Technical Paper Slag Control Treatment Program at EKPC Spurlock Station Authors: Mark Gabriel, Manager, Business Development, GE Water & Process Technologies Logan Pickrell, Process Engineer, East Kentucky Power Cooperative Abstract Coal burning power plants today are challenged by economic slowdowns and lower prices for the electric power they produce. With reduced power prices, many power companies are looking to stay competitive by burning lower cost, lower quality fuels. Switching fuels can often be more difficult for the plants to burn. Moreover, the most efficient and low cost producing plants are being kept at higher load for longer periods of time than ever before. The changes in fuel quality and boiler operation have caused many plants to experience an increase in slag deposits on the furnace walls and superheater sections of their boilers. Spurlock Station boilers 1 and 2 are sub-critical boilers with a capacity of 340 MW and 585 MW respectively. Both units currently burn 100% Illinois Basin coal. Illinois Basin coal is high sulfur, low fusion temperature coal. Burning some Illinois Basin coals would create a buildup of hard slag formation inside the boiler. Typical issues included the formation of large clinkers on SH assemblies. Spurlock Station has experienced large slag falls causing boiler damage and safety concerns. In January of 2010, Spurlock started treating their boilers with a unique GE Water & Process Technologies chemical additive to reduce the detrimental effects of burning high slagging index, low fusion temperature coal. This paper describes how the evaluation was conducted and summarizes the boiler performance results. Discussion In addition to carbon, hydrogen and oxygen found in coal, there are numerous inorganic impurities that are not combustible and contribute to slagging and convective pass fouling in the boiler. These inorganic constituents impact the ash fusion temperatures. Fusion temperatures often can correlate directly to the tendency for slag formation in the boiler. Slag deposits form when boiler fireside temperatures exceed the fusion temperature of the ash. Slag density increases with time and temperature, creating a deposit that is hard and difficult to remove with normal sootblowing. If the sootblowers cannot remove the ash build up from the upper areas of the boiler in a timely manner, the slag deposits can continue to grow, harden, and form to an enormous size. These slag deposits typically form on the leading edge of the platen superheat tubes, secondary superheater tubes or pendant reheat tubes located above the furnace or above the bull nose of the boiler. When the slag eventually does fall, it can puncture slope tubes or damage entire sections of the lower furnace, forcing unscheduled downtime and lost generation. Fouling deposits may also form in the convective back-pass sections of the boiler by condensation of gaseous ash components. Fouling deposits are typically associated with the Vertical Reheater, Primary Superheater, and Horizontal Reheater tubes. Fouling deposits can bridge across these tubes and restrict gas flow to the point of furnace plugging off. Fouling may result in a Unit derating on load, or force the boiler to be shut down for a cleaning. Find a contact near you by visiting www.ge.com/water and clicking on “Contact Us”. * Trademark of General Electric Company; may be registered in one or more countries. ©2011, General Electric Company. All rights reserved. TP1190EN.doc Jul-11 2. Also, clinkers that did form were much more difficult to grind in the bottom ash grinding operation. Operating experience also showed that under operating conditions of 100% of Coal-A, conditions could deteriorate in a matter of a few days. In order to minimize the impact of the high sulfur ILB coal, Spurlock Station opted to blend their high sulfur, high slagging index coal with lower sulfur, higher cost coal. Table 1 shows the plants typical fuel sources, tonnage and relative cost. The impact of slagging and fouling can be costly. The lost economics can be the result of unit derates, unscheduled outages, high cleaning cost, repair costs from slag fall damage, and incremental costs associated having to burn more expensive fuels. Chemical additives in combination with mechanical ash removing devices can improve control of slagging and fouling deposits on the fireside of the boiler and reduce their overall negative impact. Boiler Operating History Chemical Additive for Slag Control Spurlock Station boilers 1 and 2 are sub-critical boilers with a capacity of 340 MW and 585 MW respectively. Unit 1 is a B&W opposed wall-fired design while Unit 2 is a CE T-fired design. The scrubber for Spurlock Unit 2 became operational in October of 2008 while the scrubber for Unit 1 became operational in June of 2009. Installing the scrubbers allowed Spurlock to switch from low-sulfur compliance coal to high sulfur Illinois Basin coal. Cost advantages