial cost. Finally an RO cleaning solution would have to be purchased to clean the membrane. This could prove, pending upon the annual cost of the solution, to make the cost of this system greater than the Kinetico system. Memtek: While a proposal has yet to be obtained from this company, the objective of Memtek has been made known to Hadco. Memtek, while considering water recycling technology, is also evaluating concentrated baths for an ERU system. It is their feeling that by recovering the metals from the concentrated baths, the generated revenue will offset the cost for the water recycling technology. However, this approach may be a more aggressive approach than Hadco is looking to take. In the long run, the extra plating equipment and engineering services required to determine what could/could not be plated may end up costing Hadco more in an initial cost than previously listed vendors. 17 When performing a cost analysis on the vendor technology, many factors had to be considered. Most of the streams that the vendors recommended for recycle were low TDS and Cu streams. For this reason when performing the cost analysis the present chemistry cost was not considered to decrease with the implementation of a water recycling system. With the implementation of a recycling system, the present flow rates to the conventional waste treatment system (CWTS) would be reduced, allowing for a greater contact time. In this case the pumps would require the same amount of energy to pump water at a lower flow rate. Therefore, the electricity cost was considered to stay the same for the CWTS. The addition of a water recycling system would actually increase power consumption, imposing a larger cost for electricity. In the case of an Ion exchange system, the cost for resin replacement had to be taken in to consideration, whereas for a reverse osmosis, the cost for membrane replacement must be considered. The final consideration was the amount saved from water reduction. For each recommendation given from a vendor, all these facts were summed up and an expected payback was calculated. One consideration when performing the cost analysis was the chemical cost. When I first started to perform the analysis, the WWT department had no log for chemical usage. If a specific quantity had to be known, an operator would have to pull all prior purchase requisition forms and sum the quantities. This could prove to be a tedious task for tracking annual usage. For this reason, I developed a WWT chemical usage log. This log can be seen in appendix section IB of this report. The log allowed the operators to know how much they use of a specific chemical on a daily basis. This will also easily allow them to track chemical usage on an annual basis. By working with Rich Slager, (WWT operator) I was able to establish the chemical cost to treat the water on a daily basis. By knowing this amount, I was then able to calculate chemical cost per Kgal of water. This value could then be compared to the national average posted by the EPA. Since most streams being considered for recycling purposes, consist of low copper concentration, and a TDS level, chemical cost was considered to remain unchanged when determining chemical cost. A second value that had to be considered when performing the cost analysis was the sludge cost per Kgal of water. If a recycling system was designed to remove metals from the rinse water, a sludge reduction would be observed. Again, prior to performing these calculation Hadco TCI did not know their sludge cost per Kgal of water. By contacting Franklin Environmental, I was able to obtain the pricing matrix for sludge removal and treatment. These values could be used in the future to perform cost analysis if deemed necessary. 18 V. Mecer System The Mecer system, designed in Sweden by Sigma Maeb Corp. is an on site etchant recycling system. The system is specifically designed to treat ammoniacal etchant. The theory behind the machinery is the copper in the 19 spent etch and rinse water would be plated out using an Electrowinning unit. Various chemistries are required to remove the copper from the spent etch and water. A schematic of this process can be seen below. As you can see from the schematic, an organic solution is used to remove the copper from the etchant. The copper depleted etchant is then returned to the etcher for reuse. The organic is then combined with the rinse water, and the copper is removed from the rinse water. The copper depleted rinse water can then be recycled to the etcher for reuse. The organic solution containing the copper from the etchant and water is then mixed with sulfuric acid to produce copper sulfate. The copper sulfate is then sent off to the electrowinning process for copper recovery. While this system is designed to replace the contemporary feed and bleed system, fresh etch must still be added to the etcher by the use of a density meter to maintain proper operation parameters. However, the amount of fresh etch required would be reduced by 80-90%. 