Ice Pigging - Award Winning, Pipe Cleaning Technology Using Ice Paul Treloar – Utility Service Group ptreloar@utilityservice.com ABSTRACT Sediment fats, oils, greases (FOG) and debris accumulation in wastewater collection systems clog force mains and siphons causing pipeline restrictions. Restricted flows can cause increased energy use, increased sanitary sewer overflows and can lead to capital improvements including increased pumping capacity and force main replacement. Current approaches to clean force mains such as cleaning with hard pigs and soft swabs present a risk because hard pigs can get stuck in the force main causing a need for emergency excavation. Excavating to retrieve a hard pig is costly, time consuming and in some cases with highways, river crossings and developed areas, is not an option. Where redundant systems do not exist, the cost to install a temporary by-pass system may be enormous. Other technologies, like flushing and water-jetting are inefficient and sometimes ineffective. In addition, these processes use a lot of water which may not be readily available. This paper describes a new technique for cleaning potable water, sewer force mains and siphons using an ice slurry called, Ice Pigging. KEYWORDS: Ice pigging, pipe cleaning, sewer force mains, sewer siphons, benefits. INTRODUCTION Developed by the University of Bristol, England, Ice Pigging is an award winning, innovative, low risk, advanced pipe cleaning technology to clean force mains, siphons and better manage pipeline assets. Utility Service Group (USG) is the sole rights holder in North America. Ice Pigging has been proven to be between 100 and 1000 times more effective at removing sediment and debris than water flushing alone. The ice slurry can be inserted and removed through line taps, air valves, and other existing fittings so expensive excavations are not required. Ice Pigging harnesses the characteristics of a semi-solid material that can be pumped like a liquid but behaves like a solid once the pig is formed in the pipe Because Ice Pigging relies on the natural glacial effect of ice to pick up unwanted sediment it uses approximately 50% less water than standard water flushing and takes significantly less time, typically the section of main being cleaned is out of service for no more than 30 minutes. Traditional cleaning methods do have operational limitations that Ice Pigging can overcome. A main feature of Ice Pigging is that it cannot get stuck, if for some reason the pig would get stuck, we would allow the ice to melt and flush it from the main. Pipe bends, changes in diameter or butterfly valves can all pose problems for swabbing or pigging, yet ice pigs can easily negotiate these obstacles. To launch and receive traditional pigs, excavations have to be made to allow the installation of launch and reception stations. This can mean costly, extensive interruptions to force mains and siphons and require the installation of bypass pumping. The Benefits Ice Pigging represents a sustainable best practice over traditional approaches to force main cleaning: It is efficient, rapid and environmentally friendly. It combines operational benefits of flushing with the impact of solid pigging. Ice Slurry injects through existing fittings. System pressure pushes ice. Suitable for pipes of all sizes and materials. It effectively removes biofilm, iron, manganese, FOG, grit and sediments. Approximately 50% less water is wasted. Produces quantifiable results. Exceptionally low risk. Figure 2. French press method of testing the ice fraction Methodology To maintain the correct consistency of the Ice Pig, a freezing point depressant is used. USG uses food grade, fine table salt (NaCl) which is approved by the National Science Foundation (NSF). This is dissolved in potable water which is always sourced from the public water supply. The current maximum batch capacity for USG is 2,700 gallons. The brine is made in a 316 stainless steel delivery tanker and hose connections are made to the ice machines that are mounted on a separate trailer (Fig.1.). The brine is fed into the ice machines which, in turn freeze the liquid and return it to the delivery tanker. This cycle continues until the ice slurry is at thickness known as the ice fraction. Ice fraction measures the amount of ice crystals as a percentage of total volume. Ice fraction is related to the cooling capability of the slurry compared to pure ice (100%); this is known as the Calorimetric Value. Ice Pig operators use a simple French press coffee plunger (Fig.2.) to test the “ice fraction” (or the ice thickness) on site prior to pumping into the main. Typically, the thickest ice is used on plastic and sound concrete lined pipes as well as asbestos cement, but when older unlined cast iron pipes are cleaned, a thinner ice slurry is used that does not clean as aggressively. The thinner ice slurry will not to disturb the buildup of tuberculation which could damage the integrity of an old heavily corroded unlined cast iron pipe. Ice Delivery Figure 1. Ice production setup showing the delivery rig (left) and ice machines (right). Setup for delivery varies slightly for each different application. A typical setup for a potable water main is shown below (Fig.3.). The delivery rig connects to the inlet hydrant or other suitable