Surfactant Flushing 2009 Pilot Study Fueling Point – Military Site Northeastern USA Jeffrey H. Harwell Asahi Glass Chair of Chemical Engineering The University of Oklahoma Principal Surbec Environmental, LLC Background Jet fuel spill discovered in 2006 Probably happened in 2001 Depth to water 44 ft Sandy aquifer - 20% silt Drinking water wells within ¼ mile but in deeper aquifer Estimated 350,000 to 700,000 gal spill Pilot Study Objectives Surfactant Enhanced Aquifer Remediation (SEAR) • Evaluate effectiveness and efficiency • Demonstrate chemical/hydraulic control • Generate design for full-scale implementation Pilot Study Location • Within the LNAPL plume • generally up-gradient • minimize recontamination • No impact to existing soil vapor extraction system Treatability Study Surfactant system design • Provide proof of concept • Geochemistry considerations • Heterogeneity issues • Optimization of injection strategy • Step 1: Formulate Microemulsion I III II Micelle Monomer Monomer Increasing Salinity Organic Contaminant Step 1: Formulate Microemulsion BA-1 BA-2 BA-3 BA-4 BA-5 BA-6 BA-7 BA-8 BA-9 BA-10 BA-11 Surf. A (wt%) 0.75 0.75 0.75 0.75 0.75 0.75 0.75 0.75 0.75 0.75 0.75 Surf. B (wt%) 0.19 0.19 0.19 0.19 0.19 0.19 0.19 0.19 0.19 0.19 0.19 Salt A (wt%) 1.5 1.5 1.2 1.3 1.4 1.6 1.7 1.8 1.9 2.0 2.1 Salt B (wt%) 0.06 0.10 0.10 0.10 0.10 0.10 0.10 0.10 0.10 0.10 0.10 BA-12 0.75 0.19 2.2 0.10 Yes Clear BA-13 BA-14 BA-15 BA-16 BA-17 0.75 0.75 0.75 0.75 0.75 0.19 0.19 0.19 0.19 0.19 0.8 1.5 1.6 1.7 2.5 0.10 0.10 0.10 0.10 0.10 No Yes Yes Yes Yes Hazy Clear Clear Clear Clear Vials Middle Aqueous Phase Phase No Hazy Yes Clear Yes Clear Yes Clear Yes Clear Yes Clear Yes Clear Yes Clear Yes Clear Yes Clear Yes Clear NAPL Phase Yellow Yellow Yellow Yellow Yellow Yellow Yellow Yellow Yellow Yellow Yellow Hazy Yellow Yellow Yellow Yellow Yellow Yellow Table 1 Microemulsion Phase Behavior Mixture of food grade anionic surfactants Winsor Type I III III III III III III III III III III III I III III III III Step 2: Verify Adsorption Losses are Reasonable Summary of Sorption Test Soil: Water: i= f= Q= Ci = Ceq = V= M= Ft. Drum Ft. Drum sediment - dryed & sieved with #10 (d < 2.0 mm) DI water initial final (mass sorbed/mass media) = (Ci - Ceq)V / M Initial Concentration of surfactant Final Concentration of surfactant volume of solution mass of media Batch M V [Surf A],i [Surf B],i [Total Surf],i [Surf A],f [Surf B],f [Total Surf],f Q, Surf A Q, Surf B Q, Total Surf %, loss of # of surf PV to be applied Name g ml mg/L mg/L mg/L mg/L mg/L mg/L mg/g mg/g mg/g total surf to compensate for the loss AD022409-1 0 15 6652.8 2038.4 8691.2 6652.8 2038.4 8691.2 0.0 1.00 AD022409-2 5.0015 15 0.0 0.0 0.0 0.0 0.0 0.0 0.0 0.0 0.0 AD022409-3 5.0025 15 6652.8 2038.4 8691.2 6384.0 1980.1 8364.1 0.8 0.2 1.0 3.8 1.04 AD022409-4 5.0011 15 3326.4 1019.2 4345.6 3270.4 984.7 4255.1 0.2 0.1 0.3 2.1 1.02 AD022409-5 5.0032 15 665.3 203.8 869.1 406.6 199.3 605.8 0.8 0.0 0.8 30.3 1.30 Note: The analytical results of surfactant A are in