20 Hadco TCI experienced many problems as a result of the implementation of the Mecer system. The first problem experienced was due to flow imbalances upon start up of the system. This was followed by dendrite formation in the electrowinning unit. The copper spike built up between the anodes and cathodes would cause the system to short out. Another problem experienced was resist lift from the boards. This problem was experienced due to Hadco using this system for inner layer etching as well as outer layer etching. Chronic alarms posed a serious problems with this unit. Alarms constantly called for etch/water to be added or removed from the system. A copy of the Mecer alarm log can be seen in the appendix section IIA of this report. As can be seen from the alarm log, this unit required constant monitoring by Hadco personnel. The system was also shipped with a defect in the electrowinning unit. The fiberglass casing had a crack in it, causing the unit to leak and trigger alarms. However, it should be noted that Hadco was not alone in experiencing these problems with the Mecer system. Over the course of my evaluation, I contacted companies both domestic and overseas (overseas companies were limited to European) to obtain their perspective of the Mecer system in its daily operation. The companies consisted of: Circo Craft (Canada) Ericcson (Kumla, Sweden) H&L Electronics (Atlanta, Georgia) Praegitzer (Washington) Printed Circuit Corporation (Woburn, Mass.) Spei-Orion (Italy) Out of all the companies I contacted, 100% of the companies experienced problems with dendrite formation in the electrowinning unit. Some companies after a year of operation still experience this same problem. Out of all the companies I contacted that use this system for both inner and outer layer etching, 100% of the companies experienced problems with resist lift on the inner layer boards. Most companies experienced flow imbalances upon startup of the unit, and two companies that I contacted experienced similar chronic alarms problems as Hadco experienced. One problem that Hadco did experience solely was the problem with fine line etching by using the Mecer system. Hadco was the only company that has installed the Mecer and etches below 4-5 mm lines and spaces, that I was able to discover during the coarse of my evaluation. Therefore, it remains unknown as to whether or not the Mecer system can reproduce etch with the quality to handle fine lines and spaces. However to better evaluate this matter, I arranged for boards to be sent to a company by the name of H&L electronics located in Georgia. This company has been using the Mecer system for two years, and has the capability to etch to 4 mm lines and spaces. Upon reviewing the etched boards from H&L electronics many interesting conclusions were drawn. All the boards etched on H&l’s etcher were over etched. From this we concluded that in order to control a copper 21 footing, H&L slowed down the speed of their etcher. This in turn would cause for an over etch when dealing with smaller patterns. The second item that we found interesting when reviewing the boards, was that in certain areas, the copper had been etched from under the resist film. This shows the same problem that Hadco experienced when using the Mecer system. During the coarse of my evaluation, I had the opportunity to visit Printed Circuit Corporation (PCC) in Woburn, Mass. PCC implemented the Mecer system in their facility two years ago. Upon start up they experienced immediate problems with flow imbalances and dendrite formation in the electrowinning unit. PCC also experienced problems with resist lift and chronic alarms with the system. While it was speculated that one of the problems with the Mecer at Hadco was due to the extended distance the Mecer was located from the etcher, I found this to be an insignificant cause through my visit at PCC. PCC has their system set up such that the Mecer is located a distance of 300 ft. from the etcher. No additional problems were experienced as result of this extended distance. One major contrast that was found about the Mecer system as a result of this evaluation was the level of support and service that each company received. All European companies that I talked to about the Mecer system had no complaints about the level of service they encountered. These companies, however, received their support from Sigma directly. In the United States, all companies I talked with dealt with Cognis, the US licensed vendor for the Mecer system. Opinions on service quality varied based upon level of difficulty experienced with the Mecer system. Those companies that only experienced problems due to dendrite formation as a result of start up replied that service was adequate, if not better, from Cognis. Those companies that experienced more complex problems as a result of start-up such as flow imbalances, resist lift and chronic alarms reported that service from Cognis was poor and unacceptable. This was due to the lengthy time span experienced from the moment a problem occurred to the time Cognis would arrive to evaluate and assist in correcting the problem. Cognis in the case of EPROM’s at Hadco actually made the problem worse with their corrections. It was admitted by a Cognis representative that visited Hadco that during the initial stages of Cognis being a vendor that the technology was new to them. They may not have had the proper amount of knowledge initially required to sell and service the Mecer to US companies. As a result, US companies implementing this technology, were limited to the quality and quantity of service they received. Even with the lack of experience and support from Cognis Corporation, all the companies I contacted in the US were able to get the Mecer system