Challenges and Solutions for Cleaning No-Clean Flux Residues from Surface Mount Components Eric Camden Foresite, Inc Kokomo, IN Experimental Procedure Test Vehicle Umpire Board Populated with LCC, TQFP, and BGA Other parts available, focusing on low standoff SMT components for this study DOE Details In this study we looked at four groups of 10 Umpire test boards with identical level of contaminates. 40 Umpire boards were all processed with no-clean paste and then each component area was doped with 5ml of liquid flux, using a syringe to control application. The processing conditions are as follows Group Details Control – Fluxed Not Cleaned Group 1 – DI water only wash and rinse Group 2 – saponified wash with DI water rinse Group 3 – saponified wash, steam cleaned , DI water rinse Wash Details 2 FPM 140oF 60 PSI Top 40 PSI Bottom 52 each 1 GPM Nozzles total for wash, rinse tank mirrors wash. Test Matrix After the cleaning process all four groups of boards went through SIR testing and Ion Chromatography testing to determine the most effective cleaning approach. All SIR testing was performed to IPC TM-650 2.6.3.3(A), and IC was performed to IPC TM-650 2.3.28, with the IC extractions being performed on localized areas beneath the components after removal. Control Group Control group was not washed at all after conditioning Examples of BGA, LCC, and QFP on board and underneath components Control Group continued Baseline IC Data Sample Description Foresite Limits SMT NC Acetate Cl- Br- NO3- SO42- WOA Na+ NH4+ K+ <3 <3 <12 <3 <3 <25 <3 <3 <3 6.65 7.61 8.54 2.36 9.42 5.78 6.07 1.92 3.05 3.71 4.57 3.84 4.14 3.64 4.25 3.36 0.96 0.21 0.50 0 0.69 0.34 0.42 0.06 0.69 0.53 0.70 0.52 0.47 0.31 0.50 0.69 3.36 3.44 3.23 1.86 2.82 3.06 3.38 1.16 398.95 181.24 155.32 2.67 385.02 187.87 148.98 6.54 6.25 7.15 6.69 0.51 5.78 4.89 4.51 0.65 4.91 5.61 6.30 1.74 6.95 4.26 4.48 1.42 1.74 1.36 1.40 1.37 1.28 1.69 1.21 1.88 9.47 10.63 8.95 2.67 4.26 4.84 3.98 3.48 0.62 0.39 0.26 0 0.53 0.69 0.89 0.80 3.44 3.60 3.29 1.69 385.45 177.62 176.54 5.02 6.95 3.97 5.24 0.51 6.99 7.84 6.60 1.97 1.70 1.88 1.27 1.92 10.33 9.85 9.52 2.65 4.42 3.50 3.51 3.69 0.37 0.34 0.34 0.06 0.69 0.47 0.59 0.65 3.06 3.39 3.51 1.22 391.24 180.36 162.71 4.24 5.77 6.52 4.54 0.53 7.62 7.27 7.02 1.96 1.21 1.88 1.65 1.84 Control - not cleaned Control Umpire 4 BGA Control Umpire 4 LCC Control Umpire 4 TQFP Control Umpire 4 Ref. area H2 Control Umpire 5 BGA Control Umpire 5 LCC Control Umpire 5 TQFP Control Umpire 5 Ref. area Control Umpire 6 BGA Control Umpire 6 LCC Control Umpire 6 TQFP Control Umpire 6 Ref. area Control Umpire 12 BGA Control Umpire 12 LCC Control Umpire 12 TQFP Control Umpire 12 Ref. area Baseline SIR Data Board # Pattern Umpire 8 BGA Umpire 8 LCC Umpire 8 TQFP Umpire 8 Head2 Umpire 9 BGA Umpire 9 LCC Umpire 9 TQFP Umpire 9 Head2 Umpire 10 BGA Umpire 10 LCC Umpire 10 TQFP Umpire 10 Head2 Umpire 11 BGA Umpire 11 LCC Umpire 11 TQFP Umpire 11 Head2 Initial 24 hour 96 hour 168 hour Final 1.78E+12 4.17E+07 2.88E+07 6.31E+06 1.78E+12 1.67E+12 8.32E+05 