Fabrication and test of the LDX levitation coil

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IEEE TRANSACTIONS ON APPLIED SUPERCONDUCTIVITY, VOL. 13, NO. 2, JUNE 2003
Fabrication and Test of the LDX Levitation Coil
Philip C. Michael, Alexander Zhukovsky, Bradford A. Smith, Joel H. Schultz, Alexi Radovinsky, Joseph V. Minervini,
K. Peter Hwang, and Gregory J. Naumovich
Abstract—The Levitated Dipole Experiment (LDX) was designed by Columbia University and the Massachusetts Institute
of Technology to investigate plasma confinement within a dipole
magnetic field. The experiment consists of a 5 m diameter by
3 m tall vacuum chamber and three superconductor coils: a
Nb3 Sn Floating Coil that provides the dipole field for plasma
confinement; a NbTi Charging Coil that inductively charges and
discharges the Floating Coil current; and a high temperature
superconductor (Bi-2223) Levitation Coil that electromagnetically
supports the weight of the 620 kg Floating Coil and controls its
vertical position within the vacuum chamber.
LDX is the first U.S. plasma confinement experiment to use
a high temperature superconductor coil. The use of high temperature superconductor minimizes the electrical and cooling
power needed for levitation, allowing additional power for plasma
heating. The levitation coil is a 2800 turn, 1.3 m outer diameter,
double pancake winding. It is designed to operate at up to 150
A current at 20 K and is cooled by a combination of one stage
cryocooler and liquid nitrogen cooled radiation shield. This paper
provides details for the design, fabrication and test of the coil.
Index Terms—High temperature superconductor, fusion magnets, conduction cooled superconductor.
I. INTRODUCTION
T
HE Levitated Dipole Experiment (LDX) is an Innovative
Concept fusion experiment that was developed to investigate steady-state, high-beta plasma operation, with near-classical magnetic confinement. Major factors that set LDX apart
from earlier experiments are the absence of toroidal field coils,
and its emphasis on magnetic flux expansion [1]. Plasma is confined by a single superconductor coil, the Floating Coil (F-coil)
[2] that is magnetically supported near the center of a 5 m diameter by 3 m tall vacuum chamber.
The base configuration of the experiment uses a conductioncooled, disk-shaped, high temperature superconductor Levitation Coil (L-coil), mounted on top of the vacuum vessel, to support the F-coil. For this configuration, the F-coil is stable to
tilt and horizontal displacements, thus reducing control requirements for off-axis motions.
The vertical position of the F-coil is sensed optically, and concm band near the midplane of the vacuum
trolled within a
vessel by varying the voltage applied to the L-coil. Feedback
control simulations for F-coil positioning anticipate a nominal
Manuscript received August 6, 2002. This work was supported by the U.S.
Department of Energy under Contract DE-FG02-98ER82529 and Contract
DE-FG02-98ER54458.
P. C. Michael, A. Zhukovsky, B. A. Smith, J. H. Schultz, A. Radovinsky, and
J. V. Minervini are with the MIT Plasma Science & Fusion Center, Cambridge,
MA 02139 USA (e-mail: michael@psfc.mit.edu).
K. P. Hwang and G. J. Naumovich are with Everson Electric Company, Bethlehem, PA 18017 USA (e-mail: phwang@eversonelec.com; gnaumovich@eversonelec.com).
Digital Object Identifier 10.1109/TASC.2003.812808
Fig. 1. Section view of the L-coil winding and cryostat.
L-coil operating current of 105 A with a superposed
A, 1 Hz
control current ripple [3]. The largest predicted heat load on the
L-coil is magnetization hysteresis loss produced in the HTS conductor by the control current ripple [4]. The predicted a.c. loss
is roughly 10 W, assuming full penetration of both the axial and
radial field variations into the conductor. To provide margin for
larger than anticipated control current ripple and resulting a.c.
loss, the L-coil’s heat removal path was conservatively designed
for an average heat load of 20 W, with a temperature difference
between L-coil hot spot and one-stage cryocooler below 2 K.
