Group 17 Wexford Bridge Wexford Bridge – Chloride Ingression Group 17 Vincent Carey Amy Fitzpatrick Patrick Gibbs Mick McCarthy Fig. 1 Introduction Wexford Bridge (fig. 1) spans across the river Slaney that flows diagonally northwest to southwest dividing Wexford in two. The first bridge was wooden. It was constructed in 1794 at a cost of £15, 000 (approximately one million euro). In 1959 a seven span pre -stressed concrete balanced cantilever was constructed in its place. It spans 400 meters with piers spaced 63 meters apart. The deck needed to be replaced in 1997 due to effects of the marine environment. This will be discussed below. Discussion The original bridge was a seven span prestressed concrete balanced cantilever bridge. On inspection of the reinforced concrete, it was found that there was an excessive chloride ion content, which had resulted in serious corrosion of the reinforcement and prestressing anchors together with lamination and the spalling throughout the bridge. The corrosion had advanced to them point that the structural stability of the bridge was no longer adequate. With no possibility of salvaging the existing structure, which was irreparable, the only solution was to demolish it and rebuild the bridge. Before we analyse the replacement bridge we must first examine why the original bridge failed. To do this must answer the question what is chloride ingress? 1 Group 17 Wexford Bridge What is chloride ingress? Chloride ingress is one of the main causes of reinforcement corrosion in reinforced concrete structures. It can be said to occur in two distinct two stages. Firstly, the chloride ions must be transported from either within or without the concrete to the areas containing the reinforcement. This usually occurs through the chloride content of the water in the concrete. The water carrying the chloride ions diffuses much quicker than the ions do themselves which leads to a build up or accumulation. If they are in close proximity to steel reinforcement they will begin to attack it. This is the second stage in the process. The chloride ions destroyed the protective passivation layer, which surrounds the reinforcement bars in the concrete. Then provided that oxygen is present, corrosion will begin on the bars themselves. This type of corrosion is called pitting corrosion. Over time it can reduce the strength of the reinforcement and thus its ability to resist mechanical stress, and if left unchecked, will eventually lead to structural failure. Why does it occur? The main reason for chloride ingress is due to exposure to a saline environment. Salt water carries chloride ions through its salt content. Thus, exposure to a marine environment is a major threat to the durability of reinforced concrete structures. Other factors influencing the time for corrosion initiation from chloride ingress are the initial chloride level, the concrete quality, mix type and water-tocement ratio, concrete cover over reinforcement, consolidation, curing and the environment. Penetration of the chloride ions is affected by the heterogeneity of the material, so defects in the structure coupled with a saline marine environment makes the situation extremely hazardous. How can we prevent this? Laboratory corrosion and chloride penetration studies on ordinary Portland cement (OPC) and sulphate-resisting cement (SRPC) have been carried out and report better performance of OPC cement over SRPC cement. Investigations into the influence of different cement types on chloride-induced corrosion of reinforcing steel show that OPC performs better than SRPC in terms of chloride binding capacity, chloride diffusivity and reinforcement corrosion. In addition, the temperature of concrete plays a significant role in the diffusion rate of chloride ions increasing with the elevation of temperature. Proper placement and consolidation of concrete also determines the final quality and durability of concrete. With regard to diffusion of chloride in OPC cement, investigations show that concretes of good (consolidated) and poor (nonconsolidated) qualities have significant differences in diffusion coefficients, from which average values of non-consolidated concrete were more than two times the values of consolidated concrete. The specification and codes of practice have recommended threshold chloride values varying in the range 0.l-0.4% (or more) by weight of cement depending on the cement used and the moisture content of concrete. In general, there are three levels of chloride concentrations, expressed by weight of cement. These are low chloride content where the chloride content is up to 0.4%, medium chloride content where it is in the range 0.4-l .0%, and high content which exceeds 1.0% of the cement content. 2 Group 17 Wexford Bridge Results A new superstructure (fig. 2) has replaced the 383m long Wexford Bridge during a 10-week road closure. The replacement bridge, designed by Barry & Partners, is a continuous steel girder deck with a composite concrete slab. The girders are supported off the reconstructed original piers and abutments. The design philosophy was for maximum prefabrication of the structural elements to enable replacement in the shortest time possible. Exposed steel was painted with a Marine A 20 year maintenance specification. The interior of the structure between the steel flanges was enclosed by metal decking. Defective and laminated concrete in the bridge piers as well as areas showing high levels of electrochemical potential were broken out to expose corroding reinforcement. Repairs were carried out using repair concrete or mortar including a corrosion-inhibiting additive. Conclusion In conclusion, once it was decided to take down the Wexford Bridge and replace it due to the fact that it was in a state of disrepair, the best solution was to use good quality, highly consolidated OPC cement in the replacement bridge. It was also noted that due care and attention should be taken at the time of placement and considerations should be made for the ambient temperature at the time of construction, as these factors would further influence the performance of the new bridge against further chloride ingress. The replacement structure was built in 1997. It incorporates a continuous steel girder deck with a composite concrete slab. Corrosion inhibitors where added along with pozzolanic binders capable of immobilizing free chlorides to improve the durability of the new structure. In addition, a hydrophobic surface treatment was applied and the steel was painted to a 20-year marine specification. Fig. 2 References: www.iseroi.ie www.asconltd.ie www.barry&partners.com 3