GROUP 13 4A6(1) Disaster Report Point Pleasant Bridge Collapse Emma Finlay 08353069 Darragh Noble 07327757 Paul O’Neill 08592209 Figure 1 - Point Pleasant Bridge after Collapse Group 13 - Point Pleasant Bridge Collapse Introduction The Point Pleasant Bridge, also known as the ‘Silver Bridge’ due to the aluminium paint used, was an eye-bar chain suspension bridge built over the Ohio River. Built in 1928, the bridge which was built to connect the towns of Point Pleasant, West Virginia, and Kanauga, Ohio. At the time it was one of three such structures built in the world with eye-bar bridges being a relatively new concept of design. It was designed by the society of civil engineers and constructed in 1928 by General Corporation and American Bridge Company (Corrosion Doctors, 1999). On the 5th of December 1967 at 5pm the Silver Bridge collapsed during rush hour traffic claiming 46 lives and injuring 9 persons. The Christmas rush applied an extra load to the 40 year old bridge causing a cleavage fracture in one of the eye-bars. The structure reportedly only took one minute to completely fall into the murky water of the river Ohio directly below. An investigation immediately followed the collapse of the bridge which led to the discovery of cracks and extensive corrosion which were not visible to the eye. The collapsed bridge was replaced by the Silver Memorial Bridge which was completed in 1969. This structure, to no surprise is not of the ill-fated eye-bar chain suspension bridge design but rather a cantilever bridge design. Bridge Design The bridge was built as an eye-bar chain suspension bridge. Such bridges had usually been constructed from redundant bar links, using rows of four to six bars, and sometimes using several such chains in parallel (Wikipedia, 2011). The eye-bars in the Silver Bridge however were not redundant, as the links were only composed of two bars each. The reason why the engineers thought they could get away with this is due to the new high-strength, heat treated rolled carbon steel out of which the eye-bar was made. This had more than twice the tensile strength of common mild steel. The main problem with this was that with only two bars, failure of one could impose excessive loading on the other, ultimately causing total failure. This would be unlikely if more bars were used as redundancy. While it is possible to design a low redundancy chain, the safety is totally dependent upon correct, high-quality manufacturing & assembly (Wikipedia, 2011). The suspension bridge itself was supported by two “rocker towers”, which are designed in such a way to allow the bridge to respond to various live loads by a slight tipping of the supporting towers. They were parted at deck level rather than passing the suspension chain over a lubricated or tipping saddle, or by stressing the tower in bending. The towers required the chain on both sides for support. Failure of one link, on either side would result in complete failure of the entire bridge span. (Wikipedia, 2011) The bridge was initially designed during the 1920s and built in 1928. At the time, the typical family automobile was the Ford Model T, which weighed only 680 kg. the maximum permitted truck gross weight was roughly 9,000 kg. however, by the time collapse occurred in 1967, a typical family car weighed approximately 1,800 kg. and the large truck limit had increased to over 27,000 kg. furthermore, bumper-to-bumper traffic jams had become commonplace, occurring several times a day. The initial design loading conditions were severely less than the conditions the bridge was operating under in 1967. Group 13 - Point Pleasant Bridge Collapse Failure Mode (Collapse) The total catastrophic failure of the bridge ultimately occurred due to a minor flaw in just one of the eye-bars on what formed the suspension chain. The eye-bar responsible was no. 330 on the north face of the Ohio side of the bridge. The eye-bar was defective due to the high levels of residual stress that it was subjected to. The design of the eye-bar assembly meant that water was able to collect at the bottom. The combination of the tensile residual stress and the corrosive environment enabled a stress corrosion crack to form. The crack was allowed to grow steadily over 39 years until it reached a critical depth of approximately 1/8th of an inch in length. The steel used in the eye-bars had very low toughness in the near freezing conditions when the failure occurred, which meant that the member was susceptible to a brittle fracture. The combination of the high live loading on the bridge and the reduced toughness of the steel meant that the crack caused a brittle failure of the eye-bar. This caused the eye-bar to separate from the pin on one side. The resulting asymmetric load on the pin caused it to twist, and the single remaining eye-bar vibrated off the other side of the pin. The adjacent “rocker” tower, which needed the eye-bars on both sides as support to keep it in equilibrium and remain upright, was now destabilised and started toppling, falling to the north. The bridge deck then twisted over to the north, pulling the other rocking tower with it, and leading to a complete structural collapse of the bridge. A step by step schematic of the bridge failure is shown in the Appendix (McGuinness Publishing, 2004) – *taken from BBC documentary. Stress Corrosion Cracking is defined as the unexpected sudden failure of normally ductile metals subjected to a tensile stress in a corrosive environment (Wikipedia, 2011). In this case, the eye-bar had been subjected to an excessive live tensile strength and had