II. L-COIL WINDING AND CRYOSTAT
Fig. 1 shows a cross-section view of the L-coil winding
and cryostat. The L-coil was fabricated at Everson Electric
Company to an MIT design. The L-coil contains approximately
7300 m of American Superconductor Corporation’s (ASC)
Three-ply Narrow Bi-2223 superconductor. The conductor
consists of PIT-processed Bi-2223 in a silver alloy matrix that
is clad on both sides with 35 m stainless steel [5]. Eighteen
spools of 440 m conductor length were procured for L-coil
fabrication. The average conductor thickness and height were
0.234 mm and 3.0 mm. Each spool contained from zero to
three conductor splices per spool, with guaranteed resistance in
the superconducting state of less than 200 n per splice. The
average self-field critical current for the conductor was 63 A
at 77 K.
The main parameters for the L-coil are listed in Table I. The
L-coil is a disk-shaped, double pancake winding, with the pancakes wound to either side of a center support plate. The support plate consists of two 1.0 mm (0.04 ) thick copper sheets
that are epoxy laminated to either side a 9.5 mm (3/8 ) thick
stainless steel plate. The copper sheets conduct heat from the
L-coil to a thick copper ring mounted at the inner diameter of
1051-8223/03$17.00 © 2003 IEEE
MICHAEL et al.: FABRICATION AND TEST OF THE LDX LEVITATION COIL
TABLE I
L-COIL DESIGN PARAMETERS.
the coil. This ring is connected through a flexible thermal link
to the cryocooler. The stainless steel plate minimizes L-coil deflection when it electromagnetically supports the roughly 620
kg F-coil. The copper sheets are radially segmented to limit eddy
current losses and are separated from the stainless steel by 0.25
mm thick glass fabric.
The pancakes are joined at their inner diameters by a 0.51
mm thick by 102 mm long OFHC copper sheet. We fabricated
the center transition joint by soldering the ends of two, approximately 1 m lengths of HTS tape near the top and bottom edges
of the copper sheet. The assembled joint was insulated, passed
through a circumferential slot in the support plate, and loosely
shimmed to the proper radial location to begin the winding. Two
Teflon®-coated, stainless steel rings with 3.35 mm height and
7.95 mm radial build were bolted to either side of the support
plate to provide winding mandrels for the pancakes. The joint
lead on the lower side of the support plate was secured and the
plate was mounted to the winding turntable. The joint lead on
the upper side of the support plate was spliced to the first spool
of conductor with indium solder.
Because it was impractical to confirm in-process, the resistance of the superconductor splices made during winding, considerable effort was devoted to the development and qualification of splice fabrication methods. Analysis prior to winding
showed that if the splices were free from voids, the splice resistance would be dominated by the conductor’s stainless steel
cladding [6]. Visual inspection of the soldered joints was considered sufficient to guarantee splice quality. The L-coil contains
a total of 34 ASC qualified splices, and 22 splices made during
winding.
The L-coil was tension wound using a strain gauge instrumented idler arm and an electrically controlled drag motor, following the winding tension schedule shown in Table II. The
tensioning schedule was developed to minimize the accumulation of compressive hoop stresses near the inner diameter of the
winding. Each pancake was terminated by indium soldering a
0.51 mm thick by 102 mm long by 12.7 mm tall OFHC copper
sheet to the final conductor turn. Five layers of turn insulation
were wrapped around the outer diameter of the pancake to com-
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TABLE II
L-COIL WINDING TENSION SCHEDULE.
Fig. 2. Variation in the axial and radial magnetic field constants vs. radial
location, at three vertical heights in the L-coil upper pancake.
plete the ground insulation, followed by ten layers of scrap conductor, to mechanically protect the coil o.d. during subsequent
processing.
Once the first pancake was complete, it was covered with a
layer of ground insulation, an Armalon® parting sheet, and a
close fitting potting lid. The coil assembly was flipped over and
remounted to the winding turntable to wind the second pancake.
After both pancakes were complete, they were epoxy potted to
enhance thermal conduction to the support plate copper sheets.