8.32E+05 8.32E+05 1.20E+06 8.99E+11 6.46E+06 5.50E+06 5.01E+06 1.20E+09 2.14E+11 8.32E+09 9.55E+09 1.10E+10 7.76E+11 1.82E+12 3.09E+07 3.02E+07 2.29E+07 1.58E+12 1.78E+11 8.32E+05 8.32E+05 8.32E+05 8.32E+05 1.74E+12 5.37E+07 3.72E+07 2.63E+07 6.17E+11 3.98E+11 2.57E+09 1.70E+09 1.51E+09 1.78E+12 2.34E+11 8.32E+05 8.51E+05 9.55E+05 9.12E+05 1.78E+12 2.63E+07 1.86E+07 1.66E+07 2.00E+09 2.09E+11 1.00E+06 2.00E+06 1.12E+06 9.77E+05 1.62E+11 8.31E+10 1.91E+09 8.91E+09 1.12E+11 1.86E+12 3.09E+07 1.62E+07 1.29E+07 1.66E+12 1.32E+11 8.32E+05 8.32E+05 8.32E+05 1.62E+06 6.71E+11 8.13E+05 8.91E+05 8.51E+05 9.77E+05 7.59E+12 1.77E+09 1.12E+09 1.10E+09 9.12E+11 Control Results Bad. Of course these are worse case scenario type boards but good baseline data for the 3 cleaned groups. Group 1-IC Results DI water only wash and rinse Sam ple Description Foresite Limits SMT NC Acetate Cl- Br- NO3- SO42- WOA Na+ NH4 + K+ <3 <3 <12 <3 <3 <25 <3 <3 <3 DI Water Washed ONLY - Aquastorm 200 heated to 140F Group 1 Umpire 20 BGA Group 1 Umpire 20 LCC Group 1 Umpire 20 TQFP Group 1 Umpire 20 Ref. area Group 1 Umpire 21 BGA Group 1 Umpire 21 LCC Group 1 Umpire 21 TQFP Group 1 Umpire 21 Ref. area Group 1 Umpire 22 BGA Group 1 Umpire 22 LCC Group 1 Umpire 22 TQFP Group 1 Umpire 22 Ref. area Group 1 Umpire 23 BGA Group 1 Umpire 23 LCC Group 1 Umpire 23 TQFP Group 1 Umpire 23 Ref. area 2.01 5.62 5.33 2.04 2.98 5.55 5.23 1.54 3.07 3.72 3.45 2.64 3.48 3.64 3.11 2.04 0.16 0.18 0.34 0.09 0.26 0.14 0.57 0 0.51 0.44 0.36 0.27 0.49 0.60 0.45 0.21 1.71 3.81 3.55 1.56 3.03 2.40 2.76 1.06 135.65 104.74 118.21 1.16 201.36 101.38 121.31 1.68 2.87 3.25 2.35 0.42 2.52 2.13 4.12 0.56 2.72 7.62 7.22 2.77 4.04 7.52 7.09 2.09 1.24 2.06 2.11 1.82 1.05 1.50 1.44 1.19 4.21 5.74 5.64 1.69 3.70 3.51 4.15 2.14 0.40 0.21 0.63 0.08 0.80 0.42 0.75 0.40 2.91 3.59 3.41 1.16 167.95 96.65 105.27 1.88 3.25 3.26 3.25 0.45 5.71 7.78 7.64 2.29 1.61 1.36 1.14 1.89 4.86 6.59 6.85 2.74 4.24 4.33 4.04 2.41 0.62 0.22 0.65 0.07 1.08 0.46 0.85 0.55 3.63 1.78 2.97 1.21 175.64 97.89 124.51 1.92 2.98 2.54 2.69 0.51 6.59 8.93 9.28 3.71 2.07 1.20 2.94 1.23 Group 1-SIR Results DI water only wash and rinse Board # Pattern Umpire 14 BGA Umpire14 LCC Umpire 14 TQFP Umpire 14 Head2 Umpire 15 BGA Umpire 15 LCC Umpire 15 TQFP Umpire 15 Head2 Umpire 16 BGA Umpire 16 LCC Umpire 16 TQFP Umpire 16 Head2 Umpire 17 BGA Umpire 17 LCC Umpire 17 TQFP Umpire 17 Head2 Initial 24 hour 96 hour 168 hour Final 2.19E+12 1.41E+08 2.95E+08 9.55E+07 1.55E+10 2.24E+12 2.09E+07 8.51E+07 2.24E+07 5.37E+08 1.74E+12 6.17E+07 1.29E+08 5.75E+07 9.55E+07 1.70E+12 1.32E+09 1.95E+09 9.12E+09 1.66E+12 2.04E+12 9.33E+07 5.89E+07 5.01E+07 1.95E+10 2.14E+11 4.27E+07 3.09E+07 3.02E+07 3.89E+09 1.91E+12 7.08E+07 3.89E+07 4.17E+07 1.91E+08 1.95E+12 8.51E+09 1.23E+09 7.76E+09 1.62E+12 1.62E+12 2.14E+08 1.41E+08 9.33E+07 1.91E+08 1.32E+12 4.07E+07 2.82E+07 2.82E+07 5.37E+06 2.04E+12 7.76E+07 4.68E+07 4.79E+07 5.79E+07 2.04E+12 4.07E+09 2.24E+09 7.94E+09 1.38E+12 1.86E+12 1.38E+08 7.41E+07 6.92E+07 2.09E+09 9.33E+10 3.63E+07 