7. LACK OF HAZID (HAZard IDentification) The incidents described in this section indicate the consequences of not having put in place some form of formal hazard identification, HAZID, and risk assessment process. The four cases demonstrate different scenarios: • Compromising a safe design (Titanic) • Invalidating a safe design (P-36), although the location of the tank that ruptured created a hazard in its own right • Not carrying out a formal HAZOP on the original plant design and any modifications (Longford) • Carrying out mass production before fully understanding product behavior in different situations (reactive chemicals) or not passing this information from the research laboratory to designers of the production plant. In all cases, the consequences represented a worst-case situation, although the loss of life could certainly have been higher in some cases. The worst-case concept has been repeatedly challenged over the years in favour of a more risk-based approach. There is no doubt that the concept of ALARP (as low as reasonably practicable) is valid, provided the risk assessments are based on well founded data. The very fact that a ship/platform floats means that it can sink. A process unit operating with materials that can flash to give very low temperatures means that it will be possible to obtain these temperatures under distress conditions. Mitigating measures need to be robust and not vulnerable to a common mode form of failure that renders them all ineffective simultaneously. Consideration of human factors where mitigation is sought through procedural means must be carefully examined to ensure the right levels of checks and balances. Refer to Exxon Valdez incident description. Developing a safe design using tried and tested codes and standards is not as easy as it seems as every experienced design engineer knows. There are always compromises to be made, not least in terms of space available and the interaction with other facilities. These can be overcome using sound engineering judgement applied by competent people, confirmed through proper risk assessment. However, there are other pressures that can arise, not least financial and programme. It is the role of the Project Manager to ensure that commercial and programme pressures do not detract from developing and implementing a safe design. In order to do this the project manager needs to have expert advice to guide him or her through the programme of safety studies and review necessary to achieve a safe design and 149 150 INCIDENTS THAT DEFINE PROCESS SAFETY commissioning. Equally, Project and Business Boards need to have some form of independent assurance process to confirm that the design process has produced a safe plant. Safe operation of a process unit or other facility that has been designed to a safe standard is dependent on the integrity of operation. Operators must understand the characteristics of their plant together with the consequences of invalidating safety critical devices. The most apparent safety critical devices are process trips and pressure relief devices, but in many cases this extends down to operating procedures. Failure to operate equipment in the right sequence can lead to disaster. In many cases, the designer aims to engineer human error out of the equation, but this cannot always be done. In other cases, difficulty with maintaining steady operation where safety critical devices fail due to equipment or process problems can lead to the arbitrary disconnection with disastrous results, as seen at the Grangemouth Hydrocracker. Competent people must thoroughly review any change to any safety critical device through a rigorous management of change process. The fatal accident at BP’s Texas City ISOM unit that occurred on March 23, 2005 demonstrates the dangers of accepting previous hazard identification studies at face value. In this incident 15 people were killed in a trailer park located adjacent to an atmospheric vent of a process unit blowdown stack. The area in which the trailers were located had been identified some years earlier as a safe location for these temporary facilities, installed to service a turnaround on an adjacent unit. This has seemingly ignored the fact that the blowdown drum vent was only 150 ft (45 metres) away. The opportunity to review this situation had occurred immediately before the incident as each trailer location was subject to a Management of Change Review. In today’s facilities, the Process Safety Management programme is becoming the norm. This calls for regular review of process hazards analysis, which includes HAZOP, HAZID, FMEA (failure modes and effects analysis) and any other form of review appropriate to the process or equipment. The reasons for this are twofold, firstly to confirm that proper management of change routines have been applied to changes that have been made since the previous review, typically 3 to 5 years before, and secondly to ensure that lessons learned from incidents within the site or within the industry have been applied. A process safety or plant integrity committee made up of process safety and engineering, operations, maintenance, and inspection specialists, chaired by a senior manager, is an effective way to provide oversight to this process. Finally, appropriate training in hazard recognition and risk assessment is essential at all levels of the organisation, and should be part of everybody’s training plan. 7. LACK OF HAZID (HAZard Identification) 151 SINKING OF THE TITANIC, NORTH ATLANTIC, April 15, 1912 At around 02:20 on Monday, April 15, 1912, the liner “Titanic” sank after hitting an iceberg at 23:40 the same night, with the loss of over 1,500 lives. Titanic was built for the White Star Line, which