Research in Brief Procedures for dealing with bodyside windows broken in service T1024 For more information contact: enquirydesk@rssb.co.uk November 2015 ‘...allowing operational delays to be reduced.’ Aim There are a number of different approaches used by train operating companies (TOCs) with regards to bodyside windows broken in service. This research sought to investigate these approaches with the objective of minimising operational speed reductions and allowing trains to continue to operate with defective windows in a safe and cost effective way whilst minimising delay. Findings The practice of applying an emergency glass repair film is more common for high speed operators where window breakage is associated more with cold weather and weather events during the winter months than other causes. For medium and low speed vehicle fleets window breakage appeared to be more associated with vandalism. The windows tested comply with GM/RT2100 ‘Requirements for Rail Vehicle Structures’ issue 5 in normal and damaged conditions which indicates that there is no increase in risk to passengers if the outer pane of a window had been damaged. The research found that there are two conditions to be considered when the outer pane of a double glazed window is fractured: •When there is no hole, or a hole less than 85mm diameter, there is no technical reason to fit emergency window repair film or remove the window. •When there is a hole greater than an 85mm diameter, it is recommended that either the glass is removed or emergency window repair film is fitted. Large holes in fractured windows make the broken pane unstable when subjected to pressure pulses (eg when two trains pass). Emergency window repair film stabilises the damaged pane. In deciding to fit emergency window repair film, the TOCs should consider the risks for its operation of: •Glass dice from fractured outer panes becoming detached due to further impacts and therefore any potential consequences due to the effect of train speed. •Contact or interference at stations by passengers 2 When emergency window repair film is fitted to bodyside windows, the procedure contained in Appendix C of the research project report should be followed. The procedure only requires the film to be applied to the fractured glass minimising the risk of damage to vehicle paintwork. If a vehicle’s windows do not comply with GM/RT2100 or with the former BR Standard BR 573, the window design should be tested to the current standard. Impacts and benefits The research has delivered much needed data on the physical performance of train bodyside windows, both in intact and damaged conditions. It tested and identified suitable emergency window repair films which will benefit the rail industry. It also delivered a procedure which can be used to apply emergency window repair film to windows broken in service, both in wet and dry conditions. This enables better management of broken bodyside windows in service allowing operational delays to be reduced. Method The research project was split into two distinct phases. The objectives of the first phase were to: •Establish the practices and procedures employed by TOCs for dealing with train bodyside windows broken in service. •Identify and evaluate the emergency window repair films that are available to be used by the rail industry for managing train bodyside windows broken in service. The second phase of the project was designed to: •Deliver a testing regime to develop a better understanding of the physical properties of glazed systems used in bodyside windows of rail vehicles, both when intact and damaged. •Develop common solutions for bodyside windows broken in service based on a better and quantified understanding of the properties and limitations of windows. The research examined data obtained from TOCs to establish the frequency, and possible causes of, windows broken in service. This research also tested train windows in both intact and various degraded conditions. The tests used Mk III carriage bodyside windows as this represented the fundamental design features found on many other vehicles. In the various damaged conditions tested, windows were tested with and without window repair film applied. Small missile test apparatus 3 Where to find out more Both phases of this research project have now been published RSSB’s web portal SPARK http://www. sparkrail.org/Pages/Results.aspx?k=T1024&s=All%20Records. 4