WATER PASTEURIZATION INDICATOR (WAPI) MAKER REDESIGN Victor Rodriguez B.S., California State University, Sacramento, 2008 PROJECT Submitted in partial satisfaction of the requirements for the degree of MASTER OF SCIENCE in MECHANICAL ENGINEERING at CALIFORNIA STATE UNIVERSITY, SACRAMENTO FALL 2011 WATER PASTEURIZATION INDICATOR (WAPI) MAKER REDESIGN A Project by Victor Rodriguez Approved by: __________________________________, Committee Chair Akihiko Kumagai, Ph.D. ____________________________ Date ii Student: Victor Rodriguez I certify that this student has met the requirements format contained in the University format manual, and that this project is suitable for shelving in the Library and credit is to be awarded for the Project. __________________________, Department Chair Susan Holl, Ph.D. Department of Mechanical Engineering iii ________________ Date Abstract of WATER PASTEURIZATION INDICATOR (WAPI) MAKER REDESIGN by Victor Rodriguez Currently, the Biology Department at California State University, Sacramento is involved with the manufacturing of Water Pasteurization Indicators (WAPIs). These indicators are use to aid developing countries with their water cleaning process. The current manufacturing process has some disadvantages that make the manufacturing inefficient and unsafe. For example, the current devise used to manufacture the WAPIs is very difficult to use because it requires lots of strength to press the ends of the tubes. This devise also gets extremely hot and is very delicate to adjust the temperature to the required range. If temperature is too low, the polycarbonate tube would break. If temperature is too high, the polycarbonate tubes would melt and stick to the clamping plates. In addition, the heating system is design with parts that are not reliable. The current design is unsafe because part of the heating coil is exposed. Having the heating coil expose might also reduce its life expectancy. In addition, the current design is not easy to repair or maintained. To conclude, the device needed to be redesign to make it more user-friendly, safer, more economical, and more reliable. To solve the old device issues, the clamping and heating mechanism was redesign to a more reliable, iv economical, user-friendly and safer design. The new design was tested, and showed positive results by producing good quality WAPIs. _______________________, Committee Chair Akihiko Kumagai, Ph.D. _______________________ Date v ACKNOWLEDGMENTS I want to thank professor Kumagai for given me the opportunity to work on this project. Working on this project has given me the opportunity to grow as a person and as an engineer as well. It has been an honor to work on a highly important project, which is going to facilitate and improve the lives of many people around the world. This project has provided me the opportunity to learn new ways in which an engineer can assist communities in need. In addition, I want to thank my family for their support and for been there every step of the way, but more importantly I want to thank God for giving me strength to design and build this device on the time given. Furthermore, I want to thank GNB Corporation for donating the needed resources I used to fabricate the prototype. I want to give special thanks to Edgardo Barrera for assisting me with welding skills for this project. vi TABLE OF CONTENTS Page Acknowledgments.....................................................................................................................vi List of Tables ........................................................................................................................ viii Chapter 1. INTRODUCTION …………………… ………………………………………………… 1 2. CURRENT DESIGN .......................................................................................................... 3 3. REDESIGN ........................................................................................................................ 5 4. MANUFACTURING THE NEW WAPI MAKER ........................................................... 9 5. TEST AND RESULTS .................................................................................................... 11 6. CONCLUSION ................................................................................................................ 14 Appendix A. Figures ............................................................................................................. 15 Appendix B. Drawings and Work Instructions ...................................................................... 22 Bibliography ........................................................................................................................... 66 vii LIST OF TABLES Tables Page 1. Controlling Factors and Two Level Values……….………………………......13 2. Testing Results…………………………………….…………………………..13 viii ix 1 Chapter 1 INTRODUCTION Many third world countries lack the basic resources that allow them to have drinkable water, food, clothing, medicine, etc. Today 2.5 billion people in many parts of the world do not have access to safe drinking water. In fact, every twenty seconds a child dies because of low levels of sanitation in food, water, etc. (UN Water). Not having clean water can affect not only people’s health, but it can also spread diseases and create conflicts between villages. Furthermore, engineering can be use as a way to develop and design systems that can assist third world countries to obtain basic resources in an economical manner. To resolve this issue, Solar Cookers International (SCI) in Sacramento, CA. developed a reflective solar cooker called “Cookit.” This system is use to pasteurize water in third world countries. In addition, Dale