III. ANTICIPATED D.C. PERFORMANCE
The L-coil is optimized to produce the radial field needed for
F-coil levitation using minimal conductor volume [4]. The resulting coil design approximates a circumferential directed current sheet and produces a rather unique magnetic field distribution on the L-coil conductor. Fig. 2 plots as a function of radial
location, axial and radial magnetic field constants at three axial
heights within the upper pancake. The field constants were calculated assuming uniform conductor current density. The radial
field constants vary over the single- conductor height of the pancake from near zero at the center support plate to a maximum
value of about 3.7 mT/A at its upper surface. At each height
in the coil, the radial field is near constant across the coil’s radial build. The axial magnetic field constants are uniform over
the height of each pancake, but vary from a maximum value of
mT/A at the outer
about 8.8 mT/A at the inner diameter to
diameter.
The critical current density of HTS tapes depends on both the
magnetic field orientation and the magnetic field intensity. ASC
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IEEE TRANSACTIONS ON APPLIED SUPERCONDUCTIVITY, VOL. 13, NO. 2, JUNE 2003
Fig. 3. 77 K critical current vs. background field intensity for L-coil
conductor exposed to axial and radial magnetic fields. Load lines for the coil’s
peak axial field and the average radial field at the mid-height of the pancakes
are over-plotted in the figure. The L-coil critical current (28 A) is determined
by the lower intersection of load line and critical current curves.
provides scaling data that enables their customers to estimate
critical currents for various applications based on a conductor’s
measured 77 K self-field critical current, the background field
orientation and intensity, and the operating temperature [7]. Fig.
3 shows the expected 77 K critical current vs. field intensity for
the L-coil conductor in both axial and radial field orientations.
Representative load lines, for the peak axial field in the pancakes, and average radial field at the pancake mid-height are
also plotted in this figure. The intersection of each load line and
critical current curve shows the coil’s critical current for that
field orientation. Fig. 3 indicates that the L-coil critical current
is determined by the coil’s radial field component. Because the
radial field at each height is nearly constant across the coil’s radial build, nearly all of the coil should simultaneously exit the
superconducting state during a ramped current experiment. The
expected L-coil critical current at 77 K is roughly 28 A.
IV. LEVITATION COIL TEST
The L-coil was immersed in liquid nitrogen and tested at 77
K to confirm its viability prior to further integration into the
L-coil cryostat. Tests were performed to determine total splice
resistance, coil critical current, and normalized a.c. losses.
A. Instrumentation
Voltage taps were installed across each pancake and across
the entire L-coil. Five Cryogenic Linear Temperature Sensors
(CLTS) were installed to monitor the coil and support plate
cool-down temperature profiles. The mounting location included: one sensor each on the top and bottom surfaces of the
pancakes at radial locations 0.52 m from the winding axis; and
three sensors on the support plate copper sheets, one at the
inner diameter of the coil and one each on the top and bottom
surface of the support plate at its outer diameter. Two sets
of axially directed Hall probes were installed on the top and
bottom surfaces of the pancakes at radial locations 0.21 m from
the winding axis.
Fig. 4. Temperature vs. time traces during conduction cooling of the L-coil.
B. Conduction Cooling
The test cryostat was equipped with an internal 15 l liquid
nitrogen reservoir that that was placed in the bore of the L-coil
and used to conduction cool the L-coil from room temperature
to approximately 120 K. Conduction cooling was used to
minimize differential thermal stresses during cool-down.
Eighty-four strips of AISI 1100, commercial pure aluminum,
with 2.5 cm width, 0.41 mm thickness and 0.3 m length were
bolted to the top and bottom surfaces of the coil support plate
at its inner diameter. The strips were bent up, and over the rim
of the reservoir and immersed in liquid nitrogen to begin coil
cooling. The height of liquid in the reservoir was controlled
with an automated refill system.
Fig. 4 shows the cool-down temperature vs. time traces at
various coil locations. All temperatures remained within 20 K
of each other throughout cool-down. The cooling rate of the coil
was initially about 25 K/hr, but decreased exponentially as the
temperature difference between the coil and nitrogen reservoir
decreased. As the temperature traces asymptotically approached
130 K, we increased the refill rate for the nitrogen reservoir,
and temporarily restored the cooling rate to about 10 K/hr. The
rapid cooling observed following 25 hr in Fig. 4 was obtained
by filling the test cryostat with liquid nitrogen.