fitting (2” or greater tapping with valve control), and at the outlet, a Flow Analysis System (FAS) is connected. The FAS measures and records the flow, pressure, conductivity, turbidity and water temperature as the water and ice are discharged. Once set up, the main is flushed briefly to note and record pre-flush readings. The main is then isolated by the owners’ operators and the required amount of ice is pumped into the main. At the same time, the outlet hydrant is opened to create a flow and allow water to be displaced as the ice enters the main. With careful control between the inlet and outlet, the flows are balanced to allow slightly more ice into the main than the amount of water being displaced. This has the effect of the ice forming as a pig against a pressurized wall of water. Figure 3. Typical potable water main setup Once the required amount of ice is in the main, the delivery pump is turned off and the upstream valve is opened to allow the system flow and pressure to “push” the ice pig along the main toward the outlet hydrant. The flow rate is controlled by the outlet operator at this time. As the ice pig approaches the outlet, the conductivity reading will rise as the salty water of the melting pig arrives in front of the pig. The monitoring equipment will show the water temperature falling and conductivity rising as the ice arrives. At this stage, the operator may collect samples of the ice at regular intervals for later analysis. (Fig. 4.) The temperature and conductivity will return to pre-flush levels when all the ice and salty water has flushed out of the system and the flushing shall continue briefly to allow the turbidity levels to return to pre-flush levels or lower according to instructions from the owner. The main is then returned to normal service. No disinfection is necessary. Figure 4. Taking samples Sanitary Sewers: The setup for sewer force mains and siphons is similar to the water main set up detailed above, except no monitoring equipment is used on the outlet. Instead, the ice is pumped to a gravity main or the WWTP. (Figs. 5. & 6.) The delivery rig will connect to a suitable fitting for ice insertion. This may be an existing fitting such as an air release valve (ARV) or a lift pump by-pass fitting. In the event there are no existing suitable fittings, a 2” or greater tap and control valve can be installed. Figure 5. Sewer siphon On a typical force main, the lift pump will be isolated and the wet well will be allowed to fill to near to high water level while the ice is pumped in. The ice can only travel in a direction away from the pumps due to the check valve at the pumping station (PS). The ice will form as a pig against the head Figure 6. Sewer force main of water existing in the main. Once the required amount of ice has been inserted, the pump is turned on to give the pressure and flow to “push” the pig along the main. The main is returned to service immediately. Figure 7. USG's 2,700 gallon ice delivery rig Figure 8. Various means of ice insertion can be via; From top left clockwise, a) fire hydrant, b) air release valve, c) pump bypass arrangement, d) pig launch station CASE STUDIES Western Hills Water District – Diablo Grande, CA. –Sewer Siphon - September 2013 Figure 9. Diablo Grande Community Diablo Grande is a small community in the hills near Patterson California approximately 2hrs south of San Francisco. The water and sewer system is run by Western Hills Water District. There is one main sewer that runs by gravity over six miles down to a WWTP in Patterson. It was designed to cope with the large flows that future development will bring. The Sewer passes under two aqueducts, the California Aqueduct and the Delta Mendota Canal. At each aqueduct the main splits into two pipes, Figure 10. Ariel photo showing the California one at a slightly higher level Aqueduct and the Delta Mendota Canal than the other to allow for peak flows and is designed as a siphon to allow the contents to pass under the aqueducts by means of a siphonic action. WHWD had noticed a reduction in the flow capacity and believed it to be due to a buildup of sediment, grit and sludge at the low point of each of the siphon. Although the main was designed with mechanical pigging launch stations at the high end of each siphon, the engineer was reluctant to use this method in case the pig should get stuck in the main. Designed and built into the syphon is the ability to flush the line with raw potable water from the California Aqueduct. This connection can be used to inject large volumes of water into the sewer line for flushing purposes. Unfortunately, the flushing had not proved effective on the buildup causing a partial blockage of the siphons. USG advised WHWD that ice pigging may be the solution rather than traditional pigging to eliminate the risk of getting a pig stuck under the aqueduct where excavation for retrieval is not an option. The theory was that if the siphons could be plugged off at the lower end, then the siphon could be allowed to fill naturally from residual flow back up to the higher end point where the ice would be injected. The stations were already in place for mechanical pigging so these were adapted for ice injection. Once the siphon Figure 11. Satellite image with blue highlighted route of the was full, it could be isolated and the gravity sewer detailing the two locations of the double barrel residual flow meanwhile directed into the siphons. 