was in strong competition with Cunard and other shipping companies on the lucrative cross Atlantic routes for upper class and business travel in first and second class accommodation, and emigrants travelling third class. The ship was 50% larger than her nearest competitors, all of which had a reputation for luxury and speed. The design of the ship included 44 watertight compartments giving rise to a perception that the ship was unsinkable and in the event of an accident would be its own lifeboat. However, during her construction two safety critical decisions were taken. The first of these was to stop the vertical watertight bulkheads at “E” deck – two levels below the exterior deck – to allow much greater freedom of movement for passengers and crew. The second was to reduce the number of lifeboats from 64 to 16 to remove what the owners considered to be an unsightly and unnecessary feature, particularly as regulations at that time did not require every person on board to have a seat on a lifeboat. Titanic was launched on May 31, 1911, passing her sea trails on April 2, 1912 after which she immediately set sail for Southampton to prepare for her maiden voyage to New York. In the drive to get away on time and because of a coal strike, the ship sailed with only sufficient coal to reach New York travelling at 22 knots with 10% margin for safety. The ship was in first class condition; the only significant fault was heat damage to the bulkhead between boiler rooms 5 and 6 caused by a fire in a bunker, which had been previously extinguished. Titanic departed Southampton on April 10, at 12:00 noon, travelling to pick up additional passengers at Cherbourg followed by Queenstown, Ireland, before starting her first Atlantic crossing on April 11. 152 INCIDENTS THAT DEFINE PROCESS SAFETY The Titanic was under the command of Captain Edward J. Smith, the most senior of the White Star Line’s captains. Captain Smith had had a chequered career having previously grounded three ships, all without significant injury or damage, had been involved in a collision with a Royal Navy cruiser in 1911 while in charge of “Olympic” (Titanic’s sister ship of a similar size), and a near collision with the liner “New York” as he left Southampton at the start of this voyage. The groundings had all been written off as occupational hazards, while the collision and near collision had been caused by driving his very large ships close to stationary smaller vessels which were in turn drawn into the larger vessel through the effects of Bernoulli’s Principle. He was considered to be over confident in his seamanship and the invincibility of his ship. Nevertheless he was a seaman of considerable experience of the north Atlantic routes particularly in respect of winter ice. The ship sailed on her maiden voyage with J. Bruce Ismay, the managing director of White Star Line on board. Ismay was a forthright person whose main objective was to ensure that Titanic and her sister ships built up and maintained a strong reputation over their competitors, which were for the most part faster. Titanic was scheduled to dock in New York on Wednesday, April 17, but there is evidence to suggest that Ismay intended the ship to arrive on the afternoon of April 16, by driving the ship at over 24 knots for the final 24 hours of the crossing. It is also clear that he was involved in discussing tactics directly with the chief engineer, bypassing the captain’s authority. In reality this meant that a committee of two strong personalities, each with different agendas, was commanding the ship. Warnings that an ice field with icebergs was lying across Titanic’s course began to be received on April 12, and continued at an increasing frequency during April 14. One ship reported damaged bows, and another was stuck in the pack ice only a few miles from where the Titanic eventually struck an iceberg. Radio communication was in its infancy at the time and there is some confusion over whether message protocols were correctly followed. However, it is clear that those commanding the Titanic were aware that they were approaching an ice hazard both from the messages that did get through and from meteorological observations taken on board – the air temperature had dropped to 31°F (-0.5°C) since sunset with virtually no wind and a calm sea. At no time did the captain give an order to slow down although the ship was undoubtedly travelling through floating pack ice at the time. Titanic had two lookouts stationed in the “crows nest” some 95 feet (29 metres) above the water who had come on duty at 22:00 on April 14. A slight haze on the water hampered visibility, and although there was provision to store binoculars in the crow’s nest, none had been provided. Every time they looked forward from behind their protective enclosure the lookouts were exposed to a cold wind created by the 7. LACK OF HAZID (HAZard Identification) 153 ship’s forward motion of 22 knots. They had been briefed to look out for “growlers” — icebergs that were difficult to see as having recently been upended showed smooth, dark surfaces. Lack of sea swell meant that there would be no waves breaking against an iceberg, compounding the visibility problem. The first report from the lookouts that there was a “dark mass” on the horizon directly in the ship’s path came at around 23:33. At that time the ship was traveling at 22 knots on a heading of 266° with the iceberg an estimated 2.9 nautical miles away. However, it was only at 23:40 that an alarm call was made “iceberg directly ahead”. The delay in interpreting “dark mass” to be an iceberg has not been satisfactorily explained, but it could well be the result of there being a lot of floating ice around at the time with