the range of ±10%. Table 2 Sorption Studies Very sandy soil; very low adsorption Step 3: Examine Sensitivity to Phase Separation Sample [Surf. A] [Surf. B] [Salt A] ID P-0 P-100 P-300 P-500 P-800 wt% 0.75 0.75 0.75 0.75 0.75 wt% 0.19 0.19 0.19 0.19 0.19 wt% 1.6 1.6 1.6 1.6 1.6 [Salt B] [Calcium Chloride] Presence of Precipitate wt% 0.1 0.1 0.1 0.1 0.1 ppm 0 100 300 500 800 Yes/No No No No No No Table 3 Precipitation and Phase Separation Tests Note: * No phase separation within the first day of observation Presence of Separation Yes/No Yes* Yes* Yes Yes Yes Step 4: Mobility Ratio Solution NAPL Surfactant/Polymer (S/P) Solution Surfactant/Polymer/Alkaline (S/P/A) Solution Polymer μ(Average) (ppm) (cp) 0 100 300 500 800 1,500 0 300 500 500 800 1,500 1.4181 1.4046 1.6949 1.9367 2.7654 3.3162 3.7507 1.4046 2.0927 2.6748 2.6748 3.9592 4.2944 Table 4 Viscosity of Different Solutions Note: m(average) is the average viscosity shown in the unit of centipoise (cp) Step 5: Optimize Injection Sequence Column Test # Description % Recovery Note 1 Surfactant only 99.49 Observed some surfactant retardation 2 2PV Surfactant/Polymer 99.93 Mobilization started on the second PV of surfactant injection 3 2PV Surfactant/Polymer/Alkaline 99.94 Mobilization started on the second PV of surfactant injection 4 0.2PV P/A, 1PV S/P/A, 0.2PV P/A at 1500 ppm polymer* 99.93 More mobilized NAPL in the first PV of mobilization 5 0.2PV P/A, 1PV S/P, 0.2PV P/A at 500 ppm polymer 99.93 More solubilization observed when compared to column test #6 6 0.2PV P/A, 1PV S/P/A, 0.2PV P/A at 500 ppm polymer 99.94 More mobilization observed when compared to column test #5 7 0.05PV P/A, 1PV S/P, 0.05 PV P/A at 500 ppm polymer 99.93 When compared to column 8, less amount of NAPL mobilized and more solubilized NAPL The NAPL was mobilized out from the column 3-5 minutes before column test #7 and there was a higher amount of NAPL mobilized out from column when compared to column test #7 8 0.05PV P/A, 1PV S/P/A, 0.05 PV P/A at 500 ppm polymer 99.93** 9 0.05PV P/A, 1PV S/P, 0.2 PV P/A at 100 ppm polymer 94.6 Less amount of mobilized oil when compared to 500 ppm polymer 10 0.05PV P/A, 1PV S/P/A, 0.05 PV P/A at 100 ppm polymer 90.29 Less amount of mobilized oil when compared to 500 ppm polymer 11 1 PV S/A, no polymer 92.97 Solubilization mechanism is dominant Table 5 Summary of 1-D Column Tests *S: surfactant, P: polymer, A: alkaline; PV = pore volume **yellow highlighted: the optimal surfactant candidate based on the performance of NAPL recovery and the recovery mechanism (mainly mobilization) Pilot Study Overview • • • • • Footprint was < 1/8 acre; well spacing of 25 ft. 2 pore volumes of surfactant at 0.94 wt % 2 nine-spot patterns Submersible pumps recover NAPL/water/surfactant Process equipment • oil/water separator • injection mixing tanks/pumps • injection/extraction manifolds • influent/effluent pumps • carbon vessels Mixing & Holding Tanks, O/W Separator, GAC Canisters Site Map Timeline • Pre-Flush – 1 pore volume – 31 Aug 09 – 6 Sep 09 – Set