to work. It should be noted that for most companies it took at least one year to debug the machine and get the system to work in a proper manner. The companies I talked to in the US set up their system in such a way that the Mecer system could be shutdown and switched over to the conventional feed/bleed system by 22 the turn of a few valves. This saved in down time as a result of plumbing requirements to convert from one system to the other. Out of all the US companies I talked with, 100% of the companies stated that the first year of debugging posed many frustrations as a result of having to learn how to react to the system and handle the resulting problems. By reviewing the amount of spent etch used three months before the Mecer went on-line, during the Mecer usage, and for three months after the Mecer was turned off a percentage savings from the Mecer could be determined. It was calculated that an 87% savings in etchant usage was experienced while the Mecer system was in operation. This can be seen from the following graphical representation for etchant usage over this period. Drum Off-site shipments 93/94 14 12 # of drums shipped 10 8 6 4 2 0 11-Jan 1-Mar 20-Apr 9-Jun 23 29-Jul 17-Sep Other factors that had to be considered were scrap due to under and over etching, and missed deliveries. However, due to non-documented scrap figures, the overall estimate for scrap during this time could not be determined. Since TCI is a “quick turn” board shop, any down time experienced with the etcher would cause late or missed deliveries. By not installing the Mecer system such that to convert to the conventional feed/bleed system only required the turn of a few valves, much down time was experienced. In a shop such as TCI, this was not an acceptable result. On a final note, 100% of the shops I talked to were able to successfully get the Mecer system to run after at least one year of frustration and debugging. All US companies suggested not dealing through Cognis, but rather through Sigma Corporation directly. With the sudden decline in Cognis, the future in US Mecer sales will rely solely on Sigma Corp. in Sweden, or the development of a new US licensed vendor. It is my recommendation that Hadco Corp. take a slow approach to the Mecer system. I recommend that Hadco waits to consider implementing a new Mecer system until a new US distributor has been established. The reason for this recommendation is based upon the required amount of service this unit will require when installing and initially operating. Without a US vendor, I do not feel that Hadco would receive the level of support needed to successfully start up the Mecer system. Pending a new vendor is found, I would recommend that Hadco try and implement a new Mecer system under the following conditions: An individual is dedicated to the system as a sole project until installation and continuous successful operation has been obtained. A contract be negotiated such that Technical Assistance be provided when ever necessary, and on-site service provided without extenuous delays. The system be given at least a year and a half to allow for all bugs to be worked out and operational parameters to be established. The system be installed in such a way that to convert from the Mecer to the conventional feed/bleed requires nothing more than the turn of a few valves. This set up would minimize down time experienced as a result of the Mecer system. 24 VI. Mister Hadco Corp. uses an ammoniacal etch to etch copper off the printed circuit board. Conveyerized rollers are used to carry the board through the etcher. On the front of the etcher, a spray is used for two purposes. The first purpose is to knock down any ammonia fumes that may be escaping the front of the etcher that would pose a health hazard to plant operators. The second purpose is to clean any residual etch off the rollers that would damage the board. The problem that Hadco is experiencing with the mister, is that spent etch is escaping out of the chamber inside the etcher and mixing with spent mister water. The mister produces, at the present time, 220 gallons per day to be sent to waste treatment. If the spent mister water contained no etch, it could be treated in the CWTS without further problems. However, since etch is mixing with the water, the water now has a copper level of 1776 ppm. The mister is presently plumbed to the non-chelated batch tank so that the spent mister water, containing etch can be treated in the Romar reactor. While this system works to treat the water, the large amount of water that needs to be treated on a daily basis does not allow for other waste to be treated. The result was an excess amount of waste that had to be shipped out at a large expense. The approach to this project was to evaluate first-off why the etch was entering the mister chamber. By meeting with the technician for the etcher, it became clear that by the design of the machine, etch was going to spill into the mister chamber. The next step was to see how other Hadcofacilities using the same equipment were handling this matter. By talking with the Steve Raper (environmental engineer) at Hadco Hudson, I was able to determine how they handled spent mister water. After visiting the Hudson facility, I had a basis for comparison between Hudson’s etcher and the etcher at TCI. I found that the etcher at Hudson was only using 12 GPD of water and