C. DC Performance
The L-coil was connected in series with a 0.3 resistor and
V to perenergized at several dc voltages between 3 V and
form splice resistance measurements. At each series voltage, the
coil voltage was recorded after the coil current had settled to a
quasisteady value. The total L-coil resistance determined by this
; this confirms an average resistance of
method was
n for all conductor splices.
Fig. 5 shows a critical current measurement for the L-coil at
a current ramp rate of 0.04 A/s to 38 A current. The inductive
voltage in this figure was offset to zero at the start of the current
ramp to highlight the critical state transition. The critical current
for the L-coil was calculated using the relation:
MICHAEL et al.: FABRICATION AND TEST OF THE LDX LEVITATION COIL
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remain within the power supply voltage limits. Because a different excitation current was used for each experiment, we first
processed the ac loss data by dividing the in-phase voltage component by the coil current to obtain the equivalent loss resistance
values shown in Fig. 6. The roughly linear variation of the equivalent loss resistance with frequency is indicative of a hysteresis
loss mechanism.
We further processed the loss data to obtain normalized a.c.
coil loss energies of 2 to 5 J/cycle at 1 A current excitation;
these loss energies are slightly less than, but consistent with our
design expectations [4].
V. CONCLUSION
Fig. 5. L-coil voltage vs. current trace during a critical current measurement
using a 0.04 A/s current ramp to 38 A.
A high temperature superconductor Levitation Coil was fabricated for the LDX program at Everson Electric Company using
ASC conductor. Recent tests with the L-coil immersed in liquid
nitrogen confirm the coil performance with respect to its design
predictions. The L-coil cryostat is under fabrication at Everson
Electric and system integration should be complete by the end
of the year.
ACKNOWLEDGMENT
The authors thank the American Superconductor Corporation
for its leadership in the U.S. Department of Energy, Office of
Fusion Energy Sciences Phase II SBIR program that supported
the L-coil construction. They especially thank L. Masur and A.
Otto, whose efforts were vital to the project.
Fig. 6. Equivalent a.c. loss resistance for the L-coil vs. excitation frequency.
REFERENCES
where
is the coil voltage at operating current,
is the
electric field criterion (1 V/cm) used to define the conductor
critical current, is an “index” number that defines how steep is
the critical state transition, and is the total length of conductor
(7300 m) in the L-coil. At 77 K, the measured L-coil critical
current was approximately 33 A, with an index number in the
range 12–12.2. Both pancakes showed nearly identical critical
current values. The measured critical current was roughly 18%
larger than the value predicted in Fig. 3.
D. AC Loss
AC losses were measured electronically over the frequency
range 0.02 Hz to 4.0 Hz. To perform the measurements, a sinuV
soidal function generator was connected to 4-quadrant,
A KEPCO power supply, which was used to drive the
by
L-coil. The current amplitude was adjusted at each frequency to
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[2] B. A. Smith et al., “Design, fabrication and test of the react and wind,
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11, pp. 2010–2013, Mar. 2001.
[3] T. S. Pederson et al., “Computer simulations and design of levitation
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with the 10th International Congress on Plasma Physics, Quebec City,
Canada, Oct. 2000. presented.
[4] J. H. Schultz et al., “High temperature superconducting levitation coil
for the levitated dipole experiment (LDX),” IEEE Trans. Appl. Superconductivity, vol. 11, pp. 2004–2007, Mar. 2001.
[5] L. Masur et al., “Long length manufacturing of BSSCO-2223 wire for
motor and cable applications,” Adv. Cryo. Eng., vol. 46, pp. 871–877,
2000.
[6] P. Michael, “Joint Resistance Estimates for L-Coil Splices, Rev. 1,” MIT,
Cambridge, MA, LDX Project Memo LDX-MIT-PMichael-083 001-01,
Aug. 30, 2001.
[7] Bi-2223 High Strength Reinforced Wire Fact Sheet.
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