2nd bypass siphon. Ice could then be injected into the full siphon while the inflatable plug at the lower end would allow water to be displaced via the flow through pipe in the plug. This took very precise communication between the USCI operators at the injection end and the contractors operating the flow through plug at the "outlet" end. Prior to this happening, a backup supply of over 10,000 gallons of raw water was pumped into the sewer at one of the flushing points six miles away up at the community treatment works. This was the water that was to "push" the pig through the siphon. It was estimated that it would take approximately three hours for the backup water to arrive at the siphon once it was released. Once the full tank of ice was injected, the flow throw plug was isolated thereby holding the ice pig suspended in the first section of the siphon. It was then a matter of waiting patiently for the backup water to arrive. The timing of this was pretty crucial so as not to allow the ice pig to melt before being able to clean the main. After a few nervous moments, the backup water arrived. Simultaneously, the plug was pulled and the flow diverted into the siphon containing the ice pig. Again, a few more nervous moments waiting this time for the ice pig to arrive at the lower end of the siphon. Finally, the water started to darken in color and lumps of sludge and debris passed though the manhole at the lower end of the siphon. The water turning darker and darker (signs of the melted front end of the pig), and then, thicker and thicker. The decreasing temperature was monitored using a thermal laser thermometer. Eventually, the ice was visible in the manhole and a huge slug of ice squeezed out of the main. Once the main body of the pig passed, the fluid quickly turned clear indicating the main had been thoroughly cleaned. The siphon was returned to service and full flow was resumed. This concluded the world’s first known ice pigging of a gravity sewer siphon using the award winning technique. Statistics Delta Mendota Canal Type of Main: Gravity sewer siphon Length of main: 2 x 1,400Ft Diameter and material: 12” & 14” HDPE Ice quantity: 2,700 gallons Ice fraction: 90% Time main out of service: None Results: Siphon returned to full flow California Aqueduct Type of Main: Gravity sewer siphon Length of main: 2 x 3,151 Ft Diameter and material: 12” HDPE Ice quantity: 2,700 gallons Ice fraction: 90% Time main out of service: None Results: Siphon returned to full flow Figure 12. Ice being discharged from the siphon. Middlebury, VT. Wastewater Force Main – October 2013 The Middlebury Main Pump Station conveys wastewater through 12,000 LF of 16” and 18” ductile iron and 18” PVC force main to the Wastewater Treatment Facility. During some wet weather conditions, the pump station could not keep up with incoming flows and raw sewage was discharged to the Otter Creek (Combined Sewer Overflows or CSO events). The pumps were able to discharge 6,200,000 gallons/day with two pumps running during the first few years of operation (as designed), but pump rates decreased by more than 10% (620,000 gallons/day) over time as the force main collected grease, grit and sediment. The project objective was to clean the force main by pigging to regain the lost pumping capacity and eliminate CSO’s, improve pump efficiency and save energy. It was determined that “industry standard” solid poly pig Figure 13. Utility Service Group - winners of the ACEC Grand Award for engineering techniques would not work due to the changes in pipe size, no available insertion and retrieval stations, bends and wyes excellence on the Middlebury project. in the force main that would have restricted travel and the difficulty of handling the volume of water that would back up into the pump station wet well if the poly pig got stuck. Because of this risk, a local contractor would not even provide a quote. USG offered ice pigging as an exceptionally low risk solution. Ice pigging was evaluated and determined to be the best solution given these conditions. Calculations were made to determine the number of pipe segments to be “pigged” and location of insertion points based on the pipe diameter, pipe length and the temperature of the wastewater, to make sure the ice pig slurry would hold together as it traversed the pipe segment. The 12,000 LF force main was divided into nine segments with nine insertion points. Of the nine insertion points, seven were located in existing air-release or clean-out manholes saving time and money. The force main was exposed and taps were installed for the other two insertion points. The project was completed on schedule over a three week period. This project was the first use of ice pigging techniques to clean force mains larger than 8” diameter in North America. It was also the longest continuous run of sewer force main (12,000 LF) successfully cleaned with ice pigging. The project demonstrates that large diameter force mains (both ductile iron and PVC) can be cost-effectively and successfully cleaned by ice pigging, avoiding other more expensive and invasive pipe cleaning and repair methods. The ice pigging successfully cleaned the