was vented slightly different than etcher at TCI. After examining the mister on the TCI facility, it was found that one of the atomizers(spray nozzles) was not functioning properly and was releasing more water than expected. By reviewing this information with the Dave Pratt, (process engineer at TCI) we were able come up with four affirmative 25 actions that could be taken to control the problems being experienced with the present mister setup. These actions included: Placing new, smaller if possible, atomizers on the mister Placing a flow restrictor on the feed to the mister Setting the mister to run on the board sensor located on the front of the etcher Possibly reusing some of the spent mister water to control chloride levels in the etcher A flow restrictor set for 1 gpm was next placed on the mister feed to control the amount of water. This in turn reduced the quantity of water to 150 gpd. A second flow restrictor was then installed set for 0.5 gpm. At the same time new atomizers were installed to replace the defective ones. This then reduced the flow rate to 73 gpd. The next step in this project will be to attach the mister to the board sensor located on the front of the etcher. It is expected that the board sensor will reduce the water consumption by 1/3, thus reducing the mister flow rate to 50 gpd. This was the targeted goal at the beginning of this project. A flow of 50 gpd, could be treated in house without further complication to WWT. For a cost analysis on this project, I first calculated what it would cost to run the mister 24 hrs/day, 7 days a week at the 200 gpd flow rate. The cost break down for the mister breaks down into two categories. The first is the chemical cost to treat 700 gpw of spent water, while the second category consists of the shipping cost to ship out the remaining spent water. The two tables below show the breakdown for these costs. Chemical Costs Chemical Quant. (lb/day) 377.6 TOTALS Chemical (Cost/lb) Total Cost/Day 209.1415 Total Cost/Yr 74245.23 Shipping Costs # of drums/wk 13 Cost to ship drum 250 Cost/wk 3250 TOTAL EXPENSE : 243,245.20 / Yr. 26 Cost/yr. 169,000 This large expense and damage to WWT is the present reason for the mister not being used. With the planned modified changes to the mister, a new cost was then calculated. This can be seen in the below table. Future Expected Costs Amount Mister Water (GPD) 50 Chemicals Cost/day 52.58 Total Cost/yr. 18,559.40 TOTAL EXPENSE : 18,559.40 These changes produce a tremendous cost avoidance of $224,685.80/yr as can be seen from the above tables. The changes will allow Hadco to operate the mister in a cost effective manor while at the same time not placing a tremendous burden on WWT. 27 VII. Diffusion Dialysis Diffusion dialysis is a process used to reclaim spent acid from concentrated baths. The process was reviewed for implementation on Hadco’s solder stripper. Hadco purchases solder strip from MacDermid Corp. under the trade name of Eliminator III. The solder stripper uses a 25% by weight nitric acid to remove a Sn/Pb solder from the circuit boards. The remainder of the Eliminator III consists of a proprietary mixture. A schematic of the diffusion dialysis setup can be seen in the below diagram. The theory behind diffusion dialysis is that spent acid will be placed in contact with one side of an anionic ion exchange membrane. Simultaneously water is placed into contact with the recovery side of the membrane. The majority of the acid migrates through the membrane into the water, leaving contaminants and 28 heavy metals behind. The purified acid would then be returned to the process tank for reuse, while the concentrated contaminant and metal stream would be sent for metal recovery or to WWT. At the present time MacDermid Corp. is testing this technology on Hadco’s spent solder strip. MacDermid is developing a replenisher solution that would have to be added to the recovered nitric acid to account for the rest of the proprietary mixture that was lost as a result of passing through the membrane. By talking with a MacDermid representative, I was able to evaluate the present status of this project. I was able to learn that MacDermid has been able to successfully recover 80% of the spent nitric acid out of the solder strip. They are now designing the replenisher that would be required for the recovered acid. Pending completion of this, MacDermid will test the recycled Eliminator III on Hadco’s solder strip to insure that Hadco can maintain a high quality level of operation. At the present time it was calculated that Hadco will purchase 38 drums of Eliminator III for the entire year of 1996. This would produce an annual cost of $19878 to purchase the mixture, and $7,332 to dispose of the spent solder strip. This yields a combined cost of $27,210/yr. With the recovery of 80% of this spent solder strip Hadco would save $21,768 before including the cost of the replenisher solution. A cost analysis can be performed when the cost for the replenisher solution becomes known to Hadco. By contacting Pure Cycle, a vendor for diffusion dialysis, it was determined that Hadco would require a 5 gpd system to recover the spent solder strip. The cost for a system of this size is $8,800. Cost effectiveness for this machine will be decided upon completion of successful testing of MacDermid recycled solder strip on Hadco’s solder stripper. 29 VIII. Appendix 30