Proceedings of the Combustion Institute Proceedings of the Combustion Institute 30 (2005) 1611–1618 www.elsevier.com/locate/proci Sensitive in situ detection of CO and O2 in a rotary kiln-based hazardous waste incinerator using 760 nm and new 2.3 lm diode lasers V. Eberta,*, H. Teicherta, P. Straucha, T. Kolbb, H. Seifertb, J. Wolfruma a Physikalisch-Chemisches Institut, Universität Heidelberg, Im Neuenheimer Feld 253, D-69120 Heidelberg, Germany b Institut für Technische Chemie, Forschungszentrum Karlsruhe, D-76021 Karlsruhe, Germany Abstract CO and O2 are key combustion parameters closely linked to the process stoichiometry and most frequently determined by gas sampling. This limits time resolution and hinders the extraction of representative concentration data from inhomogeneous flue gas streams. Especially, batch-fired processes like hazardous waste incineration in rotary kilns (RK) face fast and spatially confined CO fluctuations, making them difficult to optimize. To address this sensor deficiency, we used new 2.3 lm distributed-feedback diode lasers (DFB-DL) accessing the CO-2m-band to develop fast, sensitive, and spatially integrating in situ absorption spectrometers suitable for the harsh conditions in full-scale combustion processes. Spectrally multiplexing the 2.3 lm-DL with a 760 nm-DFB-DL for the O2-A-band we also developed a simultaneous in situ CO/O2 spectrometer, which is most interesting for control strategies requiring the coverage of wide stoichiometry ranges. These new spectrometers were successfully tested for up to two weeks in a 3.5 MWth hazardous waste incinerator. The absorption path (l = 2.56 m, T = 800–1000 C) was located in the post-combustion chamber right at the RK exit. Direct absorption spectroscopy enabled calibrationfree species detection. A new data acquisition system using a digital signal processor and voltage-controlled preamplifiers ensured 100% data throughput, enabled a real-time validity and transmission evaluation of individual laser scans, and thus permitted a real-time transmission compensation and hence an automatic dynamic range adaptation. This proved to be an effective method to avoid systematic errors found in PC-based systems under these rapidly fluctuating combustion conditions. With 1 s acquisition time we achieved for CO/O2 an optical resolution (1r) of 1.2 · 104/6 · 105 OD corresponding to detection limits of 6.5 ppm CO and 250 ppm O2. Sensitivity and time resolution of the spectrometer was high enough to detect—even under fuel lean conditions—small periodic stoichiometry and CO changes caused by the periodic fuel feed of the RK. 2004 The Combustion Institute. Published by Elsevier Inc. All rights reserved. Keywords: Absorption spectroscopy; In situ; Gas analysis; Diode laser; Combustion control 1. Introduction * Corresponding author. Fax: +49 6221 545050. E-mail address: volker.ebert@pci.uni-heidelberg.de (V. Ebert). One of the most important indicators for combustion processes is the carbon monoxide level. Aside from the health issues CO is an important molecule for combustion control purposes. CO 1540-7489/$ - see front matter 2004 The Combustion Institute. Published by Elsevier Inc. All rights reserved. doi:10.1016/j.proci.2004.08.224 1612 V. Ebert et al. / Proceedings of the Combustion Institute 30 (2005) 1611–1618 plays a central role in high temperature corrosion and slagging of boilers in coal- or waste-fired power plants, thereby limiting the plant life time. Of most importance is its role as an stoichiometry indicator, its concentration being related to the combustion completeness and efficiency. Due to the discontinuous feed of solid, viscous or liquid fuels with highly variable calorific values batchfired processes, like hazardous waste incineration in rotary kilns (RK), are plagued with large stoichiometry fluctuations, which generate strong spatiotemporal CO gradients, that cannot be removed by flue gas cleaning. Hence, hazardous waste incinerators (HWI) are often designed as RK followed by a high-temperature post-combustion chamber (PCC). Unfortunately, current gas sensing techniques generally employed in industrial incinerators are mostly based on non-dispersive infrared absorption sensors that cannot detect these CO fluctuations, as they work only extractively, relying on gas samples taken from the flue gas duct. As a result, CO values are significantly delayed by the gas transport to the sensor and distorted by the gas filters needed to cool the gas and to remove dust, soot, and excessive water. In addition, the