JAMSHORO POWER COMPANY LIMITED DETAILED ACCOUNT OF POWER PLANTS Presentation By Muhammad Akram Chief Executive Officer 12th November, 2010 JAMSHORO POWER CO. LTD. 850 MW THERMAL POWER STATION JAMSHORO JAMSHORO POWER CO. LTD (GENCO-I) BRIEF INTRODUCTION 1. Installed Capacity TPS Jamshoro 850 MW GTPS Kotri 174 MW Total 1024 MW 2. Registered Office WAPDA House Lahore 3. Date of Registration 03.08.1998 4. Date of Commencement of Business 01.03.1999 5. Grant of generation License 1.07.2002 6. Authorized Capital Rs: 50,000 M 7. Application for Determination of Tariff date 27.03.2003 / 19.06.2006 8. Determination of Tariff by NEPRA. 31.03.2004 / 02.07.2007 PROJECT DIGEST (COMPLEX-I) Installed Unit Capacity No: (MW) ST - 1 ST - 2 Fuel T.P.S. Jamshoro Project Commissioning Cost Date (Mil. Rs.) 250 Furnace Oil (F.O) 27.01.1990 200 Dual (Gas/FO) 03.12.1989 ST - 3 200 Dual (Gas/FO) 17.06.1990 ST - 4 200 Dual (Gas/FO) 21.01.1991 Total: 850 Contractor Manufacturer 6762 M/s. Fuji Elect. M/s. Mitsui & Co, Japan & Co. Japan M/s. Mitsui/ Riley Japan 8869 M/s. Harbin Turbine, Boiler M/s. CMEC & Electrical China Machinery Co., Harbin China 15631 PROJECT DIGEST (COMPLEX-II) G.T.P.S KOTRI Unit No: Installed Capacity (MW) GT - 1 15 GT - 2 15 GT - 3 25 GT - 4 25 GT - 5 25 GT - 6 25 CCP-7 44 Total: 174 Fuel Dual (Gas/HSD) Dual (Gas/HSD) Dual (Gas/HSD) Dual (Gas/HSD) Dual (Gas/HSD) Dual (Gas/HSD) Through Heat recovery boilers on GT 3-6 Commissioning Date Project Cost (Rs.M) Dec. 1969 64.9 Jan. 1970 May. 1979 184.018 May. 1979 April. 1981 202.878 May. 1981 Oct. 1994 1792.479 2244.28 Contractor Manufacturer M/s. CIE Electro Mech. (CEM) CEM/BBC France M/s. Thomassan M/s. Thomassan BV Holland BV Holland M/s. Marubeni Japan M/s. Hitachi Japan M/s. HPEEC China M/s. HPEEC China M/s. Chockerill Mech. Industries, Belgium GENCO-I TECHNICAL DATA TPS JAMSHORO Size (Capacity) Dependable (MW) (IDC NET) Fuel Used Commissioning Date Age (Years) 250 205 F. Oil Jan 1990 20 S/T 200 156 Gas / F. Oil Dec 1989 21 3 S/T 200 157 Gas / F. Oil Jun 1990 20 4 S/T 200 157 Gas / F. Oil Jan 1991 19 TOTAL - 850 675 - - - Unit # Type Installed (MW) 1 S/T 2 GTPS KOTRI Unit # Type Installed (MW) Dependable (MW) Fuel Used Commissioning Date Age (Years) 1 G/T 15 8.5 Gas / HSD Dec 1969 41 2 G/T 15 8.5 Gas / HSD Jan 1970 40 3 G/T 25 18 Gas / HSD May 1979 31 4 G/T 25 18 Gas / HSD May 1979 31 5 G/T 25 18 Gas / HSD Apr 1981 29 6 G/T 25 18 Gas / HSD May 1981 29 7 Steam Unit (C.C.P) 44 34.5 G/T Exhaust /Flue Gases Oct 1994 16 TOTAL - 174 123.5 - - - JAMSHORO POWER COMPANY LIMITED CRITICAL / SIGNIFICANT PERFORMANCE INDICATORS July-2009 to June-2010 POWER PLANT INSTALLED CAPACITY (MW) TESTED I.D.C (NET) (MW) MAX: LOAD (MW) GROSS GEN: (Gwh) GROSS AVAIL: FACTOR (%Age) PLANT UTILIZ: FACTOR (% Age) LOAD FACTOR (% Age) ST-1 BLOCK-I 250 205 200 955 73 50 ST-2 BLOCK-II 200 156 180 1118 88 ST-3 BLOCK-II 200 157 180 1026 ST-4 BLOCK-II 200 157 175 GT-3 BLOCK-III 25 18 GT-4 BLOCK-III 25 GT-5 BLOCK-III THERMAL EFFICIENCY (% Age) Design (% ) Actual (% ) 50 36.63 32.92 75 71 33.89 29.39 85 69 65 33.89 28.71 1182 91 79 77 33.89 29.70 22 135 84 62 70 27.85 21.51 18 23 111 81 51 55 27.85 21.50 25 18 23 140 99 64 70 27.75 21.47 GT-6 BLOCK-III 25 18 19 84 96 38 51 27.75 21.40 CCP-7 BLOCK-III 44 34.5 38 185 90 53 56 - - GT-1 BLOCK-IV 15 8.5 10 14 99 11 16 24.50 15.36 GT-2 BLOCK-IV 15 8.5 9 13 99 10 16 24.50 15.37 