Andreatta and the Department of Biological Science at California State University, Sacramento developed a device called Water Pasteurization Indicator (WAPI). This device is use together with the Cookit to check if the water is above its pasteurization temperature, so that people can drink it (Kumagai et al.). For this project, I will concentrate on the WAPI. The Water Pasteurization Indicator is made of carnauba wax in a polycarbonate tube. The tube is seal at both ends and a washer is use as a weight to set the orientation of the WAPI. A fishing string is use for pulling the WAPI out of water. Before the water is hot, the wax is at the top of the tube, and after the water gets hot, the wax melts down. When the wax melts down it 2 means the water is pasteurize (Kumagai et al.). Figures 1 and 2 provide an illustration of this system. There are other types of pasteurization indicators; however, the WAPI has been the easiest to understand and the cheapest to manufacture. Although the manufacturing is cheap, this one has shown room for improvement. A few safety and reliability concerns needed to be address to make the device, used to make the WAPIs, more user-friendly. This project illustrates how the device was redesign to eliminate the concerns and reliability problems. 3 Chapter 2 CURRENT DESIGN Prof. Robert Metcalf in the Department of Biological Science at California State University, Sacramento has worked with his students and other researchers to develop WAPI. However, a manufacturing method to produce WAPIs had to be developed so that WAPIs are used by a large number of people in developing countries beyond a proof of concept in a lab environment. The task to tackle this challenge of manufacturing WAPIs was initially given to a group of mechanical engineering students at CSUS, who produced the first manufacturing process for making WAPIs. The design tool to manufacture WAPIs, was build fallowing specific design requirements. One of the requirements was to make a design based on technology that can be used in third world counties. In addition, this one had to be productive, simple, economical, easy to operate, easy to maintenance, and safe (Kumagai et al.). The first design consisted on a pair of aluminum plates heated by heating electrical wires. A variable autotransformer was use to control voltage for the heating wires. K-thermocouples with digital thermometer were use to monitor the temperatures of the heating plate. A vise was use to create the pressing force needed for crushing the tubes (Kumagai et al.). A more detail manufacturing process for this design is shown on figure 10. This design has been producing WAPIs successfully for a few years. Throughout this time, there have been many different operators using this devise and feedback on this 4 devise has shown that there is room for improvement. Operators say the device needs to be more user-friendly and safer. For example, the device requires lots of strength to clamp the plastic tubes, the body gets hot, and the device is unstable. The body being unstable and hot can crate a dangerous environment, which can injure the operator. In addition, the device seems to have a heating wire expose, which can also be a safety concern. Another opportunity for improvement, pointed by the operators, was the variable transformer voltage adjustment. The variable transformer is very unreliable when trying to obtain the desired temperature range needed for sealing the ends of polycarbonate tubes. When the temperature is too low, the polycarbonate tube would break, and when the temperature is too high, the polycarbonate tubes would melt and stick to the clamping plates. Due to this problem, many polycarbonate tubes have been scraped. The design of the heating system is another feature pointed out as a possible opportunity for improvement. This one is currently design with a heating coil exposed to the air. For this reason, the devise might not last long, making the design unreliable. It was also pointed out the device was not easy to repair or to do any maintenance. Many of the parts used by the device, such as the heating system, are parts that need to be specifically order from a company. As mentioned above, there are opportunities for improvement. In order to eliminate the operator’s safety and reliability concerns, this device will be redesign to make it more reliable, economical and easier to operate which would make the WAPIs manufacturing more efficient and accessible. 5 Chapter 3 REDESIGN As mentioned, the existing WAPI Maker needs improvements. The operators have safety concerns and believe the devise can be redesign to a more user-friendly, reliable, and economical design. In order to obtain a good understanding of the problems the operators were facing, I decided to test the tool by making a few sets of WAPIs. I first decided to change the clamping mechanism. During my testing, pressing the tubes was not a simple operation, especially when the part was unstable and too hot to handle. I decided to replace the vise with a standard 1.5-ton scissor jack. These are commonly use in cars. This scissor jack is strong, inexpensive, user-friendly, and reliable. In order to use it, I needed to build a frame for it. I decided to make the frame out of 3inch (1/8 inch wall) mild steel square tube. I decided to use this tube because of its strength, weight, reliability, low cost, and less conductive shape and properties. When designing the frame, I added a mounting base to keep the tool stable. I also decided to add holes throughout the body of the frame to make the assembly of the devise easier. A picture of the frame is shown on figure 2. When making the frame I decided add a base for the