hazy conditions on a dark, moonless night. The Captain was having dinner with passengers when the ship struck the iceberg, with First Officer William Murdoch having taken the watch at 22:00. When the alarm call was eventually made, Murdoch gave the order to put the helm hard over to starboard causing the bow to swing to the left. At the same time he gave the order to stop engines. It quickly became clear that while the bow would miss the iceberg, the stern would swing into it causing considerable damage. To counteract this, Murdoch ordered the steering to be put hard over to port as the ship began to pass the ice. Timing of this manoeuvre was critical and unfortunately he started his turn too soon. The bows of the ship hit the iceberg, with the bottom of the starboard (right hand) of the ship running over an undersea shelf of ice. As contact was made, Murdoch ordered the watertight doors between vertical bulkheads to be closed. 154 INCIDENTS THAT DEFINE PROCESS SAFETY The assessment of damage after the ship had come to a stop was confused. The Fourth Officer went below and reported that there was no damage to the forward passenger accommodation. The Ship’s Carpenter reported that the ship was making water with the mailroom rapidly filling. The Captain went below to see for himself with the Titanic’s chief designer who was also on board, whereupon it became clear that the forepeak, three cargo holds and boiler rooms 5 and 6 had sustained damage. Pumping could prevent the water level rising in boiler room 5 but the other compartments were lost. 7. LACK OF HAZID (HAZard Identification) 155 According to the ship’s designer, the ship should have remained afloat for some considerable time with the watertight doors holding and the water level in boiler room 5 kept under control by pumping. The Chief Engineer concurred with this view. Watertight doors aft of boiler room 5 were opened to facilitate the rigging of hoses to keep the water level down. Boiler rooms 1 to 4 could be kept in operation sufficient to maintain light and heat. The ship should, therefore, have fulfilled its ambition to be it’s own lifeboat. However, at 23:52 the order was given to restart the engines. It is thought that this resulted from pressure by Ismay to head for the nearest port of Halifax, Nova Scotia. Messages sent by wireless from Titanic resulted in newspaper articles reporting the accident and that all aboard were on their way to safety. To have the passengers rescued by another ship would have caused great damage to the reputation of Titanic and the White Star Line. Captain Smith’s belief in the invincibility of Titanic was too strong to challenge his managing director before a thorough review of all damage had been completed, which was against the basic principles of good seamanship and common sense. The result was to cause even greater damage to the riveted seams below the waterline, allowing increasing amounts of water to enter the affected compartments. As the ship moved forward at half speed, water entering the damaged compartments caused 156 INCIDENTS THAT DEFINE PROCESS SAFETY the bow to sink further. Eventually, the water rose to above the level of the watertight bulkheads that terminated at the level of E deck. Water then poured over successive bulkheads as each compartment filled and the bow settled further. The weakened bulkhead between boiler rooms 5 and 6 eventually failed. At 00:19 on April 15, the order was given to stop engines for the last time. The ship finally sank two hours later. The shortage of lifeboats made it was inevitable that there would be large-scale loss of life. This may have featured in the mind of the captain who refused to give a general order to abandon ship in order to prevent panic resulting in an even greater loss of life. The first lifeboats away were not full and it was only when about half of them had been launched, that there was any sense of urgency to get off the ship. The Captain, First Officer, Chief Engineer and Chief Designer went down with their ship. Their managing director, J Bruce Ismay, never lived down the shame of throwing himself in the last lifeboat to leave. He died, a recluse, in London in 1937. Although Titanic had launched distress rockets from around 00:35, these were misconstrued or ignored by the nearest ship “Californian”, which was trapped in the ice pack about 10 miles away awaiting daylight before attempting to move on. Another liner, “Carpathia”, had received distress messages by wireless from Titanic and raced 38 miles through the icepack to reach the scene later that morning. By that time, 1503 persons had died. Integrity Management Hazard Evaluation and Management – to meet the requirement to be unsinkable, the integrity of the watertight compartments was paramount. In the original design the bulkheads separating the compartments rose to the level of the weather deck allowing the compartments to be totally enclosed by the shutting of watertight doors and hatches. A design change had been made which terminated the bulkheads two level below the weather deck in order to allow greater freedom of movement below decks. However, it would appear that the consequences of 7. LACK OF HAZID (HAZard Identification) 157 this design change were not assessed. A simple review of the consequences of the ship hitting any object would be that water would enter the bow compartments causing the bow to drop. Simple geometry would show that once the angle of pitch had increase above a critical value, the sequential flooding of compartments was unstoppable making it inevitable that the ship would sink. The only mitigation measure would be to pump out the damaged compartments before the critical angle was reached. But, what if