of high sulfur Illinois Basin coal were significant, however there were concerns that slagging tendencies would increase significantly. Fuelsolv* FMG2960 is a highly concentrated oil based liquid additive that contains a proprietary blend of magnesium and copper based compounds. Its primary use is to inhibit slag build up on the radiant sections of the boiler (furnace walls, nose arch, radiant superheaters, and finishing superheaters). It works by altering the sintering characteristics of slag. The FMG2960 is fed directly to the coal, which greatly simplifies the feed. Transition metals and other multivalent metals such as copper have been used for many years as combustion catalysts. Not as well known is that copper, in combination with magnesium, can be an effective slag control agent and acts to reduce the cohesive strength of ash particles. If the cohesive strength is reduced, the ash becomes more friable and easily removed by soot blowing and operational load shedding. Operating experience in 2009 showed that burning 100% of Illinois Basin (ILB) Coal-A caused a severe slagging situation that resulted in the formation of large clinkers on the bottom of Pendant Platen Superheat assemblies on Unit 1. Severe slagging caused bridging across RH assemblies, blockage of gas lanes, costly de-rates and slag falls and resulted in unscheduled outages for off-line cleaning on Unit Coal Source Relative Price, $/MMBTU Heat Value, BTU Sulfur Content lb/MMBtu Slagging Index Tons/ Month Coal-A $0.0000 11,200 6.79 2.81 45,000 Coal-B $0.1995 12,500 4.13 0.95 30,000 Coal-C $0.2466 11,300 5.21 1.50 15,000 Coal-D $0.3463 11,300 5.21 1.50 25,000 Coal-E $0.5011 11,000 5.92 1.50 30,000 Coal-F $0.6343 12,200 6.57 2.01 20,000 Coal-G $0.8309 11,500 4.05 0.89 20,000 Coal-H $1.8857 11,500 4.87 1.13 20,000 Table 1 Page 2 Technical Paper Treatment Application Fuelsolv FMG2960 was applied directly to the coal at the Unit 1 and 2 Crusher House. The target dosage was 75 ml of FMG2960 per ton of coal treated. See Figure 3. FMG2960 feed was automated to two belts, PC1A and PC1B. Typically PC1A feeds Unit 1 while PC1B feeds Unit 2, however either belt can feed either unit. Chemical feed was automated using a 4-20 mA signal from each belt scale, with coal-on-belt and belt running permissive signals. An ACTech Variable Frequency Drive (VFD) and Periflo peristaltic chemical metering pump were dedicated to each belt. The Fuelsolv FMG2960 was delivered to the plant in 240gallon totes and transferred using a high volume transfer pump. A temporary feed system, for the purpose of conducting an evaluation of the FuelSolv FMG2960 slag control technology was relatively simple to install once all of the feed system components were on site. The feed system for Spurlock station was installed and operational in about 3 weeks’ time. (See Figure 1 and Figure 2) Hard slag formation across Pendant RH on Unit 2 Clinker formation on bottom of Pendant SH on Unit 2 Large clinker formation on Platen SH sections on Unit 1 Damaging slag falls on both units Unscheduled down time due to slag falls Unscheduled down time for off-line cleaning Boiler Performance Derates due to uncontrolled slag formation The objective of the FuelSolv FMG2960 slag control program was to minimize the impact of slagging while burning a high percentage of lowest cost, high sulfur, high slagging index coal. The intent was to burn 100% of Coal-A during an initial evaluation, when possible. Success of the program would be determined by the following criteria: Tools Technical Paper A number of different tools were used to document the conditions in the boilers treated with the FuelSolv FMG2960. These included: FMG2960 Application Rate Visual Inspections Slag Ratings Page 3 Digital Infrared Photography Digital Videography Off-line inspections with standard digital photography Daily Coal Belt Samples The FMG2960 Application Rate was monitored daily. Actual product usage was compared to coal tonnage since last reading to calculate milliliters of FMG2960 per ton of coal and compared to the target rate of 75 ml/ton. Application rate monitoring provides alerts to potential feed system problems and helps ensure a consistent product application rate over time. Figure 4 shows typical application rate over time. The addition of a 4-20 mA signal from each coal belt improved overall application rate control. Figure 4 Visual Inspections were conducted on a daily basis and recorded in a Visio template with Digital IR Photography. The inspections establish a point in time record and form the basis for daily slag ratings. Figures 5 and 6 represent examples of the inspection document format. Slag Ratings were developed in order to convert information from visual observations into empirical data. The data can then be used to trend performance of the slag control program when compared to coal quality or other boiler operating conditions. The slag rating used is on a scale from 