2.51E+07 2.69E+07 7.24E+07 2.00E+12 5.89E+07 3.55E+07 3.63E+07 1.86E+08 2.04E+12 9.10E+09 7.94E+09 6.76E+09 1.95E+12 Group 1 Results Still Bad. As expected the data after wash with DI water only is better than the control data but still exhibits very high levels of corrosive flux residues, primarily the acetate, WOA, and ammonium. DI water alone does not have enough cleaning energy to remove the uncomplexed flux residues in tight spaces Group 2-IC Results Saponified Wash/DI Rinse Sample Description Foresite Limits SMT NC Acetate Cl- Br- NO3- SO42- WOA Na+ NH4 + K+ <3 <3 <12 <3 <3 <25 <3 <3 <3 Saponifier Washed - Aquastorm 200 heated to 140F Group 2 Umpire 26 BGA Group 2 Umpire 26 LCC Group 2 Umpire 26 TQFP Group 2 Umpire 26 Ref. area Group 2 Umpire 29 BGA Group 2 Umpire 29 LCC Group 2 Umpire 29 TQFP Group 2 Umpire 29 Ref. area Group 2 Umpire 31 BGA Group 2 Umpire 31 LCC Group 2 Umpire 31 TQFP Group 2 Umpire 31 Ref. area Group 2 Umpire 35 BGA Group 2 Umpire 35 LCC Group 2 Umpire 35 TQFP Group 2 Umpire 35 Ref. area 1.95 1.32 1.36 0.84 1.96 1.50 1.27 0.91 1.73 1.48 1.10 1.09 1.05 0.86 1.04 1.30 0.26 0.16 0.06 0.04 0.23 0.19 0.22 0.06 0.42 0.36 0.25 0.33 0.45 0.62 0.58 0.31 1.42 1.24 1.49 0.78 1.36 1.75 1.27 1.07 79.85 53.26 74.11 0.22 84.06 61.48 78.11 0.58 2.36 2.44 2.63 0.41 2.06 2.14 2.17 0.15 2.64 1.79 1.84 1.14 2.66 2.03 1.72 1.23 0.32 0.26 0.25 0.17 0.26 0.25 0.34 0.28 1.56 1.59 1.47 0.84 1.03 0.55 1.14 0.98 0.24 0.15 0.42 0.06 0.26 0.51 0.22 0.09 1.36 1.27 1.32 0.89 91.45 59.64 81.41 1.02 2.35 2.69 2.48 0.34 2.11 2.16 1.99 1.14 0.36 0.26 0.25 0.36 1.71 1.67 1.30 0.84 1.36 1.45 1.22 1.48 0.40 0.10 0.23 0.03 0.41 0.36 0.26 0.35 1.63 1.78 1.54 0.95 74.58 63.28 74.61 0.59 2.36 2.05 2.65 0.37 2.32 2.26 1.76 1.14 0.41 0.51 0.36 0.28 Group 2-SIR Results Saponified Wash/DI Rinse Board # Pattern Umpire 24 BGA Umpire 24 LCC Umpire 24 TQFP Umpire 24 Head2 Umpire 25 BGA Umpire 25 LCC Umpire 25 TQFP Umpire 25 Head2 Umpire 30 BGA Umpire 30 LCC Umpire 30 TQFP Umpire 30 Head2 Umpire 32 BGA Umpire 32 LCC Umpire 32 TQFP Umpire 32 Head2 Initial 24 hour 96 hour 168 hour Final 2.19E+12 1.17E+08 3.72E+08 9.33E+07 1.62E+10 5.62E+12 2.34E+07 9.77E+07 3.47E+07 5.01E+09 2.09E+12 2.75E+07 1.07E+08 4.27E+07 8.91E+09 2.09E+12 1.07E+09 1.95E+09 8.91E+09 1.48E+12 2.14E+12 3.02E+07 1.45E+08 6.31E+07 1.78E+10 6.17E+12 1.38E+07 9.12E+07 3.72E+07 5.37E+08 2.00E+12 1.91E+07 1.26E+07 4.68E+07 1.78E+10 2.04E+12 1.15E+09 2.82E+09 3.79E+09 1.78E+12 2.24E+12 1.12E+08 2.40E+08 1.02E+08 1.70E+09 6.92E+12 2.19E+07 3.99E+07 3.55E+07 5.62E+09 1.95E+12 2.95E+07 2.02E+07 4.68E+07 1.38E+10 2.00E+12 8.71E+09 1.86E+10 8.71E+10 1.07E+12 2.82E+12 9.33E+07 3.99E+07 1.20E+08 8.32E+08 5.75E+12 2.40E+07 1.02E+07 4.37E+07 4.52E+06 1.70E+12 2.69E+07 1.29E+07 6.92E+07 1.38E+09 1.74E+12 1.17E+09 2.09E+09 1.26E+09 1.48E+12 Group 2 Results Better, but not quite good enough. Group two results; wash with saponifier at 10%, showed much better IC data overall but the WOA levels are still very high and at these levels would pose a mid to high risk of field