the pumps were of insufficient capacity or failed for whatever reason? Some may say that it is not reasonable to consider double jeopardy. But what if there is some form of common mode and the consequence is the total loss of the unsinkable ship? Major Accident Potential – the worst case scenario for any ship is that it sinks. In the case of the Titanic the ship was considered to be unsinkable, even to the extent that under any foreseeable emergency situation it would remain afloat to be its own lifeboat until help arrived. Sadly, the fallacy of this approach was only finally realised when the Captain failed to give a general order to abandon ship as he realised the inevitability of the situation. Management of Change – the major management of change issue was the lowering of the heights of the bulkheads separating the watertight compartments. Pressure from senior managers to make the ship as passenger friendly as possible had prevailed. Similarly, the reduction in the number of lifeboats was made for cosmetic reasons. Engineering Authorities – in this case this role is clearly that of the ship’s chief designer. He had initiated a design to build an unsinkable ship. However, he unwittingly allowed the customer to get what he wanted even though the integrity of his design had been compromised. Plant Integrity – with the exception of the issues discussed above, the ship had been built to robust engineering standards. There has been some public debate over the lack of ductility at low temperatures of the steel used in the construction of the ship’s hull. While it may not have been to today’s standards, it was the best available and countless other ships have operated safely under extreme cold conditions using the same material. What the Captain clearly did not understand was the inherent property of damaged riveted seams to “unzip” when placed under the type of stresses created when the ship was restarted. The perception of invincibility overcame good practice and common sense with catastrophic results. Competent Personnel and Procedures – the Captain and his crew were certainly experienced seamen, but from the accounts of his previous groundings and near misses, it is clear that the Captain had no understanding of the characteristics of big ships when manoeuvring near to smaller vessels. The Captain had a hidden 158 INCIDENTS THAT DEFINE PROCESS SAFETY personal agenda to retire at the top of his profession, which may well have influenced his behaviour when he should have been challenging his managing director in the face of orders that compromised the safety of the ship. Incident Investigation – there was clearly no culture of near miss reporting to prompt the investigation of events such as groundings, they were considered inevitable. Even in a “no blame” culture the very act of learning lessons can move individuals to consider how they may otherwise have acted and thus influence their behaviour. Emergency Response – the nearest ship to the Titanic was stopped in the ice field awaiting daylight before proceeding. There is evidence to suggest that even though the officers and crew knew the Titanic was in trouble they ignored this and made no response. The ship that was the first to arrive at the scene travelled 38 miles though the ice field in the dark at maximum speed, exposing itself to the very conditions that sank the Titanic. It is easy to condemn the former and praise the latter. In reality the concept of the ship being able to sustain itself while awaiting rescue is clearly flawed as the very conditions which led to its situation will equally affect the rescuer. The emergency response factor that would have made the biggest difference to preserving life aboard the Titanic would have been the provision of lifeboat seats for everybody. Incidents of a Similar Nature Long Bolt Exposed Fittings In 1990 concern was raised during an insurance audit of a facility in the USA over the use of long bolt fittings. There are different from the conventional flanged fittings, as they are sandwiched between pipework flanges, using long bolts. Typical examples are Mission Duo-Chek non-return valves, and wafer type butterfly valves as shown here. These valves provide great savings in terms of cost and weight and in some cases flow characteristics and sealing properties. However, they are vulnerable to leakage in a fire situation or other extreme thermal transient condition (including application of thermal insulation when at operating temperature) due to the length of the bolt sandwiching the valve between piping flanges that is exposed to ambient conditions. One plant, the Gas Oil Hydrodesulphuriser at a French refinery, suffered a number of leakages of this type of fitting since the unit had been commissioned in 1963, culminating in a major fire in January 1995. A process temperature control valve of the wafer type leaked badly immediately after a sudden 7. LACK OF HAZID (HAZard Identification) 159 hailstorm. Two further fires followed in 1996 on similar valves, which precipitated a decision to replace these with conventionally flanged valves. The link with the Titanic accident is in the way in which this type of valve was introduced to hydrocarbon service. Traditionally, flanged valves were used where the bolts are almost totally enclosed by the pipework and valve body flanges. The move to the use of wafer valves was made primarily on cost grounds, although where weight is a critical factor, this too favours the wafer design. What the designers failed to realise was that what was previously a safe design was made vulnerable under extreme conditions. Some references to read more: • The Last Log of the Titanic, David G. Brown, McGraw-Hill, 2001, ISBN 0-07-136447-1 (both sketches) 160 INCIDENTS THAT DEFINE PROCESS SAFETY SINKING OF THE PETROBRAS P-36 SEMI-SUBMERSIBLE PRODUCTION VESSEL, RONCADOR FIELD, BRAZIL, May 15, 2001 The Petrobras oil and gas production semi-submersible P-36 sank in 4,460 feet (1,360 metres) of water on March 15, 2001 with the loss of 11 lives. P-36 was claimed to be the world’s largest semi-submersible deep-water oil production rig valued at $450 millions. It produced 6% of the daily production of the Brazilian state oil company, Petrobras, and was located 150 km from the shore in the Roncador Field. P-36 was a conventional semi-submersible with four columns terminating in two underwater pontoon hulls. The columns and pontoons provide the buoyancy to keep the vessel afloat, and contain tanks that can be ballasted to submerge the vessel to the required depth to maximize stability and minimize movement. Semi-submersibles are used as floating production systems where water depths are too great for the installation of a fixed structure. P 36 had started production in March 2000 with an output of 80,000 bbl/day of oil 3 3 and 1.3 million m /day (36.6 million ft /day) of gas. On the day of the incident there were 175 people on board, of whom 85 were crew. 7. LACK OF HAZID (HAZard Identification) 161 The sequence of events that led to the sinking started on February 10, when the starboard emergency drain tank (EDT) pump was removed for repair. The EDT’s were located in the port and starboard legs of the platform collecting wastewater contaminated with oil, which was pumped to the platform’s oil production header and hence into the processing plant. The EDT’s are designed for atmospheric pressure. The atmospheric vent from the starboard EDT was blanked to prevent water from entering it from an open drain tank as it already contained a considerable amount of contaminated water. The starboard EDT was isolated from the port EDT by closed valves. At 22:21 on March 14, attempts were being made to pump out the port EDT. However, lack of positive isolation resulted in a back flow of production fluids into the starboard EDT. At 00:22 the starboard EDT ruptured due to an internal overpressure of about 10 bar g (150 psig). The physical effects of the rupture were to release water and oil into the supporting leg, and to break an 18 inch (450 mm) diameter sea water line next to it, causing flooding of the leg. This also caused the fire main to depressurise leading to shutdown of the processing plant. Seawater pumps located within the starboard legs were automatically started up when the fire main depressured, adding to the flooding of the legs. However, flooding continued even after the seawater pumps had been shutdown because the sea chest valves connected to the ocean failed in their set position, i.e. they did not fail open or closed. A release of flammable vapour spread upwards through the column as ventilation dampers and watertight doors between levels in the leg had been opened in preparation for an inspection of repair work to cracks found in the stability box scheduled for the following day. Gas detectors were activated on the deck. The vapour ignited 17 minutes after the tank rupture with the resultant 162 INCIDENTS THAT DEFINE PROCESS SAFETY explosion killing 11 members of the emergency response team who had been sent to open the hatch between the third and fourth level within the leg. The situation was made more serious because the open ventilation dampers and watertight doors/manhole allowed water to fill all the compartments including the ballast tank, pump room and stability box. Exhaust and blower system dampers, although not designed to be watertight, should have closed but their actuators failed. The platform progressively listed as the spaces in the leg filled. Water was deliberately admitted into the diametrically opposite pontoon to contain the list, but the platform continued to sink. Evacuation of non-essential personnel commenced about 80 minutes after the explosion, with final abandonment at 06:03 the same morning. By 08:15 the platform had listed by 16°, sufficient for water to enter the chain lockers and submerge compartment vents. After that point in time it was inevitable that the platform would sink. Attempts were made to stabilise the sinking platform by the injection of nitrogen and compressed air into flooded compartments, but the progressive submersion continued until the unit finally sank at 11:30 on March 20, 5 days later. 7. LACK OF HAZID (HAZard Identification) 163 3 At the time of the accident the platform contained about 1,200 m of diesel 3 fuel, and 350 m of crude oil in on-board storage and processing plant. In the first 3 24 hours after the sinking about 350 m of oil came to the surface, which was partly recovered with the balance dispersed using chemicals. Integrity Management Hazard Evaluation and Management – the process diagram shows that even a very simple HAZOP would have identified the potential for backflow of production fluids into the EDT from the production header. It is not known whether the atmospheric vent was designed to protect the tank should this occur, it certainly should have been. Even so, this was a safety critical device certainly designed for the external fire case (which could have happened at any time), and should only be blanked off after the EDT was totally emptied of hydrocarbon with all other connections blinded. Major Accident Potential – the wisdom of locating a wastewater collection tank inside a major supporting member. The very nature of the tank makes it highly likely that a flammable atmosphere would exist within it at least some of the time, which if ignited by whatever means would have compromised the safety of the