force main and force main capacity was returned to 6,260,000 gallons/day, based on daily draw-down tests at the pump station after each day of pigging. Figure 14. Drawdown tests show steady increase in flow after each operation. Through ice pigging, accumulated deposits were removed, decreasing friction loss and increasing capacity in the force main by more than 640,000 gallons/day. Pumping efficiency was increased, lowering pump run times and saving energy and wear. The success of ice pigging was evident each day when sand, grit, organics and grease discharged at the WWTF. The increase in pump capacity should eliminate sewer overflows, protecting public health and the environment. C-factor analysis has shown that the friction loss in the pipe is now typical of that of a new pipe. After determining pumping velocities for different pump speeds, the Town Engineer was also able to recommend programming changes in the pump cycles and pump speeds to increase the velocity of flow through the force main during pumping to achieve a “scour velocity” that should greatly reduce build-up of sediment in the future. Middlebury should be able to operate the pump station at full capacity, saving energy and eliminating sewer overflows for many years to come. Capital improvements to increase pumping capacity or replace the existing force mains was avoided. Statistics Type of Main: Wastewater sewer force (pumped) main Length of main: 11,772 Ft Diameter and material: 18” PVC and Ductile Iron Ice quantity for each run: 2,700 gallons Ice fraction: 85-90% Time main out of service: 1 hour max during each run. Results: 15% increase in flow. Dallastown Borough, Pennsylvania – December 2012 The first sewer force main in the US to be cleaned by ice pigging was performed at Dallastown Borough, located in South Central Pennsylvania. The Borough was experiencing an underperforming waste water pumping station and consulting engineers were discussing capital upgrades the PS to meet the current demands. After being introduced to the ice pigging technology, the Borough agreed to an ice pigging cleaning project as one last attempt to put off any expensive capital improvements. No other options were considered because of the long disruption to service and cost of required enabling works. Figure 15. Dallastown PA This wastewater force main project of 1,200 linear feet of 4-inch diameter unlined cast iron took approximately 2 hours to complete using 600 gallons of ice slurry. The ice was injected in two batches to allow a primary partial clean followed by a secondary clean to clean out any remaining sediment. This was done to avoid any potential heavy buildup of sediment in the small 4” pipe. The entire operation took just two hours and the ice pigging technology removed an obstruction in the main increasing the pump flows by almost 30%. The Borough could abandon the capital expenditure and put the money to good use elsewhere. Statistics Type of Main: Wastewater sewer force main Length of main: 1,200 Ft Diameter and material: 4” unlined Cast Iron Ice quantity for each (of 2) runs: 300 gallons Ice fraction: 80% Time main out of service: 30 minutes maximum during each run. Results: 30% increase in flow capacity Stokes County NC – Distribution Network The water system for the Town of Danbury is over 30 years old and is supplied by two wells, both having some iron and manganese that over time had resulted in a buildup on the interior lining of the system pipes. Regular customer complaints about discolored water made it necessary to search for a solution and having limited water production capabilities and only 100,000 gallons of storage, flushing was not a viable option. A number of calls were made looking for a company that had experience in pigging water lines and it was during those inquiries that the client discovered “Ice Pigging”. After some research the Public Works Dept. learned that Ice Pigging had many advantages over the more traditional cleaning techniques, such as minimal interruption of service, up to 70% less water required, and no digging necessary. The Stokes County Public Works Dept. identified the need to clean 18,500 FT of 6” PVC potable water mains with the aim of removing as much sediment and manganese matter as possible to improve water quality and reduce customer complaints of discolored water. A desktop study was carried out at Utility Service Corporate Office using the water maps provided by the Stokes County Public Works Dept.to measure out the lengths of pipe to be cleaned in order to determine ice quantities and set out a proposed schedule of work. This was backed up by a detailed site survey to determine the suitable insertion/extraction points. Project objective: To provide a service that is a sustainable best practice method of cleaning the water pipes using minimal amounts of water, giving the most effective results and with minimal disruption to the water supply for the client’s customers. Project team: Consisted of a three man team supervised by the Ice Pigging Project Manager. Project equipment: A 10 Ton ice delivery tanker, a 10T ice production unit powered by a portable diesel generator and a Ford F-250 carrying a “Flow Analysis System”. Project features: Existing hydrants used to insert and extract ice. An existing fitting in a PRV pit was