failures. The SIR data at this level of cleanliness perform better than the first two groups, but still show more failures than not. Group 3-IC Results Saponified wash with Steam Sample Description Foresite Limits SMT NC Acetate Cl- Br- NO3- SO42- WOA Na+ NH4 + K+ <3 <3 <12 <3 <3 <25 <3 <3 <3 Saponifier / Steam Washed - Aquastorm 200 heated to 140F Group 3 Umpire 36 BGA Group 3 Umpire 36 LCC Group 3 Umpire 36 TQFP Group 3 Umpire 36 Ref. area Group 3 Umpire 37 BGA Group 3 Umpire 37 LCC Group 3 Umpire 37 TQFP Group 3 Umpire 37 Ref. area Group 3 Umpire 40 BGA Group 3 Umpire 40 LCC Group 3 Umpire 40 TQFP Group 3 Umpire 40 Ref. area Group 3 Umpire 44 BGA Group 3 Umpire 44 LCC Group 3 Umpire 44 TQFP 0.26 0.35 0.33 0 0.59 0.63 0.59 0.24 0.24 0.22 0.26 0 0 0 0 0 0 0 0 0 3.54 5.63 4.77 0 1.05 1.03 0.87 0.22 0 0 0 0 0 0 0 0 0.45 0.65 0.36 0 0.63 0.38 0.49 0.33 0.13 0.27 0.16 0.08 0 0 0 0 0 0 0 0 2.43 4.27 3.29 0 0.97 0.69 0.55 0.07 0 0 0 0 0 0 0 0 0.51 0.32 0.22 0 0.21 0.29 0.25 0.69 0.68 0.58 0.27 0.40 0.36 0.45 0.22 0.18 0.21 0.08 0.24 0.15 0.24 0 0 0 0 0 0 0 0 0 0 0 0 0 0 2.77 3.88 3.54 0 2.05 3.14 3.33 1.05 0.67 0.39 0.05 0.94 0.85 0.62 0 0 0 0 0 0 0 0 0 0 0 0 0 0 Group 3-SIR Results Saponified wash with Steam Board # Pattern Umpire 38 BGA Umpire 38 LCC Umpire 38 TQFP Umpire 38 Head2 Umpire 39 BGA Umpire 39 LCC Umpire 39 TQFP Umpire 39 Head2 Umpire 41 BGA Umpire 41 LCC Umpire 41 TQFP Umpire 41 Head2 Umpire 45 BGA Umpire 45 LCC Umpire 45 TQFP Umpire 45 Head2 Initial 24 hour 96 hour 168 hour Final 2.09E+12 8.68E+08 2.39E+09 8.45E+09 1.91E+12 5.75E+11 4.07E+09 2.13E+09 2.04E+09 5.50E+12 1.95E+12 2.63E+09 1.70E+09 1.02E+10 1.78E+12 2.00E+12 4.72E+09 3.02E+09 4.17E+09 1.95E+12 2.04E+12 9.20E+08 8.51E+09 2.45E+10 1.70E+12 4.68E+11 8.13E+08 1.15E+09 5.37E+09 3.72E+11 1.91E+12 9.33E+08 2.04E+09 9.33E+09 1.58E+12 1.66E+12 1.38E+09 5.13E+09 2.57E+09 1.48E+12 2.29E+12 3.72E+09 5.89E+09 2.14E+10 1.86E+12 5.62E+11 9.33E+09 1.48E+09 5.75E+10 5.13E+11 1.82E+12 1.29E+09 2.19E+09 1.32E+10 1.41E+12 1.91E+12 9.55E+09 2.19E+10 1.20E+10 2.04E+12 1.91E+12 4.90E+09 3.89E+09 9.00E+09 2.57E+12 6.03E+11 5.25E+08 1.41E+09 9.62E+09 5.01E+11 1.66E+12 1.00E+09 1.74E+09 1.19E+10 6.31E+11 1.74E+12 1.66E+09 2.63E+09 3.72E+09 1.78E+12 Group 3 Results Good! The test results for group 3 show acceptable results on both the ion chromatography and SIR test which indicates good field performance. The steam energy combined with the saponifier on the PCB between the wash and rinse cycles of the in-line process are effective at removing all of the uncomplexed no-clean flux residues. Conclusions Sometimes more is indeed better. With more cleaning energy applied with steam pushing the saponified wash underneath the low standoff components the results are clear according to ion chromatography and SIR testing, the more energy you throw at it the cleaner and more reliable the product becomes. Conclusions cont. The parameters in the study are not intended to be implemented into normal production of PCB’s but for rescue and remedial cleaning of contaminated