BioTraps on 3 Sep 09 – Tracer (NaBr) injected 4 – 5 Sep 09 • Surfactant Flush – 2 pore volumes – 6 – 21 Sep 09 – Groundwater sampled on 10 and 17 Sep 09 – Surfactant first observed – EX-02 and OWS on 20 Sep 09 – EX-01 on 23 Sep 09 Timeline • Post Flush - 5 pore volumes – 21 Sep 09 – 1 Nov 09 – Applied vacuum on extraction wells on 25 Sep 09 – Reconfigured injection/extraction on 20 Oct 09 – Groundwater sampled on 1 Oct 09 and 2 Nov 09 – BioTraps 7 Oct 09 – Injected remaining treated water 3 – 6 Nov 09 to empty tanks Mixing Tanks Size: 18,000 Gallons Transfer Pump Mixing Tanks Size: 18,000 Gallons Mixer with propeller Injection Manifold Flow Meters and Flow Controllers Flow Meter Flow Control Unit Remediation and Monitoring Wells Oil/Water Separator 45 min. Residence Time Surfactant Concentrate 330 Gallon Totes Added Manually to Mixing Tank Quality Control Check NaCl: 0.3-1.7% with 0.1% increment 2.5 min 3 min Phase Behavior Test Phase Behavior Test NaCl: 0.3-1.7% with 0.1% increment 1 hour Data Assessment • Pre-Pilot Conditions – API Model estimated 2,300 gal LNAPL • Results – Total LNAPL Recovery was 2,740 gal – API Model estimated140 gal remained LNAPL Thickness/Distribution API Model Soil Sampling Results - Upper Soil Sampling Results - Middle Soil Sampling Results - Lower 11/3 11/1 Sys down from 5 am 1 Nov tp 4 pm 2 Nov for GW sampling 80 10/30 100 10/28 10/26 10/24 10/22 10/20 10/18 10/16 10/14 10/12 10/10 10/8 10/6 120 1,500 60 1,000 40 500 20 0 0 Cumulative Recovery (gal) End of Post-flush (PV5) New configuration 13-hr power outage Cum_OWS 10/4 10/2 Sys down to readjust EX-01 Vacuum applied 2-hr Power outage Post-flush started Cum_total 9/30 9/28 9/26 9/24 9/22 Daily_OWS 9/20 Surfactant-flush started Daily_tanks (estimated) 9/18 9/16 9/14 9/12 9/10 9/8 180 9/6 Tracer injection 200 9/4 140 Pre-flush started 160 9/2 8/31 Daily Recovery (gals/day) LNAPL Recovery Oasis SEAR Pilot Study LNAPL Recovery Note: Vacuum truck events done on 9, 14, 20, 21, 27 Oct, and 9 Nov 09 3,000 2,500 2,000 Extraction Well - Partial Plugging Key Findings • Motivation for full-scale implementation – Significant LNAPL removal - 2,740 gal – Significant reduction in LNAPL thickness – Significant reduction in soil TPH-DRO – Hydraulic control achieved and maintained – No increase in dissolved-phase concentrations – Optimized surfactant formulation Key Findings • Lessons learned as a result of the pilot study – Heterogeneous NAPL thickness along perimeter – Heterogeneous stratigraphy – Mobilization of fine sand – Emulsification within process equipment • Fixes – Better placement of well screens – Improved well locations – Improved surfactant formulation – Longer residence times in oil/water separator Full Scale Implementation Final review with State Regulatory Agency, Military Base Groups on November 12th Decision for full scale (3.6 acres) made - RFP issued Implementing in 3 parcels of 1.2 acres each System installation in May 2010 Surfactant injection in June 2010 Post surfactant flush to be finished November 2010