spatial CO gradients within the flue gas cause large systematic errors since the gas samples are not representative of the average gas composition across the duct. O2, the natural CO-antagonist in most combustors, may also serve as stoichiometry indicator, especially for fuel-lean conditions, when CO may become too low to be detectible. But, as for CO, O2 is mainly detected via slow and error-prone extractive paramagnetic sensors or ZrO2-sensors which only probe locally. These severe limitations of industrial CO/O2 sensing techniques prevent a reliable stoichiometry detection, hinder the development of efficient combustion control strategies, and prevent a minimization of the spatiotemporal CO fluctuations. Consequently, waste incineration processes have to be run with high safety margins, which significantly limit process throughput and minimize costs. Accordingly, there is a large interest in in situ CO/O2-sensors with fast response, high sensitivity, and the ability to determine representative concentrations. Industrial applications require such devices to be robust and inexpensive. One promising technique to fulfill these complex requirements is in situ laser absorption spectroscopy [1]. Especially, near infrared diode lasers (NIRDL) show great potential for industrial applications, as they possess an otherwise unavailable combination of spectroscopic and technical properties. NIRDLs, mainly developed for the telecommunication industries, have a large commercial market and have been extensively optimized. The growing interest in NIRDL-based gas sensors can be deduced from an increasing number of publications over the last few years [1–21]. NIRDLs are frequently used to study CO [7– 10] due to their overlap with the 3m CO overtone band. While these lasers are readily available and rather inexpensive, the weak intensity of the 3m-band allows only moderate detection sensitivities. Commercial room-temperature 2.3 lm diode lasers for the stronger 2m-band were not available until recently, when research grade lasers have been realized as Fabry–Perot structures (FPDLs). Although 2.3 lm FP-DLs enabled first CO measurements in absorption cells or small laboratory flames [11–13,17], they generated many spectroscopic difficulties making them unsuitable for industrial applications. The recently developed, complex gain-coupled, distributed-feedback diode laser (CGC-DFB-DL) [22] may resolve this dilemma, as we show here. Using this new feedback principle a purely single-mode 2.3 lm room-temperature DFB-DL could be fabricated that provides excellent side mode suppression ratio (SMSR), good tunability, and sufficient optical output power [14]. In this paper, we demonstrate the first in situ CO detection in a HWI using 2.3 lm DFB-DLs which is highly interesting for combustion control applications needing a representative, high-sensitivity, high-speed in situ CO sensor. Further, we realized the first simultaneous in situ CO/O2-detection based on 2.3 and 0.76 lm-DFB-DLs, which is very promising for combustion control systems that need to cover wide stoichiometric ranges. 2. Experimental details 2.1. Absorption spectroscopy The measurement principle used in this paper is known as ‘‘direct absorption spectroscopy’’ (DAS). This method, described in detail elsewhere [1–7], permits absolute and calibration-free measurements of absorber concentrations. Thus, DAS is well suited for in situ gas analysis in harsh environments where calibration is difficult. The trade-off for DAS is of lower sensitivity compared to double modulation techniques like wavelength modulation spectroscopy (WMS) [15] and frequency modulation spectroscopy (FMS) [8] or dual beam techniques [16]. The basic setup is rather simple: a diode laser beam is directed through the measurement volume onto a photo detector. The laser is continuously and repetitively scanned over the absorption line by linear laser current modulation, while the detector signal, including all offsets and disturbances, is digitized. Great care has to be taken to correct the in situ signal for various strong disturbances created in the measurement volume: V. Ebert et al. / Proceedings of the Combustion Institute 30 (2005) 1611–1618 these are caused by broadband absorption, scattering by particles or beam steering and create strong fluctuations in the transmission Tr (t) of the measurement path. Further, there may be background radiation E (t) that adds to the laser radiation. Assuming a homogeneous medium, the resulting signal can be described by BeerÕs law [1]: IðkÞ ¼ I 0 