platform. Engineering Authority – isolation of equipment is one of the technical standards on which the safe operation of any process facility depends. Engineering Authorities have the responsibility to ensure compliance as well as the technical excellence of the standard itself. The location inside the platform support legs of equipment and tanks directly connected to the process was allowed by classification societies under certain circumstances. However, it must be recognised that engineering standards and rules focus on individual systems and may not consider interfaces in any depth. An Engineering Authority approach during design should have identified this as a critical interface issue and sought a resolution based on rigorous risk assessment. Protective Systems – ventilation dampers and watertight doors were safety critical items that had been opened in preparation of an inspection the following day, contrary to procedures. A similar situation arose on Piper Alpha when the fire pumps were isolated to allow divers to inspect the underwater structure but not put back onto “remote” when the inspection need was no longer there. Supervisors and operators need to identify all of the safety critical items on their plants, together with the consequences of bypassing them or rendering them inoperable. Another protective system that compounded the problems faced on that day was that the sea chest valves, used to route water into and out of the ballast tanks, “failed set” as they were designed to do. Clearly, in other situations major problems 164 INCIDENTS THAT DEFINE PROCESS SAFETY could have arisen if the sea chest valves had been designed to fail either open or shut. In this case the situation was outside of the design assumptions supporting the decision to install “fail set” valves for this duty. The implication in this is that when carrying out the hazard studies to identify the correct mode of failure for critical equipment, it is necessary to think “outside the box” to identify if there are any other situations which need to be protected against. Competent Personnel and Procedures – there were three areas of competence raised in the investigation report. • The crew who isolated the starboard EDT by valves only and blanked the vent. Anybody with rudimentary HAZOP training should have been able to identify the hazard they were creating. • The persons who authorised the opening of the ventilation dampers and watertight doors when there was no immediate need, breaking the platform rules. • Criticism was voiced at the conduct of the Bargemaster who allowed the diametrically opposite ballast tanks to fill in an attempt to reduce the listing, possibly hastening the inevitable. Emergency Response – the people who died were the emergency response team. Everyone else was rescued. The message is that emergency response teams are the most vulnerable people in an incident. Their actions may put themselves at particular risk. There should be an assessment of all credible incidents which may occur on any site and this should include a risk assessment of the activities requested from the emergency response teams in the emergency response plans. In the event of an incident, the ER teams should update that risk assessment taking into account the specific circumstances of the incident and must be competent to do so. If no prior risk assessment has been carried out, they should stop and think clearly about the hazards and the risks to themselves. Above all, it should make it clear that people are not expected to put their lives at risk to protect plant and production. They may put themselves at risk to save the lives of others but only if there is a realistic prospect of saving those lives. Performance Management of Integrity Management and Learning – one of the key recommendations from this incident is to implement an operational Excellence Programme in this type of facility. The Brazilian National Petroleum Agency Inquiry recommended that a standard should be applied in future projects that tanks or equipment connected to the process should not be located within support legs or pontoons. 7. LACK OF HAZID (HAZard Identification) 165 Incidents of a Similar Nature Rupture of Liquid Nitrogen Tank, Japan, August 28, 1992 On August 28, 1992, there was a failure of a storage vessel containing liquefied nitrogen at a manufacturing facility. The catastrophic failure of the vessel resulted in the collapse of almost half of the factory, damage to the walls of 25 houses and to some 39 different vehicles, all within a 400–metre (1300 ft) radius. Fragments of the vessel were projected up to 350 metres (1150 ft), including part of the top head of the outer shell, which was 1.5 metres wide and 8 mm thick. The estimated property loss was 440 million yen (about $4.9 million or £3 million). The vessel was filled on June 26, 1992, and was used for the following 2 days. It 3 3 was filled again on July 2 with 2,000 m to give total contents of 2,800 m 3 (99,000 ft ) — volume measured at standard state conditions. The vessel was not used for the next 61 days up to the time of the rupture. The inner vessel broke into seven fragments, with the fractures showing an appearance typical of ductile fracture, indicating that the failure was due to excessive pressure. The outer vessel of carbon steel broke into 11 main fragments plus many other smaller pieces that were not recovered. Parts of the fracture surface showed low temperature brittle fracture; but the majority showed a ductile fracture that, again, indicated a failure due to excessive pressure. The piping and valves connected to the inner and outer vessels were projected away and had damage which was mainly ductile rupture, deformations, or