0 to 5 with boiler specific criteria for each level. A slag rating of 0 represents very little slag formation while a rating of 5 represents severe slag conditions. Page 4 Figure 5 Digital Videography was used routinely to record conditions and observe the impact of periodic events such as soot blowing. A standard digital video camera in an air-cooled enclosure was typically used to record slag buildup between RH assemblies from either sidewall observation port on the Unit 2 CE boiler, in 15-30 second video clips. Off-line inspections documented with digital photography were conducted following every planned and unplanned outage. Inspections were conducted at the earliest possible time following boiler cool down. This is the best time to examine the fireside of the boiler for clinkers. It is also a good time to assess the ability for existing slag to shed as the boiler cools down and the friability of any remaining slag Technical Paper significantly with the addition of the FMG2960 slag control program. Unit 2 operated at very good levels of slag control throughout the evaluation period. The feed of the highest slagging index coal began following the start of the FMG2960 slag control treatment program. Daily Coal Samples were conducted to provide a reference to coal and ash quality through the early stages of the FMG2960 evaluation. The intention was to compare coal quality to observed slagging conditions in the treated boilers. The evaluation period on Unit 2 began on 1/29/2010 and ended on 5/9/2010. Throughout this period plant operations experienced no observed clinker formation on Planten SH and were able to consistently control slag buildup at the hot spot on the right side of the Front Pendant RH. Results Summary Unit 1 and 2 began evaluations of the FMG 2960 at different points in 2010. Unit 2 began its slag control evaluation on January 29th, while Unit 1 began its slag control evaluation on April 19th. The plan with Unit 2 was to run 3 of 5 silos with 100% Coal-A throughout the evaluation period. The plan with Unit 1 was to run 100% Coal-A during its evaluation period. In the past, Spurlock Station was unable to run either boiler with this fuel diet. In both cases, baseline information from visual observations was established. Slag Ratings-Unit 1 operated at high slag ratings for the period of approximately 3 months leading to the start of the FMG2960 evaluation. Slag buildup in trouble spots on Unit 1 decreased significantly as indicated by the visual observations and the resultant slag ratings. Figure 7 shows Unit 1 slag rating over time versus coal burned. Coal-A and Coal-F are the highest slagging index coals. Overall slag control improved Technical Paper Unit 2 slag control was most effective when sootblowers IK#5 through IK#10 were deployed every 3 to 4 hours. However compressed air capacity was a limiting factor at times, restricting sootblower availability. Infrared Digital Photo- The ability to control slag was evident when comparing observed conditions prior to and during treatment with the FuelSolv FMG2960 additive. Page 5 Unit 1-100% Illinois Basin Coal-No Treatment Unt 1- Bottom of Rear SH Platen from Front wall at Center Right 6-18-10 Unt 1- Pendant SH from Front wall Right 3-26-10 Unt 1- Pendant SH from Front wall Left 3-26-10 Heavy slag buildup on SH Pendants and bottom edge of SH Platens. Slag falls from Platens caused damage to lower furnace tubes. No Slag buildup on SH Pendants. No Clinkers on bottom edge of SH Platens. No slag falls from Platens. Unit 2 experienced similar results. The FuelSolv FMG2960 treatment program did not eliminate slag buildup; however, slag that did develop was more friable and easier to remove with sootblowing. Outages Unit 2 experienced three outages in March, May and October 2010, following the start of the FuelSolv FMG2960 treatment program. In the March outage, clean gas paths between RH assemblies were observed. Little slag was seen on the bottom of the SH Pendants. The slag that was present was a very brittle and friable deposit that shed easily as the unit came down and cooled. Some wall clinkers that did not shed as the unit cooled were present. The largest wall clinker at the Left Front Wall trouble spot was removed with a shotgun in about an hour. Compared to the prePage 6 Technical Paper vious clinker in the same location, the clinker was more brittle and easier to remove. The previous clinker had to be high-pressure water blasted. possible to soot blow the areas where slag buildup occurred at the frequency that was required. Unit 2-October 12th Outage Likewise in the May outage, most existing clinkers shed as the unit came down and cooled. The largest wall clinker at the Left Front Wall trouble spot was removed with a shotgun in about 10 minutes. Compared to the previous clinker in the same location, the clinker was more brittle and easier to remove. The previous clinker took about an hour to remove. No