ðkÞ exp½SðT Þ gðk k0 Þ N L TrðtÞ þ EðtÞ; ð1Þ where I (k), respectively, I0 (k) are the detected and the initial laser intensity. The absorption signal is described by the temperature-dependent line strength S (T), the absorber number density N, the absorption path length L, and the normalized line shape function g (k k0), which is centered at wavelength k0 [1]. To compensate for rapid transmission and emission variations, we developed techniques to effectively separate them from the molecular absorption by taking advantage of the diode laserÕs fast wavelength tunability [1–7]. By tuning the laser much faster than the disturbances they can be assumed to be constant during the wavelength scan and corrected during the fitting process by removing the offsets first and than dividing the scan through the baseline function. Phase locked averaging of the wavelength scans is used for further noise reduction. Finally, to calculate the absorber number density the absorption line area is extracted using a fitting algorithm. 2.2. CO and O2 spectroscopy Diode laser-based CO detection has been performed (Fig. 1) on the fundamental band at 1613 4.5 lm [23] and on the 2m- (2.3 lm) [11–14,17] and 3m-bands (1.5 lm) [7–10]. The strong 1m-lines frequently used for basic research are only accessible via cryogenically cooled lead salt DL [18] or sparsely available quantum cascade DL [23]. The 3m-band lasers combine low cost and excellent availability with near perfect fiber-coupled DLpackages. However, the 3m-lines are more than 1000 times weaker than 1m and plagued with strong interfering H2O lines. Further, the 1.56 lm lasers are designed to deliver a minimized wavelength chirp, which is contradictory to the gas sensor needs. A good compromise between CO line strength and H2O/CO2 interference is the 2m-band at 2.3 lm, which is about 60· stronger than the 3mband. Synthetic absorption spectra (Fig. 2) calculated using HITRAN96/HITEMP data [24,13] reveal that some CO lines are virtually H2O/CO2 interference free. The R30 line at 2302 nm (Fig. 2) with 1782 cm1 ground state energy is well suited for higher temperatures, while the R18 line (2315 nm) is good for lower temperatures and simultaneous H2O detection. Diode laser-based O2 sensing is only possible via the O2-A-band at 760 nm [3,16] using vertical cavity lasers or as in this paper via non-telecom DFB-DLs. 2.3. 2.3 lm DFB diode lasers DFB-DLs unlike Fabry–Perot types are a near perfect choice for gas phase spectroscopy, combining continuous tuning with spectral purity and stability. However, their complicated and expensive production largely prevents the development of devices outside the telecom wavelengths. Recently, the first commercial samples Fig. 1. HITRAN line strength data of the CO-2n- and 3n-bands, the O2-A-band and the interferences CO2 and H2O. 1614 V. Ebert et al. / Proceedings of the Combustion Institute 30 (2005) 1611–1618 Fig. 2. Simulated CO absorption spectra for a typical gas composition of a combustion process. Laser current tuning is mainly caused by a temperature change by current-induced ohmic heating. However, for kHz modulation frequencies, the temperature response is successively delayed by the thermal mass of the laser module, so that the dynamic current tuning, dm/dI(t), becomes increasingly damped and non-linear. This leads to a severe reduction of the scan depth and a significant asymmetry of the absorption line in time space, which furthermore depends on the position of the absorption line within the scan. As higher modulation frequencies are needed for an effective disturbance suppression, there is a trade-off necessary between suppression effectiveness and scan width reduction, i.e., a complete coverage of pressure broadened absorption lines. Due to the importance of precise dynamic tuning data for calibration-free measurements and stability, we realized a high-resolution measurement of dm/dI(t) as a function of the modulation frequency from 500 Hz to 5 kHz [14]. This range is most important for measurements under the harsh conditions in industrial combustion systems. Compared to the static current tuning this laser showed a strong decrease in the tuning coefficient of 50% even at rather low frequencies of 500 Hz. At 5 kHz, the tuning span was reduced by 66% of the static value and showed a strong non-linearity across the scan with about 30–40% variation between maximum and minimum value of dm/dI(t). of room-temperature 2.3 lm-GaSb-CGC DFBDLs could be fabricated. Based on new lateral metal gratings [22], they eliminate crucial manufacturing steps and allow cost-effective piece-bypiece processing with precise wavelength tailoring for each individual laser. Our first spectroscopic characterization showed that these lasers provide excellent spectral purity (40 dB SMSR), good tunability, and sufficient optical output power (1 mW) at low driving currents (45 mA). Using a gas cell (l = 75 cm, 79 vol.