used for ice insertion on one run Entire project carried out in total 4 runs over 2 days Maximum supply interruption time 2 hours on each run Ice samples were collected for further analysis Waste tanker used to capture and dispose of the discharged ice. Summary of results Total length of mains cleaned Average time taken per run Average volume of water used Average amount of sediment removed 18,500 FT 2hrs 20 minutes 1.6 x pipe volumes 87.6 lbs. per mile of pipe SUMMARY Ice Pigging in the United States Over 300 miles of pipe has been cleaned worldwide using Ice Pigging, including 150 miles in the United States across 28 states, (120 projects in all). (Fig. 16.) Pipes ranging from 2”-24” diameter have been cleaned and the maximum length cleaned in one pass in the US to date, is 2.25 miles on a 6” PVC main in Murfreesboro, Tennessee. USG continues to apply Ice Pigging techniques on potable water, raw water, sewer force mains and sewer siphons with successful results. There are upcoming wastewater projects in Michigan, Wisconsin, North Carolina and Washington. Figure 16. Map of US shows the green shaded states where Ice Pigging has been performed. Ice Pigging is being adopted as a cost-effective method of pipe cleaning in many countries around the World. The experience gained by USG and others has shown that the technology offers an opportunity to make real cost savings by reducing energy bills. More importantly, large capital expenditure on new pumps, pipelines and structures can be avoided with a system that provides the owner with a rapid, environmentally friendly, effective solution, at exceptional low risk. FREQUENTLY ASKED QUESTIONS: Q. How much salt is used and what effect would it have on my Waste Water Treatment Plant? A. USG use a brine solution with a similar salt percentage to seawater. The salt used as a freezing depressant is food grade, NSF approved table salt. The effect on WWTP needs to be considered as the salt can harm the good bacteria used in the treatment process. It is a simple matter of dilutions and a question of what quantities the plant takes in a typical day. Generally, the ice quantities are insignificant compared to the capacity of the treatment plant. Q. Is it effective on cast iron pipes that have heavy tuberculation? A. The ice is effective on any pipe material. A certain amount of care is required when applying to heavily tuberculated cast iron. The ice slurry is prepared with a lower ice fraction, therefore, it is runnier and less aggressive. This allows the pig to give an effective clean removing all the loose sediment, biofilm and manganese buildup without breaking off too much of the tuberculation. Q. What pressure is required to push the ice through the main and will it require excessive force? A. The ice flows through the main using the normal system flows and pressures. There will be no undue pressure applied to the main. Prior to ice insertion, the static pressure shall be tested so that the bar is set when inserting the ice. The operators have the experience and skill to control the pressure by adjusting and balancing the flows as they inject the ice. Q. Is the equipment clean or is there a risk of cross contamination? A. The equipment is disinfected prior to every new project and at the end of every working week. All hoses are disinfected, capped and stowed in clean boxes ready for use. There is a separate set of hoses clearly marked for potable and waste water. No hose is ever used on a main for which it is not designated. Q. How will you dispose of the discharge? A. Once the ice is delivered into the main, it becomes the property of the pipe owner. Disposal will be according to the owner's instructions. Public sewer is the preferred choice but in the event of the sewer not being suitable or available, then a waste disposal tanker can be arranged. A last resort would be to discharge to ground but only after written State approval is obtained by the customer. Q. How does it perform in the heat of the desert? A. Extreme temperatures are not the ideal situation, ice pigging can still be effective in these conditions. Ice quantities would normally be increased to allow for the expected higher water temperature. This may add to the cost to the customer so we may suggest that the work be done in cooler periods in Spring, Fall or Winter. Q. This is a pretty new technology, how can I be sure it is safe and will work effectively? A. Ice pigging was developed over ten years ago in the UK. It was introduced to the US in 2012 and to date (September 2014), over 300 miles worldwide and 150 miles in the US have been successfully cleaned. The operators are experienced and skilled, USCI has employed one of the worlds most experienced ice pigging experts to oversee the service. There are a number of case studies of our more notable projects on the USCI website and a list of references in the US is available on request. Q. Will the cold ice cause the main to break? A. No. Tests were conducted on an exposed pipe that was ice pigged in the usual manor. Strain gauges and temperature sensors showed no undue stress on the main at all when the ice passed through the main. Figure 17. Temperature sensors and strain gauges attached to main ACKNOWLEDGEMENTS Figure13. By permission of Aldrich + Elliott, PC Water Resource Engineers.