off-line, high-pressure water blasting was required. Unit 2-March 5th Outage SH Pendant, Bullnose and RH from IK #10 In the Unit 2 October outage, some slag was observed at the bottom of the RH at the bullnose near the right corner. Mostly clear gas paths were observed between RH assemblies. The large clinker at the Left Front Wall trouble spot would not break up with a shotgun but shed as the boiler temperature dropped overnight. Small clinkers present at the bottom of SH Platens were easily removed with a shotgun. Aside from some small clinkers, furnace walls appeared very clean. Lower Bullnose and SH Assemblies from IK#1 RH Gas Lane Right Wall from IK #10 Lower Bullnose and SH Assemblies from IK#2 Impact of Load Drop Unit 2 experienced 18 days at the highest slag rating due to bridging on right RH & inability to remove with sootblowing. Under these circumstances Unit 2 was dispatched to a reduced load causing slag to shed. No noise or damage was caused by the thermal de-slag. Burning the same coal blend in 2009, Through some periods during the FuelSolv FMG2960 treatment program, the ability to soot-blow was limited. This was primarily due to limitations of the plants compressed air system. It was not always Furnace pressure went positive and everything behind the RH went very negative. Technical Paper Slag developed over 80% of RH ID Fan Inlet pressure equaled –33 inches Furnace pressure at +9.6 inches (Unit trips at +10 inches) Page 7 Fuel Cost Savings Unit 2 RH from Right Wall at IK #10 7-2-10 As many as eight different Illinois Basin coal sources were used to fuel Units 1 and 2 in 2010. Coal-A was the lowest cost, but the coal with the highest slagging tendencies. In the past Spurlock Station was unable to continuously burn Coal-A. Burning alternate fuels came at an incremental cost per ton. Coal-A comprised 22% of all coal burned in 2010. Relative costs of all fuels are shown in Table 10. Minimum savings associated with the ability to burn Coal-A are shown in Table 11 while maximum savings are shown in Table 12. Replacing Coal-A with 100% Coal-B is not practical and so the total Fuel Cost savings are realistically between $2,413,000 and $7,600,000. Total operating cost for the FuelSolv FMG2960 program is estimated at $2,172,000. Conclusions Unit 2 RH from Right Wall at IK #10 after De-rate 7-4-10 Impact of Slagging and Fouling Index The fouling index of coal burned in Unit 2 increased significantly. EKPC Spurlock found a different type of buildup during the May 2010 Air Heater repair outage. A lighter weight fouling deposit was seen as opposed to the heavy slag typically seen. Slagging or fouling that did form came off tubes easier with sootblowing. Figure 9 shows coal slagging and fouling index plotted against slag rating. We saw Unit 2 slag rating increase due to deterioration of burner tips over time. Page 8 The FuelSolv FMG2960 program was successful when applied directly to a coal belt and combined with targeted sootblowing practices. Application of FMG2960 slag control chemistry with consistent boiler operating practices produced the following results: Eliminated clinkers on Unit 1 SH Platens and eliminated damaging slag falls Reduced pluggage on Unit 2 RH. Slag that formed was brittle and easily removed with air sootblowers The majority of slag that developed shed at shutdown, eliminating much of the cost of offline high pressure water blasting Slag that did form broke up very easily, significantly reducing problems with grinding hard bottom ash FMG2960 enabled EKPC Spurlock to regularly burn high slagging coals without pluggage or large slag falls Enabled EKPC Spurlock to burn high slagging coals that they were not able to burn in the past Reduced overall fuel costs by as much as $7,000,000 per year Technical Paper Table 10 Supplier Incremental Delivered Price, $/ MMBtu BTU/lb Tons/Month Coal A $0.0000 11,200 45,000 Coal B $0.1995 12,500 30,000 Coal C $0.2466 11,300 15,000 Coal D $0.3463 11,300 25,000 Coal E $0.5011 11,000 30,000 Coal F $0.6343 12,200 20,000 Coal G $0.8309 11,500 20,000 Coal H $1.8857 11,500 20,000 Total Tons 205,000 Total Tons Non “Coal A” 160,000 Table 11 Alternative to “Coal A” Source % of Total Coal Burned (less Coal A) Equivalent Tons MMBtu Monthly Savings Annual Savings Coal B 100 40,320 1,008,000 $201,096 $2,413,052 Total Savings Assuming Replacement with 100% of Lowest Cost Alternative $2,413,052 Table 12 Alternate to “Coal A” Source % of Total Coal Burned (less Coal A) Equivalent Tons MMBtu Monthly Savings Annual Savings Coal B 18.8 7,560 189,000 $37,706 $452,466 Coal C 9.4 4,181 94,500 $23,304 $279,644 Coal D 15.6 6,969 157,500 $54,542 $654,507 Coal E 18.8 8,591 189,000 $94,708 $1,136,495 Coal F 12.5 5,164 126,000 $79,922 $959,062 Coal G 12.5 5,478 126,000 $104,693 $1,256,321 Coal H 12.5 5,478 126,000 $237598 $2,851,178 $632,473 $7,589,673 Total Savings Assuming Replacement with Historical Proportion of Alternatives Technical Paper Page 9