% CO in air at 1 bar, 293 K) and temperature tuning (DT = 18 K) the laser over five CO absorption lines between 2300 and 2305.8 nm we realized the first CO detection with a 2.3 lm DFB-DL. After removal of the amplitude modulation, the resulting spectrum (Fig. 3) coincides well with a HITRAN96 simulation. Temperature tuning extracted from the line positions was very linear with a quasi-static tuning coefficient of 0.423 cm1/K (0.224 nm/K). The static current tuning coefficient determined with a 10 cm airspaced etalon yielded 2.45 · 102 nm/mA (4.6 · 102 cm1/mA). All spectrometers were tested at the 3.5 MWth hazardous waste incinerator THERESA [25] at the Forschungszentrum Karlsruhe (Fig. 4). THERESA is comprised of a rotary kiln (RK, 8.4 m long, 1.4 m diameter) for solid, highly viscous and liquid wastes heated by one 1.5 MWth burner, followed by a post-combustion chamber (PCC, Fig. 3. Measured cell absorption spectrum (black), HITRAN simulation (grey) of 79% CO in air recorded by laser temperature tuning. Quasi-static temperature tuning of the 2.3 lm DFB-DL (line with circles). Fig. 4. Schematic of the hazardous waste incinerator THERESA comprised of a RK and a post-combustion chamber. The CO/O2 measurement location (black arrow) is located in the PCC right at the kiln exit. 2.4. Process and spectrometer setup V. Ebert et al. / Proceedings of the Combustion Institute 30 (2005) 1611–1618 1.9–2.5 m diameter, 12 m height) that is equipped with two 1 MWth burners. The following setup was used to realize in situ CO/O2 measurements in this highly dynamic batch-fired combustion process: the measurement path of the spectrometer was 2.5 m long and located right at the RK exit in the lower part of the PCC. This location minimized signal delays while simultaneously avoiding complications due to the temperature gradients within the RK. Thermal expansion movements of the furnace were compensated for by mounting the spectrometer optics directly onto the furnace walls (Fig. 5). Optical access to the PCC was possible via flanges attached to steel pipes (l = 80 cm, /inside = 100 mm) to cross the furnace insulation. The collimated laser beam was directed into the PCC through Brewster windows (/ = 50 mm), which were purged with intentionally ‘‘leaky’’ window gaskets, taking advantage of the reduced process pressure. This ensured sufficient window transmission over the two-week measurement period. The transmitted light was collected with a 3 in. spherical goldcoated mirror, filtered with dielectric filters (FWHM = 10 nm) to remove background radiation, and softly focused onto an InGaAs detector (/ = 1 mm, cut-off 2.6 lm). Analogous to our previous studies on multi-species detection [3], we spectrally multiplexed a 760 nm DFB-DL with the 2.3 lm DFB-DL to enable the first simultaneous in situ 2m-CO/O2 detection. The two-color laser beam was separated after passage of the measurement volume exploiting the CO filters high reflectivity for 760 nm radiation and directed on silicon and InGaAs detectors. An automatic alignment system [3,7] based on a motor driven #–u-mirror mount and a line-byline search algorithm was used for the initial spectrometer setup and to compensate for load dependent thermal distortions of the combustion chamber. Even under difficult conditions we obtained perfect alignment within a few minutes. Fig. 5. Optical setup of the in situ CO-spectrometer based on the 2.3 lm DFB-DL. 1615 Excellent noise immunity was ensured by isolating the weak modulated laser radiation from the luminous background using phase-sensitive detection. A combined laser/Peltier-element driver stabilized laser current and temperature. A digital signal generator modulated the laser current with a triangular 1 kHz signal. The photodiode signals were preamplified, digitized by fast ADCs, averaged and finally stored for offline evaluation. To extract the absorption line area and simultaneously correct for transmission/emission fluctuations we used a Levenberg–Marquart-Algorithm with approximated Voigt line shapes [26] and background polynomials up to 3rd order. Line areas were converted into concentrations applying the extended BeerÕs law (Eq. (1)), the