View metadata, citation and similar papers at core.ac.uk brought to you by CORE provided by Lehigh University: Lehigh Preserve Lehigh University Lehigh Preserve Fritz Laboratory Reports Civil and Environmental Engineering 1964 High strength bolting in the U.S.A., August 1964, Reprint 275 J.W. Fisher L. S. Beedle Follow this and additional works at: http://preserve.lehigh.edu/engr-civil-environmental-fritz-labreports Recommended Citation Fisher, J.W. and Beedle, L. S., "High strength bolting in the U.S.A., August 1964, Reprint 275" (1964). Fritz Laboratory Reports. Paper 163. http://preserve.lehigh.edu/engr-civil-environmental-fritz-lab-reports/163 This Technical Report is brought to you for free and open access by the Civil and Environmental Engineering at Lehigh Preserve. It has been accepted for inclusion in Fritz Laboratory Reports by an authorized administrator of Lehigh Preserve. For more information, please contact preserve@lehigh.edu. Large Bolted Connections by "John W. Fisher Lynn S. Beedle CONTRIBUTION TO THEME lIb: HIGH STRENGTH BOLTING IN THEUoSoA o by John Wo Fisher, Research Assistant Professor of Civil Engineering,Lehigh' University Bethlehem, Pennsylvania, and Lynn S.Beedle, Research Professor of Civil Engineering, Lehigh University, Bethlehem, Pennsylvania DESIGN CONCEPTS IN THE U9 SQA Q The original application of ~.SoAo ~igh-strength was based upon friction-type joints only. A325 bolts in the The first specifica- tion in 1951 merely permitted the substitution of a like number of bolts for hot-driven rivets(l)o It is well known that friction-type joints are dependent on proper bolt tension and an adequate coefficient of frictlono In the UoSoA o the faying surfaces are usually only clean mill scale, and numerous tests of A7 stee 1 Joints have indicated that a slip coeffi.cient of 0035 is representative of values encountered in actual construction. Because of higher labor costs in the UoS.Ao it 18 considered uneconomical to increase tpa slip coefficient by treating the faytngsurfacese Generally it is less expensive to use a larger joint with more bolts. the recent introduction of the higher strength AA90 bolt(2) will allow the use of smaller joints because of higher clamping force per bolt; thus it can be expected that there will be even less of a tendency to make use of special faying surface treatments. 288.22 -2- The concept of a bearina-type conneetionw81flrstlntroduced when the specification was revised in 19.54. At that time,the omission of palntwas required ·to apply only to Ja,tnts subJected· to stress rever . . • .:." > sal or vlbration,or where joint . sllppalewou,1c1 beuncleslrable 0 Tests conducted at the University of Washingtonh.d sbQwn, thatpaintlna the faylngsurfaees8ubstanti.ally, reclucedt,he slipcoefflctent o •••• ". • • • ••••• ' ••••••• '• • • • •" ••••••• ' • • ," •••• '• • • • • • • • • • • • • • • • • • • • • • • • (3) .' . I t "8S recognlz.d tbat many jolnts were'e r ecce:<I,ln bea'tioa 'ndthat slipP',ge was not a'problettto into beart'hg Movement althe conn.ecteclpart,. brlnI1ns··the bolts a8~in8ttheslcle8ofthebol.8~a. t'othestren:gth or sbape of tne8truetUr'e6 '1naowaydetrtmental Allo,thecc>,.t ofle.vins I,ft the 1960 revision of the a,eclflb.fiIt 1011 of the Research Counci.l onliveted and Bolte'd Structural Joiri.ts selear 4tstinetiotl this time the greater sbear. streoICh·..,of· .the blllliliJl,tlie,qtb ·b,(),lt··.w8s not recognized. planes. In 1960, the stresses u.e4: to proportlonbeari.ng-type- Thus) the allowable stresses u",d in ,ft.lctton-typeJof.nts reflect the abl1ityof' the jolnttore'18tllil.pwhet."lJtbilvalues for the bearing-type joint reflecttb.,.h••riqltrllft8':tb of the bolt. type joints correspo<nd to a factor. of safety alainst Ilip of, 104·0 under grayity and live 108480 It is recQgnlzed that the bolts are not actually stressed in shear nor 18 bear,inS a eQn8ideratlonin frlc- tion-type connection8 o However, "It is conventeotto specify an allow- able "shear'stres. 