transformer. This helps to keep everything together and makes it easier to move around if needed. Drawings and work instructions for modifications to the scissor jack, and to build the frame are shown in Appendix B. Once the frame was ready, it was painted with high temperature paint to prevent it from corroding. This extends the life of the frame, because mild steel was use. In 6 addition, plastic caps were use to cover the ends of the square tubes to protect the electrical wires and connections. To operate the scissor jack, I needed a user-friendly handle. I decided to go with a 12-inch stainless steel float rod. These are threaded at both ends and are widely available. At the ends of the rod, I used black phenolic ball knobs. By combining, the phenolic knob and the float rod I was able too obtain a user-friendly, economic, and reliable handle. A picture of the handle and modified jack is shown on figure 3. The next feature to redesign was the heating system of the devise. As mentioned before, the existing heating system was unreliable and had safety concerns. I decided to replace the existing heating design with 1-1/2” strip heaters. These are widely available, reliable, and are easy to replace if they get damage. In addition, these can reach high temperatures in a short period with low voltage. The only problem with these strips is the middle of the strip gets hotter than the ends. This was a problem because a constant temperature is needed throughout the heating system to make five WAPIs at a time. To solve this problem, I use a ¼-nch copper plate to protect the strip heating plates. The copper helped conduct the heat of the strip heating plate throughout the five tubes. In addition, during my testing with the old device, I notice that the WAPIs were not consistent after pressing the ends. The ends did not have established dimensions, as a result, these could very on thickness and length. To solve this problem, I decided to give it a length and thickness by adding a step on one of the copper plates. This step help indicate how much the tube needed to be pressed. The step also eliminated the problem of applying too much force when pressing the tube at higher temperatures. 7 Another problem encounter during the testing was the short temperature range allowed to make the WAPIs. The temperature to operate the tool successfully ranges from 300-315° F, which is not easy to maintain with the current device. When the temperature is too high, the tube melts and sticks to the plate, and when the temperature is low, the tube breaks. To solve this problem, I decided to use aluminum plates to hold the tubes, while these were pressed. The aluminum plates bolt to the body of the heating system. The body and the copper plates conduct heat to the aluminum plates. The aluminum holder heats the plastic tubes, while the ends of the tubes are pressed. Heating the tubes with the aluminum plates helps form the ends of the tubes to a shape that will not break while also allowing the device to operate successfully at a wider temperature range (315-350°F). The aluminum plates are also use to help align the scissor jack and the heating system. This alignment was accomplished by using dowel pins as aligning shafts. With this heating design, I was able to obtain a more consistent and bettor quality seal on the ends of the tubes. To reduce cost and to make the device more reliable, I changed the thermometer used to read the heating system’s temperature. The existing device uses k-thermocouples with the digital thermometer Model HH12 to read the temperature. The cost for this devise is over $100 dollars while the cost for a digital cooking thermometer, TP3001 model, is $15 dollars or less. These cooking thermometers are widely available and can be from any brand or model as long as withstands the temperature. As we see above, the device was redesign with the purpose to eliminate the concerns mentioned by the operators. The new design is more economical and reliable 8 due to the changes made to the clamping and heating system. By redesigning the heating system, the safety concerns were eliminated. The device is now more user-friendly due to the changes made to clamping mechanism. Overall, I believe this design can be use as a base to develop an economical mass-producing WAPI facility. 9 Chapter 4 MANUFACTURING THE NEW WAPI MAKER Once the redesign was completed, the next step was to manufacture the tool itself. When redesigning the WAPI Maker, specific manufacturing requirements were taken in to account. The requirements consisted in designing the individual components to a low complexity where simple machining techniques could be use to fabricate them. The purpose of having these requirements was to make the device simple enough so that it can be build by people in developing countries with little machining experience and machining resources. To ensure the device was design in accordance with these guidelines, I decided to machine all the components using a Bridgeport manual milling machine. This gives me a good understanding on what complexity level the components were design. In addition, by doing the machining, I was able to make design changes to make the machining step simpler. To facilitate and organize the manufacturing of the WAPI Maker itself, a bill of materials (BOM) was created. The BOM provides a clear description on the materials and components needed to build the WAPI Maker. It also organizes the manufacturing process by establishing assembly layers. The assembly layers allow the fabricator to know the next fabrication step of a component after a certain operation. In addition, the BOM designates work instruction numbers to components that need