dents. By inspection and use of X–rays it was found that most valves were shut, including the top liquid inlet valve M2, the delivery valve M4, the isolation valve for the relief valve M5 and the bursting disc isolation valve M6. The vessel was, therefore, under completely closed conditions at the time of the incident. An inspection of the rupture disc showed that it had ruptured outwards despite the closed inlet valve. Performance tests on a relief valve and a bursting disc of the same type as involved in the incident showed that the actuation pressures were 10.4 bar g (150 psig) and 18.2 bar g (265 psig), respectively. These confirmed the setting pressures and also showed that, if they had actuated, they would have been noticed. A test on an isolation valve of the type used for the bursting disc showed that it would satisfactorily isolate the disc without leakage up to a pressure of 98.1 bar g (1,422 psig). 166 INCIDENTS THAT DEFINE PROCESS SAFETY The investigation committee concluded that the inflow of heat under static conditions was sufficient to build pressure inside the inner vessel sufficient for it to rupture as the over pressure protection devices were isolated. The recommended daily checking of the vessel pressure at the beginning and end of the day was largely neglected and no safety instructions were given to employees, underlining a general lack of basic knowledge of the facility. The company also did not maintain any manuals describing the safe operation of the nitrogen storage vessel. Some references to read more: • • • • P 36 Accident analysis, ANC/DPC Inquiry Commission Report, Agência Nacional do Petróleo/ Diretoria de Portos e Costas, July 2001. (Brazilian National Petroleum Agency and Directorate of Port and Coasts joint report). BP Safety communication “Lessons Learned from the Petrobras P-36 Sinking”, August 2001 Considerations with respect to DNV classification rules and systematics By: Svein Flogeland, DNV Head of section, classed units in operation, Presentation at NPD / Petrobras seminar, Stavanger 2002-04-30 Ruptured Nitrogen Tank – “Loss Prevention Bulletin, Issue 123”, UK Institution of Chemical Engineers, 1995. 7. LACK OF HAZID (HAZard Identification) 167 ESSO LONGFORD GAS PLANT EXPLOSION Australia, September 25, 1998 A major explosion and fire occurred at Esso’s Longford gas processing site in Victoria, Australia. Two employees were killed and eight others injured. The incident caused the destruction of Plant 1 and shutdown of Plants 2 and 3 at the site. Gas supplies were reduced to 5% of normal, resulting in 250,000 workers being sent home across the State as factories and businesses were forced to shutdown. Product gas to sales Arial photo Esso plant, Photo courtesy of ABC Network Lean oil inlet The site receives crude oil and gas from production platforms in the Bass Strait and converts it into raw LPG, stabilized crude oil SIMPLIFIED SCHEMATIC OF ABSORBER and sales gas (mainly ethane and methane). The plant produces 6 million litres of LPG, 30 million litres of stabilized crude oil and 15 3 Rich oil to flash drum million m of sales gas per day. Plant No. 1 is a lean oil absorption plant, which separates methane from LPG by stripping the incoming Gas + liquid gas with a hydrocarbon stream called “lean Liquid hydrocarbon condensate oil”. Methane rises to the top of the towers, with heavier hydrocarbons dissolving in the descending lean oil. The oldest of the three plants, No.1 was commissioned in 1969. Plants 2 and 3 are cryogenic plants. They cool incoming gas until its LPG component liquefies and the methane floats to the top. The fire, which broke out following an explosion at 12:30 p.m. on September 25, burned for over two days before being declared extinguished on September 27. Gas plant 1 was “severely damaged” by the fire, as was common piping and other systems shared with plants 2 and 3. At shortly before 12:30 p.m. a plant supervisor 168 INCIDENTS THAT DEFINE PROCESS SAFETY was checking on a hydrocarbon release that had been leaking for about 4 hours when a huge blast sent a gas and oil cloud over the area, drenching workers in liquid hydrocarbon. The cloud ignited 60–90 seconds later resulting in a massive explosion and flashing back to envelope GP 905 reboiler heat exchanger. The gas feed from the offshore platforms into the plant was cut. The plant supervisor was killed in the explosion, as was a maintenance supervisor. A major part of the process in Gas Plant No: 1 was a pair of Absorbers operating in parallel. A mixture of gas and liquid hydrocarbons entered the Absorbers, which both had a gas/liquid disengaging region at the base with an absorption section above where gas was contacted with a stripping oil to remove heavier hydrocarbons. During the previous night shift, the hydrocarbon condensate level had started to increase in the knock out section in the bottom of Absorber B. As the normal disposal of condensate to Gas Plant No: 2 was not available, the alternative condensate disposal route was to a Condensate Flash Tank. Under this set of circumstances, it was normal to increase the temperature at the base of the Absorber, but this had not been done. The inlet to the Condensate Flash Tank was protected against excessively low temperatures by an override on the Absorber level controllers. The consequence, therefore, was that the disposal rate of condensate from the Absorber became less than that in the inlet flow, resulting in a build up of liquid condensate in the Absorber base. 7. LACK OF HAZID (HAZard Identification) 169 The condensate level rose in the Absorber to a point where it mixed with the exiting rich stripping oil stream. Condensate mixed with rich oil passes flashed over the rich oil level