assemblies. Rescue cleaning is becoming a very important option for hardware found to have cleanliness issues long after the boards are built. It is of most importance to remember not to build a recipe according to flux manufacturer spec sheets but to the product being built. Secondary Study Flux residues are introduced to PCB’s in a number of ways. Hand solder Selective solder Touch up Repair and Rework Real World Problems A customer came to Foresite with a problem with boards failing at ICT and even more after environmental testing. Most of the process was WS flux and the PCB’s are washed after wave with a few components being hand soldered after wash due to water intolerant issues. Real World Problems After looking at the entire process all of the thermal profiles were well within acceptability limits on the reflow and wave solder equipment. A large water intolerant thru-hole transformer was being hand soldered after wash. Line operator was using a bottle of liquid flux to achieve better solder joints faster without regard to the effect of non-complexed no-clean flux has on neighboring components. Real World Problems Transformer has large thermal dissipation properties and required massive amount of heat to fully complex the NC flux, and make an acceptable solder joint. Liquid flux was spreading to resistor network adjacent to transformer without being fully complexed and causing the failures. Real World Problems Customer did not want to use localized cleaning due to the issues with water intolerant components. Also did not want to use pen type de-fluxer because of the flux being under resistors. Solution? Real World Solution Send the PCB’s through another thermal excursion to fully complex the flux using a reflow oven. Lose the bottle of liquid flux! Further education for line operators to convey how every action impacts the quality of the boards. IC Results The PCB’s were tested with ion chromatography to ensure that secondary thermal excursion was effective at complexing the flux Ionic Species Bare Panel After SMT After Wave After in line wash Top side of hand solder After secondary thermal Cl0.78 8.78 370.23 1.14 7.90 1.60 - NO2 0.10 7.36 0 0.10 0.09 0.07 Br0.05 2.28 0.28 0.07 0.56 0.08 - NO3 0.20 2.27 0.28 0.22 0.43 0.16 2- PO4 0.48 0 0.02 0 0.29 0.07 2- SO4 2.93 4.86 1.42 2.20 12.80 2.51 WOA 0 0 5.37 0.37 159.53 0.23 IC Results Looking at the IC results from a localized extraction area over the resistor network before and after thermal excursion the levels of ionics is reduced to an acceptable level. Final Conclusions Flux is good Active flux after the build process is bad Thermal mass plays an important role in soldering that no flux spec sheet can adjust for. Flux can come from many sources Selective wave Palletized wave Secondary hand solder, repair/rework Localized cleaning Bottles of liquid flux are among the worst offenders. Questions? Special thanks to Terry Munson, Meaghan Munson, Josh Fording, Cameron Solis for support on this study. Eric Camden Foresite, Inc Kokomo, IN ericc@residues.com