Overall GENCO-I 1,024 798.5 879 4,963 90 65 68 - - JAMSHORO POWER COMPANY LIMITED CRITICAL / SIGNIFICANT INDICATORS July-2009 to June-2010 POWER PLANT INSTALLED CAPACITY (MW) TESTED I.D.C MAX: LOAD (MW) GEN: (Gwh) AVAIL: FACTOR (%Age) PLANT UTILIZ: FACTOR (% Age) LOAD FACTOR (% Age) THERMAL EFFICIENCY (% Age) Design (% ) Actual (% ) BLOCK-I JAMSHORO 250 205 200 955 73 50 55 36.63 32.92 BLOCK-II JAMSHORO 600 470 535 3326 87 71 71 33.89 29.82 BLOCK-III KOTRI 144 106.5 125 655 92 67 67 27.80 29.91* BLOCK-IV KOTRI 30 17 19 27 100 30 31 24.50 15.36 1,024 798.5 * Overall Efficiency of Block-III with CCP FUEL SUPPLY SYSTEM FUELS TPS JAMSHORO GTPS KOTRI Fuel Oils R.F.O H.S.D On fortnight basis from PSO - Tank Lorries - Source Mode of Supply Oil Decanting Capacity 5000 M.T / Day - 100,000 M.T 6, 600 M.T 30,000 M.T NIL M/s SSGC Ltd Hyd M/s SSGC Ltd Hyd Mode of Supply Through 16” Pipeline Through 12” Pipeline Gas Allocation 62 MMCFD (53 MMCFD Guaranteed)) 15-20 MMCFD (10 MMCFD Guaranteed)) 925-1030 925-1030 Oil Storage Capacity Average Stock GAS SUPPLY SYSTEM Source Average Gross Calorific Value (Btu/Cft) THERMAL POWER STATION JAMSHORO MAXIMUM LOAD SHARED (MW) MW 900 800 700 600 500 400 300 200 100 0 775 2005-06 760 2006-07 730 2007-08 730 2008-09 700 2009-10 GAS TURBINE POWER STATION KOTRI MAXIMUM LOAD SHARED (MW) MW 180 149 146 141 144 136 150 120 90 60 30 0 2005-06 2006-07 2007-08 2008-09 2009-10 THERMAL POWER STATION JAMSHORO AVAILABILITY & UTILIZATION FACTORS Availability (%) 100 90 80 70 60 50 40 30 20 10 0 Utilization (%) 81 75 77 65 74 64 68 61 62 47 2005-06 2006-07 2007-08 2008-09 2009-10 GAS TURBINE POWER STATION KOTRI AVAILABILITY & UTILIZATION FACTORS Availability (%) Utilization (%) 120 100 92 95 88 80 94 63 59 94 64 64 54 60 40 20 0 2005-06 2006-07 2007-08 2008-09 2009-10 THERMAL POWER STATION JAMSHORO ENERGY GENERATED (MKWH) FUEL MIX F.O 5000 4500 4000 3500 3000 2500 2000 1500 1000 500 0 GAS TOTAL 4346 4281 4228 3899 3051 2718 2505 1628 2493 2453 1723 1446 2005-06 2006-07 2007-08 1709 1342 2008-09 1788 2009-10 THERMAL POWER STATION JAMSHORO Fuel Cost (Paisa/KWH) F.O GAS TOTAL 1117 1200 1050 884 900 600 450 623 1446 750 499 347 256 494 381 827 3899 288 417 422 304 300 150 0 2005-06 2006-07 2007-08 2008-09 2009-10 THERMAL POWER STATION JAMSHORO Overall Cost (Paisa/KWH) Overall Cost 950 850 750 650 550 450 350 250 150 50 865 685 486 385 416 2005-06 2006-07 2007-08 2008-09 2009-10 GAS TURBINE POWER STATION KOTRI ENERGY GENERATED (MKWH) GAS 950 850 750 650 550 450 350 250 150 50 741 791 810 785 683 2005-06 2006-07 2007-08 2008-09 2009-10 GAS TURBINE POWER STATION KOTRI Fuel Cost (Paisa/KWH) GAS 550 500 450 400 350 300 250 200 150 100 50 411 296 288 2006-07 2007-08 433 245 2005-06 2008-09 2009-10 GAS TURBINE POWER STATION KOTRI Overall Cost (Paisa/Kwh) Overall Cost 600 550 500 450 400 350 300 250 200 150 100 50 461 295 2005-06 347 336 2006-07 2007-08 2008-09 496 2009-10 Future Plan for the Repair and Rehabilitation of Jamshoro Power Plant For the rehabilitation of Units 1,2,3&4 of Jamshoro, a Fixed Amount Reimbursement Agreement (FARA) has been signed on 20.05.2010. Under this agreement, the USAID will provide US$ 18.36 million for the repair & rehabilitation. The following table summarizes the proposed rehabilitation works and the associated costs. Sr. No. Unit Details of Works/Spares No. 1- 1 Rehabilitation of air Pre-heater