1 2 sio Vi n, M ission, Values & Stra teg y sio Vi n, M ission, Values & Stra teg y ture & Passion Cu l set, Market & Customer Orientation ntin uo ntin uo nd Mi ture & Passion tion, Creativity & Co tion, Creativity & Co us us Le Le n ar ing n ar ing Cu l set, ira nsp s-I ira nsp s-I nd Mi am Te am Te Market & Customer Orientation 3 INTRODUCTION TITLE OF THE PROJECT Reduction in consumable nozzle cost With improved efficiency THEME OF THE PROJECT Waste Elimination TEAM DETAIL Meeting Day : Tuesday , Meeting Time : 3:30 PM Ownership Area : Welding Machine Area Team formation date : 01.07.04 TEAM MEMBER RESPONSIBILITY K.V. Joshi( Leader) To Provide Resources and Guidance, Data analysis & Use of PS Tools P.J. Prajapati Execution of jobs mentioned in action plan such as welding, brazing etc. Mahendra Panchal Development of fixtures related to spot facing and internal drilling Mehul Kachhia Machining of fixtures related to spot facing and internal drilling ( Operation of Lathe and milling machine) Pravin Chitte Equipment Study and Co-ordination during machining jobs 4 5 Hindalco Industries Limited (Unit : Birla Copper ) Village : Lakhigam P. O. : Dahej - 392130 Taluka :Vagra District : Bharuch Gujarat Birla Copper Complex 6 Product Profile BIRLA COPPER – Cathode (99.99%) – Continuous Cast Rod • in 8, 11, 12.5, 16 and 19mm dia . Precious Metals (99.9 %) – BIRLA Gold – BIRLA Silver DAP & Complexes – Birla Balwan • Di-Ammonium Phosphate (DAP) • 20:20:0 Ammonium phosphate sulphate • NPK 10:26:26 & NPK 12:32:16. By Products Copper Slag Sulphuric Acid Selenium PGM Mix Phospho Gypsum HFA 7 Achievements 8 Birla Copper's quality standards are recognized internationally. It has been accorded the LME (London Metal Exchange) registration: its copper cathodes marketed as "Birla Copper", have been approved as a 'Grade A' Copper brand by the LME. Birla Copper has been accredited ISO-9001:2000 (Quality Management System) and ISO-14001:1996 (Environmental Management System) certification. Recommended for OHSAS – 18001 Certification. Dahej Harbour and Infrastructure Ltd. has been awarded the ISO 9001:2000 (Port Management for Handling Dry and Liquid Cargo) certificate by KPMG. Birla Copper is awarded commendation certificate - Ramakrishna Bajaj National Quality Award 2002 of Indian Merchant Chambers for Business Excellence and Quality Achievements in manufacturing companies category for the year 2002 9 Our Focus Areas Receiving third prize in CII QC Circle Competition at Ahmedabad. Receiving third prize in Inter Hindalco Kaizen Competition at Renukoot. (January 2005) Process Flow 10 11 QUALITY POLICY – BIRLA COPPER We at Birla Copper are committed to evolving and sustaining excellence in every area of activity . Birla Copper will be driven by a sharp focus on maximizing customer satisfaction . Towards that end, an accent on quality will mark every aspect of our operation We will also work continuously to improve on existing processes and introduce innovative technology. P Balakrishnan Executive President-Birla Copper 12 PROBLEM Unavailability of Plasma Cutting Machine on account of non availability of Nozzles Lower cutting length per Nozzle High cost of nozzles 13 FISH BONE DIAGRAM Method Improper Method of cutting Material Cutting Head Holding Time Cutting Profile Tightness of Nozzle Improper Cutting Head Height Plate Thickness Hole Worn Out Gap at Plate Bottom Moisture in Air Nozzle Head Operating Personnel skill Spacer Ring Air Pressure Material’s Personnel Availability Improper Earthing Machine Type of SS Material Man 14 WHY-WHY ANALYSIS Unavailability of Plasma Cutting Machine WHY Earthing Problem WHY It was difficult to maintain the Gap between plate and Nozzle WHY Burr Generation WHY Nozzle Hole became Oval Shaped instead of Circular 15 Plasma Cutting Nozzle New Nozzle Damaged Nozzle 16 PDCA CYCLE P STEP 1 STEP 2 STEP 3 STEP 4 D STEP 5 C STEP 6 A STEP 7 Act Plan Check Do 17 ROOT CAUSE After brainstorming, It was found that High consumption of nozzle is attributable to oval shape in cutting nozzle hole and due to this Nozzle is getting discarded. Can we do with this Oval Shaped Nozzle and make it further usable ????????? 18 ACTIONS TAKEN Brazing of Oval Shaped Nozzle with 1805 Copper Filler Wire. Inside Spot facing to maintain 1.5 mm gap between plasma electrode and cutting nozzle. Ø 1.4 mm center hole drilling on lathe 19 PROBLEM FACED IN IMPLEMENTATION During brazing, metal of nozzle melt and distort the shape and size of nozzle. Inside holes provided for cooling, get chocked. Holding of Nozzle for Spot Facing Holding of Nozzle for Internal Hole drilling ACTION TAKEN TO OVERCOME THE FACED PROBLEM Instead of conventional top heating (90º job heating) , we have used inclined heating (45º job heating) Fixture has been developed for spot facing as per drawing. Fixture has been developed for internal hole drilling as per drawing. 20 Fixture for Spot Facing and Internal Drilling 21 22 RESULT ACHIEVED Reduction in Consumption of Cutting Nozzles. Uninterrupted Availability of Plasma Cutting Machine. Cutting length per nozzle (in meter) increased. Reduction in Inventory of Cutting Nozzle. 23 BASIC COST FOR PROJECT: Cost Of Implementation per Nozzle (In Rs.) Brazing – Spot Facing – Hole Drilling Total - Rs. 07.00 Rs. 13.00 Rs. 05.00 Rs. 25.00 Thus total repair cost per nozzle is Rs.25/ as against Rs. 400/ for a new one 24 TANGIBLE BENEFITS: (A) Consumption of Cutting Nozzle (Before Improvement) = 725 Nos./Year Consumption of Cutting Nozzle (After Improvement) = 290 Nos./Year Cost of One Nozzle procured from O.E.M. = Rs. 400/ Cost of Repairing one Nozzle = Rs. 25/ (725-290)x(400-25) = Rs. 1,40,625 /- per annum Total saving per annum is Rs.1,40,625 /- 25 TANGIBLE BENEFITS: Down time (Before Improvement) Down time (After Improvement) (B) = 20 hrs./month. = 0 hrs./month. Thus reduction in down time per annum =240 Man hrs/ annum Total saving per annum is Rs.1,40,625 /- 26 KEY LEARNING 1. Better understanding of the use of problem solving tools. 2. Improved communication skill. 3. Opportunity for management. team members to give suggestion to 4. Enhancing team capability for presentation in front of public audience. 5. Better understanding of methodology. 6. Better service to internal customer. 27 THANK YOU.