ideal gas law and taking into account the dynamic tuning coefficient of the laser and the process gas temperatures measured with thermocouples. Spatial inhomogeneities—mainly in temperature—along the beam path are another important issue for in situ measurements, as they affect line strength and shape. To be able to apply the simplifications of Eq. (1), we experimentally verified the temperature variations along the beam path using suction thermocouples. Within the PCC the temperature was typically flat to less than ±50 K. Further, we minimized the effect of changing temperatures on the measured CO mixture fraction to 2.8% per 100 K temperature variation by use of the R30 CO line, which shows a broad maximum in S (T)/T at 1150 K. In the beginning, we used a PC-based data evaluation system based on a 5 Ms/s 12 bitADC-Board (NI 6110E) and custom-designed Labview code under Win98. Due to Win98/Labview limitations only 1–10% of all scans in a given time could be captured. This low duty cycle generated a statistical noise penalty factor of 3–10. To overcome system throughput limitations associated with this PC-based data acquisition (DAQ), a fast monolithic real-time DAQ unit based on a digital signal processor (DSP) and a microcontroller was developed [27]. This system captures and averages 100% of the scans even at kHz modulation frequencies and simultaneously performs a real-time evaluation of individual scans before the averaging process. It contains all electronics necessary to control lasers and Peltier elements, to generate the modulation signals and to readout detector and process control signals. It provides a four channel low-noise analog front end with an electrically variable amplifier gain of ±20 dB and individual 5 Ms/s 12 bitADCs. The 100% data throughput improves the optical resolution by up to a factor of 10 or the temporal resolution by a factor of up to 1000 to the ultimate limit, the laser scan frequency. Utilizing variable amplifier gain and real-time evaluation capabilities of the DSP we developed an advanced data acquisition that can cope with 1616 V. Ebert et al. / Proceedings of the Combustion Institute 30 (2005) 1611–1618 the quite severe and highly dynamic transmission fluctuations found in batch-fired processes. The transmission fluctuations in the incinerator were as large as a factor of 2 within a millisecond and 3–4 orders of magnitude within a second, and thus even faster and stronger than in our previous measurements in full-sized power plants [7]. The custom-designed DSP software simultaneously rejects clipped, excessively distorted or attenuated absorption profiles in real-time. The percentage of the rejected scans depends largely on the temporal and dynamic behavior of the transmission fluctuations. To remove only unusable scans and avoid excessive rejection quota, we largely compensated the transmission variations before the scan digitization by a new closed-loop gain adaptation. This function adapts in real-time for each single wavelength scan the gain of the analog voltage-controlled preamplifiers according to the results of a rapid transmission assessment of the preceding scan performed by the DSP. The gain control loop reacts stepwise within 5–10 ms, i.e., 5–10 scans. This proved in most cases fast enough to deal with the transmission fluctuations in this incinerator. But even if the gain adaptation speed is too small compared to the speed of the transmission changes, excessively distorted scans will still be rejected by the scan evaluation before the averaging procedure. This compensation not only ensured low rejection quota, often below the 1% region, it simultaneously matches the analog signal to the dynamic range of the AD converter, and thus enhanced the resolution compared to the PC-based DAQ. Further, it avoided overmodulation of the front-end amplifier as well as saturation of the ADCs. All these problems created significant systematic errors in the PC-based DAQ, since invalid absorption scans were incorporated in the scan averages. A simultaneous comparison of both data evaluation strategies clearly proved the advantages of the rapid DSP-based scan selection and gain adaptation. The DSP-based DAQ completely avoided the systematic errors, which showed up before as spike like CO excursions, that sometimes were up to a factor of 100 higher than the average CO value. The useful application range of in situ absorption spectroscopy could thus be extended even further to full-scale pulsed batch combustors. fuel lean conditions, similar to those conditions