developed a stress corrosion crack of critical depth of 1/8th of an inch thick upon failure. This crack was developed over 39 years before it eventually reached critical size! Aftermath & Conclusions This disaster focused a lot of attention on older bridges and bridges built in the same fashion (eye-bar type construction). There were two other bridges built to a similar design, one further upstream at St. Mary’s, West Virginia and one in Florianopolis in Brazil. The bridges in Florianopolis and the Hi Carpenter Bridge in St. Mary’s, which was built by the same company, were immediately closed. The use of the bridge in St. Mary’s was different, in that it didn’t carry the same heavy traffic loads. The National Transportation Safety Board had to condemn the bridge because they could not prove its structural stability. The Hi Carpenter Bridge was demolished in 1971 with controlled explosions on the main charges. The Brazilian bridge remains but is still closed to traffic although it was designed to a higher factor of safety than the bridge at Point Pleasant (Lonaker, 2006). The legacy of the Point Pleasure Bridge collapse was in bridge safety in general. In 1967 President Johnson established the National Bridge Inspection Standards. There are definitions used in the NBIS regulation to ensure all bridges are checked to a specific standard. Quality assurance (QA): Effectively means that measures such as sampling check the adequacy of quality control procedures which are used to measure the quality level of the bridge and how it’s designed for loading. Quality control (QC): Effectively the quality of the inspection on the bridge and the load rating to be at or above a required level. These are the guidelines used on all bridges inspected in the U.S. It requires that every bridge be inspected at least every 2 years and if any problems are found the frequency of those visits Group 13 - Point Pleasant Bridge Collapse should be increased depending on the problems found in the specific structure (U.S. Department of Transport, 2011). There are over 1,000,000 bridges in America, which are all checked in accordance to the guidelines. The structural integrity of a bridge can now be found using modern non-destructive testing methods such as sonogram reading with a gel and a sound probe, as well as x-raying the frame. Any minor cracks or defects can be acknowledged with maintenance carried out where necessary on older bridges. A lot of older bridges of similar distinction have been replaced with various other modern styled bridges (McGuinness Publishing, 2004). Lessons Learned & Prevention The first lesson to be taken from this tragedy should be to always include some type of redundancy in structural design as a type of safety net against potential failure due to faulty design, underestimation of loading conditions or other such problems. Furthermore, another lesson to be learned is that all structures should be designed and constructed so that all parts of the structure can be easily inspected and maintained. In addition, regulation should be increased and constantly and thoroughly policed and enforced by the relevant governing bodies. It is also evident from this report that structures should be designed with the future in mind. Design loading conditions should be thoroughly reviewed and a design load of 4 or 5 times what is currently required should be designed for. This allows for a change of use of a structure in the future. The Silver bridge was designed for cars that on average weighed 680 kg, and at the time of failure, the average weight of a family car was almost three times that number. Furthermore, the levels of traffic expected greatly increased. This is also applied in environmental engineering in the design of Wastewater Treatment Works (WwTW). A WwTW is designed for an expected population of 2 or 3 times. If the population is predicted to increase in excess of this, then the WwTW needs to be redesigned. References Corrosion Doctors. (1999, August). Corrosion Doctors. Retrieved October 19, 2011, from Corrosion Doctors: http://corrosion-doctors.org/Bridges/Silver-Bridge.htm Lonaker, T. (2006). Silver Bridge Collapse. Retrieved October 19, 2011, from Silver Bridge Collapse: http://www.freewebs.com/silverbridgeaccident/thebridgecollapse.htm McGuinness Publishing. (2004). Mothmen.us. Retrieved October 20, 2011, from Mothmen.us: http://www.mothmen.us/silver-bridge.htm U.S. Department of Transport. (2011). U.S. Department of Transport. Retrieved October 20, 2011, from U.S. Department of Transport Federal Highway Administration : http://www.fhwa.dot.gov/bridge/nbis/nbisframework.cfm Wikipedia. (2011). Wikipedia. Retrieved October 19, 2011, from Silver Bridge: http://en.wikipedia.org/wiki/Silver_Bridge Note: Screen shots taken from BBC documentary “The Point Pleasant Silver Bridge History” Group 13 - Point Pleasant Bridge Collapse Appendix Figure 2 - Stress Corrosion crack formed Figure 4 - Brittle fracture of eye-bar causes it to separate from pin Figure 6 - The twisting of the pin causes the eye-bar on the other side to vibrate off the pin Figure 3 - Combo of high live loads & reduced steel toughness causes brittle fracture failure of eye-bar Figure 5 - Resulting asymmetric load on pin causes it to twist Figure 7 - Eye-bar now completely dismantled causing a domino effect type failure of the suspension structure Figure 8 - the adjacent tower is now destabilised and starts to topple, falling to the north. The bridge deck twisted over, pulling the other rocking tower over with it leading to a complete structural collapse of the bridge