Side-B Rotor 2- 1 Replacement of Final Super Heater Coils 3- 1 4- 1 Estimated Cost (US$) 500,000 Planned Completion date 30.11.2011 1,000,000 -do- Complete replacement of Flue Gas Duct & Air Pre-heater Bottom hoppers 600,000 -do- Complete Rehabilitation of Cooling Towers 500,000 -do- Sr. No. Unit No. Details of Works/Spares Estimated Cost (US$) Planned Completion date 5- 1 P-Gradation/Replacement of Auto Burner Control System & Data Acquisition System 300,000 30.11.2011 6- 1 F.D. Fan duct up to Steam Coil Air Heater 200,000 -do- 7- 1 Major Overhauling 1,650,000 -do- 8- 1 Soot Blower Spare Parts 100,000 -do- 9- 1 Tube Bundles of Steam Converter 250,000 -do- 10- 1 Spares for Oil & HSD Burners & Igniters 200,000 -do- 11- 1 Air Pre-heater Elements & Seal 670,000 -do- 12- 1,2,3 &4 1,000,000 -do- Use of fuel oil additives to prevent soot buildup and cooling water treatment chemicals to prevent scale buildup Sr. No. Unit No. Details of Works/Spares Estimated Cost (US$) 3,450,000 Planned Completion date 13- 2,3&4 Replacement of HP Heaters along with the valve and controllers including Rehabilitation of Instrument Control & Protection System 30.11.2011 14- 2,3&4 Complete Rehabilitation of Cooling Towers 750,000 -do- 15- 2,3&4 Modification/Rehabilitation of Electro Hydraulic and Mechanical Hydraulic Governing System 900,000 -do- 16- 2,3&4 Complete Rehabilitation of Drain Valves 300,000 -do- 17- 2,3&4 Rehabilitation of soot blowing system 600,000 -do- 18- 2,3&4 Replacement of Coagulator Agitators 1,200.000 -do- Sr. No. Unit No. Details of Works/Spares Estimated Cost (US$) Planned Completion date 19- 2,3&4 Replacement of Data Acquisition System (DAS-100), Auto Regulation System (MZ-III) & Temperature Scanners for Generator Winding Temperature, Super Heater/ReHeater Temp:, Boiler Drum Metal Temp: FD, ID Fan Motor Temp: Boiler Feed Pump Temp: with latest Distributed Control System (DCS) 900,000 30.11.2011 20- 2,3&4 Replacement of Existing FSSS along with Furnace Flame Monitoring 390,000 -do- 100,000 -do- 1,000,000 -do- 21- 2 Procurement of Boiler Feed Pump Motor Complete 22- 3 Replacement of Final Super Heater Coils 23- 3 Three Way valve of Oil Burner 200,000 -do- 24- 3 Spares for Overhauling of Turbine 500,000 -do- Sr. No. Unit No. Details of Works/Spares 25- 2&4 Replacement of Turbine Vibration System with ViBro-Control-4000 Schenk 200,000 30.11.2011 26- 4 ID Fan Impellers 500,000 -do- 27- 1,2,3 &4 Off-line Efficiency Monitoring System & Training 400,000 -do- Total Cost (US$) Estimated Cost (US$) 18,360,000 Planned Completion date Targeted load after Rehabilitation The targeted rehabilitation of the four Units will re-capture 95MW of the derated capacity. The MW recovered after targeted rehabilitation as under:Unit # Installed Declared DePresent Capacity rated Operational (MW) Capacity Capacity (MW) Gross (MW) Gross Gain After Rehabilitation (MW) Capacity after Rehabilitation (MW) 1 250 225 190 35 225 2 200 170 170 20 190 3 200 170 170 20 190 4 200 170 170 20 190 Total 850 735 700 95 795 Critical Issue Serious Problem due to saline River Water of high conductivity (1,200µs/cm against designed 500µs/cm). This has badly affected the operation of the Power Plant and caused high consumption of Chemicals, resulting increase in per unit cost Solution Installation of Reverse Osmosis Plant Thank you 29 ORGANIZATION STRUCTURE Board of