1n ordertbatproportionlns of friction-type co;nnectiona may be carried, out usinlth.s&mewell-eeta..,lllbed methods as areuBed In the del:lsn of rlvetedjolnt8q A'llo".b1e stresse. for tiearlftl-type con••etloR8 are b•••clon the ultimate.h••r ",Ct:enltb of thef•• tlllClr.Jla.eo.:lvetelt.ofllJ:lt A7 and .l\440.lt881 JalAli have .hown that'tbe faetor,of •• fety ".ri•• from about 303 for'hort connection. eleva to 202 for Joints up to .50 inches long (4)(.5 >. In bearins-typedointe ,even thougb the bolt. are tightened so'thatfrlctlonmay ,earl", tbe WOrking load. frict10nal resistance 1s not requlredandthe deslgnls 'properly based on th. shearing strenathofthe bolts. 1 'P'lltlIYe. T.'~.'.()f. JO~Qt, 'Co~n.<;~.4bYA3~5Io1t •..·wltbOQt.W... btra 0 Durinl the'pastfew year•• number of fatlgue·te8ts on bolted lap spU.ees we.re. conducted at tbe. Unive.rl1ty of tlHnots (6). Theee tests tl'lcludedspecirnensde818ned for extreme conditions: overliled holes"no washers. and inmostc8ses, minimum clampini employed. When the turn~of-nutmetbodwa8 used w~s to preload the bolt' none bf,the specimens faUe.duntil at least 2.4 x 1Q6 ..._ •• we..e applied at a 0-30 kai stress cycle o This was true even tboulh .nuDtber 0·£ the specimens slipped into bearing during the flr8t cycle of loading. -4- One specimen with no washers and oversized holes (1/8-ino instead of 1/16-in.)s11pped into bearlol during the first cycle of loading and ran 3 x 10 6 cycles at 0 to 30 kll without failure. Rel.xation teats tooetarmine 101. of clamping force tilth time were also conducted by the University of:nll11noll on blab-tler.oatb bolts (6) There wa. no differen.e·e 1n bolt load for boltIiJ with 1/16-1n. 0 overslzeholes. whether ·or not a wa.herwa. URoer' tb.e·bolt he.do when no washers were u8ed. during the first d·.yo Tbe Molt olthi'• •utlll loslaenerally occurred. :Measurement on boltl Cllntened by the turn-of.. nut method in test joints agreed with the.e special relaxation tesu(5). Even after 10 months, elongation measurements indicated no signif:Lcant addit"ional relaxatton other than whatoe,eurred l1X1tled.1ately .ftertbe initial tightening o As a· result of thesestudies,washerB are no lonler required under the turned element when A325 bolt•••re installed by the turn-of- nut method. They are used under ·the turned a lame n.t to minimize iriteau- larities in the torque-tension relationship When bolts are tightened by the calibrated wrench method o The use of washers' in the U.S.Aopra.ct:Lce 1s specified in order to provide a non-galling surface under thepat:tturned in ti.abteft~ ing as tests have shown they only play a minor role in distributing pressure due to bolt tensiono ,-5- 288.22 3. Static Testa of A7 .oct ~44Q$tt'.1 JQlrtt' Numerous tests of connections of structural carbon steel connected by high-strength bolts have indicated that for clean mill scale a slip coefficient of 0.35 is repre.-entative (3) (4) (5) (7) • Neither length norwldth was found to appreciably affect the slip resiStance (5). Reference 8 reported similar reau1ts. Tests at Lehigh University on A440 hi-p-strength steel connec- ted by 1\325 high-strength bolt. showed a slllht deere.le in the mean slip coefficient (10). More recently. tests of A440 neel connecU.ona connected with the biaher-strength A49'O bolt have given a 811pcoefflThe te,.ta are too cient sl18ht1y h·igher than that reported in Itef. 100 few to give conclusive results; however, the indication 1s that th~ higher clamping force of the A490bolt .y. improve the slip coef,ficient 0 A few constructional alloy steel joints connected by A325 orA490 bolts were also tested at Lehigh and have yielded similar resultso Recently. theoretical solution w.Re developed for the unequal distribution of load among the bolts in double-lap tension spl:lceswhlch have non-linear behavior(ll). Analytical studies supported by tests have shown that an increase in net plate area increases the .'verale shear strength of the fasteners in the lon,aer jo:lnts :- summarizes the analytical and experlmentalfindings 40 Joint ~ovement~:l.n 0 Figure 1 0 II Railroad Bridge During the BUDmer of 19598n inveitigation was undertaken in conjunction with the through-truss bridge for the Michigan Central Railroad near Chicago, Il11nois. A cooperative investigation by the 288.22 -6- Association of American Railroads Research Laboratory and the University of Ililnois was initiated at the time of fabricatlon o Initial readings were taken in the fabrication yard durlngfinal assembly and reaminlo Additional readings were taken after erectioft and at periodic intervals thereafter. The readinll were taken at all joints of'one trus80 The bolts were installed by the turn-af-nut method. \ Reference 12 presents the results of the measurements which were conducted over a J-,!