to be fabricated. This helps identify the work instruction number needed to fabricate the part using the BOM. 10 As mentioned, work instructions are designated to parts that need to go through any fabrication or modification. The work instructions provide detail information on how to fabricate the part. These give the stock material required, drawing number, and inform the sequence of operations needed to complete the part. In addition, these are use to give detail information such as procedures to the fabricator. The work instruction packages are use by the fabricator to minimize possible manufacturing errors and to standardize the manufacturing process of the part. The BOM, drawings, and work instructions for the WAPI Maker are shown in Appendix B. Using work instructions to manufacture the WAPI Maker will help reduce fabrication time by allowing the parts to smoothly flow through a shop until successfully building the device. 11 Chapter 5 TEST AND RESULTS After manufacturing and fully assembling the WAPI Maker, the devise was ready for testing. I decided to perform similar tests the students who made the old design performed. This provided a good illustration on the areas that were improved by comparing the results to the previous data. During their testing, they experimented three control parameters; temperature of the heating plates, clamping gap, and clamping time. These parameters affected the quality of the WAPI produced (Kumagai et al.). On the new design, the clamping gap control variation was eliminated. The clamping gap was set at .08 inches by the new heating system. As a result, we end up with a two process factors and their two level values. After analyzing the old design results, I notice the higher the temperature the higher the quality of the WAPI. This was until facing the limit temperature. With this observation, I assumed that extending the operational temperature of the device, but not damaging the tubes, would increase the probability of having a good quality WAPI, regardless of a gap variation. The theory was proven following the tests of the new device. Table 1 shows the two controlling factors and their two level values. Table 2 shows the results which indicate how more efficient the device works with the new features and controlling parameters. During the testing, the time the device took to get to the desired temperature was nine minutes. After recording the time, the testing begun with the high temperature and ten seconds clamping. All WAPIs were tested under hot water to ensure these were 12 operational. By reviewing the results, we see the device can successfully operate at a range of 315-350 °F and with a clamping time that can be as low as ten seconds. Other parameters were also tested to find out about the limits on temperature and clamping time. Temperatures over 360° F would start damaging the material and a bad quality end would form. Temperatures, below 300°F would not always seal and it would take more clamping time to make it work. The clamping time of five seconds was good for temperatures above 335° F. Below this temperature it did not always worked. The best results were obtained at the 320-335° F range and a ten-second clamping time. With these parameters, the WAPIs looked and wok the best. 13 Table 1) Controlling Factors and Two Level Values Time to heat up to 300 F = 9 min Table 1: Controlling Factors and Two Level Values Middle Level High Level Factor A (Temperature) 315-330 F (A1) 335-350 F (A2) Factor B (Clamping time) 10 sec (B1) 15 sec (B2) Table 2) Testing Results Table 2: Testing Results Combination Pass Total A1B2 9 10 A1B3 10 10 A2B2 10 10 A2B3 10 10 Totals 39 40 Percentage 90% 100% 100% 100% 98% 14 Chapter 6 CONCLUSION To conclude, we can say the new improved design met the desired goal. The devise was redesign following the given design specifications. The goal of eliminating the operator’s safety and reliability concerns was reached by redesigning the heating system. The new heating system produces consistent WAPIs and allows the device to operate at a wider temperature range, which makes the devise easier to operate and reduces the probability of error. The clamping system was also redesign. This helped the device to be more compact and user-friendly. With this project, the old design was improved by eliminating many of the operators concerns, but this is the first step to eventually build a device or a manufacturing process that can be use to mass produce WAPIs on a economical manner in third world countries. To be able to reach this goal, it is necessary continuously improving this devise. 15 APPENDIX A Figures 16 Figure 1) WAPI description figure 17 Figure 2) Frame Figure 3) Modified Scissor Jack 18 Figure 4) Assembly Picture 1 Figure 5) Assembly Picture 2 19 Figure 6) Assembly Picture 3 Figure 7) Assembly Picture 4 20 Figure 8) Final Assembly 21 Figure 9) Cookit by solar Cookers International (SCI) Figure 10) Old WAPI Maker 22 APPENDIX B Drawings and Work Instructions 23 BILL OF MATERIALS (BOM) 24 25 LABOR HOURS SUMMARY 26 27 28 29 30 31 32 33 34 35 36 37 38 39 40 41 42 43 44 45 46 47 48 49 50 51 52 53 54 55 56 57 58 59 60 61 62 63 64 65 66 BIBLIOGRAPHY UN Water, Statistics Graphs and Maps: Drinking Water and Sanitation, 16 Nov. 2011, <http://www.unwater.org/statistics_san.html> Solar Cookers International, Water Pasteurization Indicator, 16 Nov. 2011, <http://solarcooking.wikia.com/wiki/Water_Pasteurization_Indicator> Kumagai, Akihiko, Tien I. Liu, Minhaj Khan, Scott Yu, Brian Wargala, Anthony Littke, Robert Jhonson, Jeff Bear, “Manufacturing Methods For Producing Water Pasteurization Indicators (WAPI).” ASME Mechanical Engineeirng Congress & Exposition Nov. 5-10 2006.