Directors Company Secretary Chief Executive Officer Internal Audit Finance Director Technical Director Jamshoro Plant HR &Admn. Director M.I.S. Director Kotri Plant BOARD OF DIRECTORS Private Sector PEPCO Prof. Dr. Khawaja Amjad Saeed, Chairman Mr. Salman Iqbal Executive Director (L&CA) Syed Wajid Ali Shah Chief Engineer, GSO, Lahore Mr. Ashfaq Ahmed Waraich, GM,Wazir Ali Industry Hyd Mr. Muhammad Mumtaz Chief Engineer (WPPO) Mr. Mohammad Akram, Chief Executive Officer, GENCO-I Mr. Yousuf Suleman Ex-President Hyderabad Chamber of Commerce & Industries, Hyderabad WAPDA/JPCL Total Land of JPCL = 800 Acres JAMSHORO POWER COMPANY LIMITED Energy Generation Since Commissioning up to June 2010 T.P.S Jamshoro Unit No Date of Commissioning Operation Hours Energy Generated (MKWH) ST-1 27.01.1990 123074 20092 ST-2 03.12.1989 116366 17081 ST-3 27.06.1990 110537 16311 ST-4 21.01.2991 108584 15918 458561 69402 G.T.P.S Kotri Unit No Date of Commissioning Operation Hours Energy Generated (MKWH) GT-1 Dec-69 104730 896 GT-2 Jan-70 125540 1021 GT-3 May-79 164438 2923 GT-4 May-79 186340 3305 GT-5 Apr-81 160377 2878 GT-6 May-81 163089 2864 CCP-7 Oct-94 117441 2910 1021955 16797 A- Present De-rated Load This Power Plant comprises four conventional Steam Power Units with a total capacity of 850MW. The Units have been derated to a capacity of 675 MW. The Unit wise configuration of this Power Station along with the de-rated capacity is enumerated as under:Unit # Installed Capacity (MW) Declared De-rated Capacity (MW) Make Year of Commissioning 01- 250 205 Fuji Japan 1990 02- 200 156 CMEC China 1989 03- 200 157 CMEC China 1990 04- 200 157 CMEC China 1991 Total 850 675 C- Reasons of De-rating i) a) b) c) d) e) f) g) h) i) Unit-1 Aging Factor Damaged APH Elements Damaged Steam Coil Air Heaters Condenser Choking Frequent leakages in Final Super Heaters Frequent leakages in Re-heaters Low Efficiency of Cooling Towers Leakages from Air Pre-Heaters Damaged flue Gases duct a) b) c) d) e) Unit-2,3&4 Aging Factor Outage of HP Heater Frequent choking of APH Elements Condenser Choking Low Efficiency of Cooling Towers ii) KEY PERFORMANCE INDICATORS 1. 2. 3. 4. 5. Plant Availability Factor (%) Plant Utilization Factor (%) Plant Load Factor (%) Plant Heat Rate (Btu/kWh) Thermal Efficiency (%) Rehabilitation of Jamshoro Power Plants Recovering the lost output of existing power plant is the dire need of PEPCO’s system to bridge the gap to some extent between demand and supply and reduce the generation cost per Kwh. It has therefore been planned to regain the lost capacity of Jamshoro Power Plant by rehabilitation. Keeping in view the present power crises in the country, US Government plans to assist the GoP and resolving the power crises through Repair & Maintenance measures to improve the operating capacity of the Jamshoro Power Plant. Rehabilitation of old Units means to refurbish or upgrade the components in order to recapture the lost capacity and bring the performance near to the designed capacity. Despite proper operation & maintenance, aging is a major factor causing higher generation cost due to excessive forced outages period resulting less availability, loss of output and increase in heat rate. Rehabilitation of old steam power units is not only a financially viable option but also shorter in implementation period as compared to installing a new power unit.