-year ,eriod o In aeneral. this study has shown that little 1f any chanse has occurred in the structure Duringerec- 0 tion, movements up to 1/16-1n. were noted '1n randomdirectioRs. Joint movements measured over 3 years ofd:ervice averased only Oo002-ino and were so small that experimental techniques could have caused the varia... t1on o No significant change in camber has oecurred o The erection movements were random in direction and magnitude and did not always coincide with the direction of dead load Stre.ss:lng (12) 0 5. Tests of Bolted Steel Moment Connections Three identical beam spli.ces with lap connections .were tested in a project at Corne 11 Uni versity (13) • The bolts were designed on the 'basis of 22 kai shear stress as permitted In.bearing-type connections o None of the connections slipped belOW the working loadP w the connections developed the full plastic ~ment and all of of the gross section and showed satisfactory deformation characteristics. A similar test at Cambridge University with the bolts desianed for 30 ksi shear stress also developed the full plastic moment(14). -7- 288 22 0 INSTALLATION QF HIGH-STRENGTH BOLTS Early Uo So specifications stated the well-known formula relating torque to bolt tension and listed a table of torque-tension values(l). However, a number of later studies indicated that such re- lationships are unreliable because of theare4t variability of thread condition, surface conditions under tbe Rut, lubrication an" other factors that use up tbe torque enera, without :Ln4uclnltens1.on in the bolto Studies at NOJ:thwesteJ:n UniveJ:sUy in 1946(1.5) and at the . . .. . (16) . University of M1sIourlln 1955 . . have s:hotfllth.t thest4nd.r:d devia- tion of torque was about 15'10 Bolt tension baaed' on applied torque could vary as much 8£1 ±30% from the averase of ,8sroup as shown in Fig. 2 ( 16) by Me 81 rs 0 0 of8i~lar bolts This i8 cofts14eJ:ably above the .s'l. mentioned Tomonaga and Ta j ima (8). The 1.5'1. va lue :is can.idered to be realistic for installation conditions in. the UoSo The torque re18>tion- ship becomes especially erratic when bolts are tiahtened into the 10elastic range and the threads begin to def~rmo In addition, installa- tion costs are hlgh for the torque wrench method of installation and with the large diameter A325 boltsanel the new A490 bolt considerable torque is required to pr,eload the bolt 0 Two methods of controlling bolt tension are recommended by the Research Council - the calibrated wrench and the turn-af-nut method o The calibrated wrench method is essentially a torque control and success depends on using a hardened washer under the nut in order to limit the variation of friction between the underside of the nut and the gripped 288.22 material o -8- The wrench 1s usually calibrated in 8 hydraulic calibrator as shown 1n F1go 3. A number of factors led to the turn-of-nut methodo As noted earlier, tests have indicated that 'bolts suffer no injury when tightened into their inelastic region o Secondly, bolta actually were being tightened far above their proof load due to faulty torque wrench inspection without any noticeable ill effect. The tUl'n-of-nut method utilizes a strain control 8<nd there- fore 18 ideally suited to controlling tightenina in the inelastic ranl80 The procedures currently in use have shown that a uniform tension 1s achieved because relatively large variations 1n bolt elongations cause only minor variations in tenslon aince the load-elonaatlon curve is reasonably flat(17). Numerous tests Includina those summarized by Dr o Thurlimann 1n the Final Report of 6th Congress (18) have shown that the inelastically loaded bolts have performed wallo In fact, har4ened washers were once required under both the head and nut of A325 bolts ,in order to provide a consistent torque relation, to prevent galling of the structural material and to prevent bolt,relaxation o Tests have now shown