requiring high safety margins to minimize CO peaks. Figure 6 shows typical absorption scans (the CO-2m-R30- and the O2-R17Q18/R19R19 lines) of the dual-species version after transmission/ emission correction, clearly indicating the capability for a simultaneous in situ CO/O2 detection. Both absorption profiles are averages of 1000 wavelength scans captured within 1 s at 1 kHz modulation frequency using the DSPs 100% data throughput. The averaged scans were transferred to a PC via a serial port, as the rather complex final fitting process was still realized on a PC. With 1 s measurement time this reduced the temporal separation between two concentration values to 3.4 s. A future implementation of fast data transfer protocols and DSP-based fitting routines will remove this bottleneck and allow real-time concentration data with millisecond time resolution. The optical resolution of the spectrometer was deduced from the fit residuals. For the R30 line in Fig. 6 (equivalent to 160 ppm CO) we determined an optical resolution, i.e., one standard deviation (1r) of the residuum, of ±1.2 · 104 OD. At 900 C this corresponds to an excellent 1r detection limit of 6.5 ppm CO or a detectivity of 16.5 ppm m s1/2. Compared to our previous CO measurements based on 2.3 lm FP-DLs and PCbased data acquisition [17] we thus achieved a 15-fold resolution improvement. For the O2 lines in Fig. 6, the optical resolution was ±6 · 105 OD. Even though this value is obviously dominated by discrepancies in the line shapes caused by absorption contributions from outside air which have a different line width this is the best optical resolution we have achieved with DAS in a full-scale technical combustor to date. The unknown temperature profile in the 3. Results A 2.3 lm-CO- and a dual-species CO-2.3 lm/ O2-760 nm-spectrometer were successfully tested at the THERESA waste incinerator for periods of up to two weeks. Various solid and liquid fuels were fired under different stoichiometric conditions. CO detection limits were determined under Fig. 6. In situ signals of the R30 CO line (left) and two O2 lines (right), corrected for transmission, emission and amplitude modulation and compared with the fitted Voigt line shape (dashed lines). Fit residuals shown underneath (horizontal dashed lines indicate 2r values of the standard deviation). V. Ebert et al. / Proceedings of the Combustion Institute 30 (2005) 1611–1618 1617 Fig. 7. Periodic CO fluctuations (left) with ±17 ppm amplitude (±10 ppm for 10 s average) measured at the RK exit. A FFT of the fluctuations (right) over a 2 h period shows same frequency as the feeding cycle of the incinerator. air-purged optical access tubes also hampered the absolute O2-evaluation so that only relative O2 changes could be extracted. Based on HITRAN calculations we approximate that 50% of the spatially integrated absorbance is caused by hot gases in the PCC and thus estimate an 1r-O2 detection limit of 250 ppm respectively 600 ppm m, which indicates at least a 4· improvement to our previous studies [2]. N2 or steam purging will remove both problems in the future. The residual noise floor in Fig. 6 indicates that resolutions of about ±1.5 · 105 for O2 (±2.5 · 105 for CO) become available in that case. By combining the current setup with our digital fast scanning WMS technique [15], the resolution may be improved further to below ±1 · 105 OD, so that even in industrial combustors CO/O2 detection limits in the subppm/sub-100 ppm range seem feasible. At the kiln exit we currently found for lean conditions (kburner = 1.5) in average 100 ppm CO and for stoichiometric conditions in a previous study with 2.3 lm FP-DLs [17] 1000–2400 ppm. The first measurement within the kiln, based on 1.5 lm-DLs [17], revealed consistently higher and quickly pulsating CO values of up to 5000 ppm, which could be nicely anti-correlated with the O2 fluctuations, that were simultaneously measured with a 760 nm DFB-DL. In the present study, we could detect similar quasi-periodic CO fluctuations with amplitudes of 30 ppm and 1/30 Hz periodicity (Fig. 7), thanks to the high sensitivity and time resolution of the 2.3 lm DFB-CO-spectrometer. However, the anti-correlated O2 signals were not detected and are probably below our O2 detection limit. The precise frequency of the CO oscillations was determined via a FFT on a two hour set of CO data. The resulting spectrum (Fig. 7) shows a single, pronounced peak at 0.033 Hz. A comparison with other process parameters reveals that these fluctuations coincide nicely with the feed frequency of the solid fuel into the RK. Using the new 2.3 lm-CO-spectrometer it is therefore possible to detect in real-time the small fluctuations in the combustion stoichiometry caused by the introduction of new fuel into the process. 