that the washer is not needed for the last two reasons and since the turn-ofnut is a strain control rather than a torque control, no washers at all are required when this method of tightening 1s used for A325 bo1ts(2) 0 -9- SUMMARY Current design concepts in the UoS. are discus.ed o Two types of connections are used: friction-type and bearing-typeo The friction- type connection reflects the ability of the Joint to resist sllp whereas the bearing-type connection reflects the ultimate strength of the jolnto Experience with bolted connection 1n the laboratory and in the field is summarized 0 Finally, the factors which have led to currently used in- stallation procedures are discussedo -10- REFERENCES 1. Research Council on Riveted and Bolted Structural Joints of the Engineering Foundation SPECIFICATIONS FOR THE ASSEMBLY OF STRUCTURAL JOINTS USING HIGH-STRENGTH STEEL BOLTS, 1951 2. Research Council on Riveted and Bolted Structural Joints of the Engineering Foundation SPECIFICATIONS FOR STRUCTURAL JOINTS USING ASTM A325 or A490 BOLTS, March 1964 30 Vasarhelyi, Do Do, Beano, So Yo, Madison, R. Bo, Lu, Zo Act and Vasishth, U. Co EFFECTS OF FABRICATION TECHNIQUES, Transactions ASCR, Vol. 126, Part II, 1961, pp. 764-796 4e Foreman, Ro To, and Rumpf, J Lo STATIC TENSION TESTS OF COMPACT BOLTED JOINTS, Transactions, ASeE, Volo 126, Part II, 1961, PPo 228-254 5. Bendigo, Ro A., Hansen, Ro A., and Rumpf, J. Lo LONG BOLTED JOINTS, Journal of the Structural Division, ASCE, Volo 89, Noo 8T6, December 1963 60 Chesson, Eo, Jr. and Munse, Wo H. STUDIES OF THE BEHAVIOR OF HIGH-STRENGTH BOLTS AND BOLTED JOINTS, University of Illinois, Engineering Experiment Station, Bulletin 469, 1964 70 Hechtman, Ro Ao , Young, Do Ro, Chin, Ao Go, and Savikko, Eo Ro SLIP OF JOINTS UNDER STATIC LOADS, Transactions, ASeE, Volo 1'20, 1955, ppo 1335-1352 8. Tomonag8, Ka, and Tajima, Jo THE USE OF HIGH-STRENGTH BOLTED JOINTS IN RAILWAY BRIDGES, Preliminary Publications, 7th Congress lABSE, 1964, PPo 0 379-385 90 Carpentier, L., and Alemany, B. EXPERIENCE FRANCAISE DES BOlLONS A HAUTE RESISTANCE, Preliminary Publications, 7th Congress lABSE, 1964, ppo 397-405 10. Fisher, Jo Wo, Ramseier, P. 00' and Beedle, Lo S. STRENGTH OF A440 STEEL JOINTS FASTENED WITH A325 BOLTS, Publications, IABSE, Volo 23, 1963, pp. 135-158 288 22 -11- 0 lIe Fisher, Jo We' and Rumpf, Jo Lo THE ANALYSIS OF BOLTED BUTT JOINTS, Fritz Engineering Laboratory Report Noo 288.17, Lehigh University, Bethlehem, Pa., 1964 120 Chesson, Eo, Jr. JOINT BEHAVIOR OF A BOLTED RAIUlAY BRIDGE DURING ERECTION AND SERVICE, SRS No o 284, University of Illinois, Urbana, I111nois, 1964 130 Douty, Ro To, and McGuire, W. HIGH-STRENGTH BOLTED CONNECTIONS WITH APPLICATIONS TO PLASTIC DESIGN, Preliminary Publications, 7th Congress, IABSE, 1964, PPo 565-576 140 Johnson, Lo G., Cannon, Jo Co, and Spooner, Lo Ae HIGH TENSILE PRELOADED JOINTS, British Welding Journal, September 1960, po 560 15 Maney, Go Ao 0 WHAT HAPPENS WHEN A BOLT IS TWISTED OFF?, Fasteners, Vol. 3, Noo 4, 1946 160 'auw, A o ) and Howard~ L. Lo TENSION CONTROL FOR HIGH-STRENGTH STRUCTURAL BOLTS, Proceedings, AISC, 1955, pp. 13-21 178 Rumpf, J o Lo, and Fisher, Jo Wo CALIBRATION OF A325 BOLTS, Journal of the Structural Division, ASeE, Vol. 89, Noo 8T6, Decembe'r 1963', pp. 215-234 180 Thurlimann, Bo RESEARCH ON lARGE COMPACT JOINTS WITH HIGH STRENGTH STEEL BOLTS, Final Report 6th Congress IABSE, 1960, ppo 191-201 8~_ i Single Bolt / SfJngle Dolt (II tot) --- ..j'/....... -- - (8U l,ot) -. -- -- -- - -- -- 60t- o Plate Failure Uoundory H t2 ~ ::D tj z ~ I !td-~ ~ Test Points ~ o An/As tI) « ~ V) rAJ ~ ~ « ~ • An/As ::: .. 0.8 1.0 t + An fA 8 • 1.2 2 - I. in. grip 20 .. I in. grip 40 60 80 JOltrr LENGTII, INCIIES Fip;urc 1. SUMl1ARY OF ANALYTICAL AND EXPERlMEID'AL RESUlJTS FOR A325 BOLrrS IN A440 STEEL JOINTS .' . CALIBRAl'ED IMPACT WRE1'1Cll Tnrget Value 198 - 7/S" bolts 15 en 10 ,'0 5 I oL 35 30 I J 40 45 CLAMPING FORCE, KIPS Figure 2. HISTOGRAM OF IKTERNAL BOLT TENSION ......:-:-.>--.i-.--~...... ~..____ _ ___,-----'-.... _._-.. , ---,,,- -'j .i. ,)l);) '~~, ,{O~;;JX , ...... _ ..... ....,.~ - ~ i I...~-- Fig. 3 . ~ - - , - --.-----.-'- --- -. , ~ 'Hydraulic Calibrator for Torq~ed Inst~llat~on ,'_ I