4. Summary and conclusion Two calibration-free absorption spectrometers for the sensitive and rapid in situ CO/O2-detection in harsh combustion environments have been realized for the first time. New 2.3 lm- and 760 nm DFB-DLs were successfully used to enable a simultaneous CO/O2-detection right behind the kiln exit in a hazardous waste incinerator. Direct absorption spectroscopy in combination with DSP-based real-time transmission/emission correction as well as automatic alignment techniques were deployed. A 1 s measurement time allowed optical resolutions in the 104–105 OD range, which permitted 1r-detection limits of 6.5 ppm CO and 250 ppm O2. Hence, small periodic CO and stoichiometry fluctuations could be detected in the incinerator even under fuel lean conditions. The CO and the CO/O2 spectrometers are therefore powerful tools for active combustion control strategies to optimize full-scale batch-fired combustors, even if a wide stoichiometry range has to be covered. Since the spectrometer is easily expandable to other species[1–3,7] or other parameters like gas temperatures [3] or gas residence times [6] DSP-enhanced in situ absorption spectrometers will become very valuable tools for advanced combustion control applications. Acknowledgments We thank J. Koeth for providing the 2.3 lm laser. V.E. thanks J. Fleming for his valuable assistance. Contributions of the THERESA control team and the financial support by the state of Baden-Württemberg within the COSI-Project is acknowledged. 1618 V. Ebert et al. / Proceedings of the Combustion Institute 30 (2005) 1611–1618 References [1] V. Ebert, J. Wolfrum, in: F. Mayinger, O. Feldmann (Eds.), Optical Measurements. Springer Verlag, Heidelberg, 2001, pp. 227–265. [2] V. Ebert, J. Fitzer, I. Gerstenberg, K.-U. Pleban, H. Pitz, J. Wolfrum, M. Jochem, J. Martin, Proc. Combust. Inst. 27 (1998) 1301–1308. [3] V. Ebert, T. Fernholz, C. Giesemann, H. Pitz, H. Teichert, J. Wolfrum, H. Jaritz, Proc. Combust. Inst. 28 (2000) 423–430. [4] E. Schlosser, T. Fernholz, H. Teichert, V. Ebert, Spectrochim. Acta 58/11 (2002) 2347–2359. [5] E. Schlosser, J. Wolfrum, B.A. Williams, R.S. Sheinson, J.W. Fleming, V. Ebert, Proc. Combust. Inst. 29 (2002) 353–360. [6] E. Schlosser, J. Wolfrum, L. Hildebrandt, H. Seifert, B. Oser, V. Ebert, Appl. Phys. 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Phys. Lett. 81 (2002) 4330–4331. A. Kosterev, F.K. Tittel, R. Köhler, C. Gmachl, F. Capasso, D.L. Sivco, A.Y. Cho, S. Wehe, M.G. Allen, Appl. Opt. 41 (2002) 1169–1173. L.S. Rothman, C.P. Rinsland et al., J. Quant. Spectrosc. Radiat. Transfer 60 (1998) 665–710. H. Dittrich, L. Malcher, H. Seifert, VDI-Berichte 1629 (2001) 397–402 (in German). E.E. Whitting, J. Quant. Spectrosc. Radiat. Transfer 8 (1968) 1379–1384. V. Ebert, Rev. Sci. Instr. 2004, in preparation. Comments Gus Nathan, University of Adelaide, Australia. Did you validate the effect of particle scattering by simultaneous measurement with a third line, tuned away from any absorption bands? Reply. The effect of particles on the in situ absorption signals has been described in the text and in our previous publications, as referenced in our paper. Particles generate spectrally broadband losses along the absorption path and reduce the total optical power which can be directed from the laser to the detector. However, the shape of the absorption line itself and even the baseline of the absorption signal will not be changed, since the laser is intentionally scanned much faster than typical changes in the particle density. Thus the broadband absorption effects generated by particles can be corrected for by a simple multiplicative term in the Lambert Beer Law Eq. (1). d Franz Winter, Vienna University of Technology, Austria. Along your optical path you may experience in large-scale combustors a wide range of CO concentrations. How will this affect your quantitative data evaluation? Reply. Any absorption spectrometer will integrate the absorption signal over the entire absorption path and thus provides a path-averaged CO concentration only. This is an important feature of our in situ absorption spectrometers and a quite useful property, as it avoids the pitfalls of common, locally acting sensors and provides a much more representative CO signal than any single-point measurement.