control valve resulting in a much reduced temperature in the downstream Rich Oil Flash Tank. This caused temperatures to drop across the plant as rich oil flowed through the recovery process where hydrocarbons where stripped from the rich oil before returning it to the Absorbers as lean oil. Eventually, the lean oil pumps tripped out, causing major thermal excursions on a plant with a high degree of process and thermal integration. Loss of lean oil was a critical event, but was not communicated to the supervisor until he returned from the morning production meeting 1_ hours after the pumps had tripped. Temperatures in parts of the plant fell to -48°C. At 08:30 a.m., a condensate leak occurred on heat exchanger GP922. The absence of lean oil flow meant that the condensate flowing through the rich oil system was not warmed as it entered the recovery section. The reason for the leak was probably due an extreme thermal gradient created while attempts were being made to re-establish the process. Other parts of the process showed signs of extreme cold with ice forming on uninsulated parts of heat exchangers and pipework. At 10:50 the leak from GP922 was getting worse, and the Supervisor decided to shutdown Gas Plant No: 1. By 12:15, two maintenance technicians had 170 INCIDENTS THAT DEFINE PROCESS SAFETY completed retightening of the bolts on GP922 without making any appreciable difference to the leak. It was decided that the only way to stop the leak was to slowly warm GP922 by starting a flow of warm lean oil through it. However initial attempts to restart the lean oil pumps were unsuccessful. Ten minutes later after operating a hand switch to minimise flow through another heat exchanger, GP905, that heat exchanger ruptured, releasing a cloud of gas and oil. It is estimated that the cloud traveled 170 metres before reaching fired heaters where ignition occurred. After flashing back to the point of release flames impinged on piping, which started to fail within minutes. A large fireball was created when a major pressure vessel failed one hour after the fire had started. It took 2 days to isolate all hydrocarbon streams and finally extinguish the fire. The investigation concluded that the immediate cause of the incident was loss of lean oil flow leading to a major reduction in temperature of GP905, resulting in embrittlement of the steel shell, which was followed by introduction of hot lean oil in an attempt to stop the hydrocarbon leak in GP922. Throughout the whole sequence of events, operators and supervisors had not understood the consequences of their actions to re-establish the plant. A Royal Commission was set up to investigate the accident. This concluded that Esso’s complex health and safety management system, Operation Integrity Management System (OIMS), was difficult to understand and had become divorced from the reality of operations in the field. Esso were subsequently fined US$1 million for breach of occupational health and safety regulations. Although the courts ruled against compensation for economic loss suffered by customers, claims were allowed for those suffering property damage as a result of the incident. Integrity Management Hazard Evaluation and Management – a HAZOP study for this plant had never been carried out prior to the accident. A HAZOP for Plant No: 1 had been planned for 1995 but was never carried out despite being allowed for in Esso’s budget for that year. One reason given for this was that it would have picked up too many small items, but why this was perceived to be a problem was never explained. If properly conducted, a HAZOP would have clearly identified the 7. LACK OF HAZID (HAZard Identification) 171 consequences of loss of lean oil to create dangerously low temperatures in the process equipment. Major Accident Potential – the Safety Case methodology adopted in Europe after accidents at Flixborough and Seveso were applied by Esso to its offshore facilities, which was a legal requirement. However, there was no legal obligation to apply this approach to its onshore facilities. Legal requirements invariably represent the lowest common denominator and even if there had been no legal requirement to apply the methodology, it would have been prudent to do so in what is clearly a high hazard plant with major consequences and liabilities in the event of failure. Management of Change – over the previous two years there had been a relocation of experienced engineers away from the plant at Longford to the company’s head office in Melbourne. Supervisors and operators were given greater responsibility for day-to-day operations, including troubleshooting. There was also a reduction in the number of plant supervisors and operators. As a result, there were no experienced plant operators at the site at the time of this incident. A second management of change issue was identified. Modifications to the condensate transfer system over previous years had recognised the potential to carryover from the absorbers into the rich oil stream, but the impact on downstream vessels was never subjected to any form of risk assessment. Engineering Authorities – the plant was commissioned in 1969 but nobody had seen the potential for this accident to happen, despite a number of experienced engineers having been associated with the plant since that time. Engineering Authorities have an essential role in defining safe operating envelopes together with operations management, and need to ensure that their discipline engineers allocated to individual process units are making the appropriate input. On the day of the accident the one person who would have identified the hazard of operating at extremely low temperatures would have been an experienced engineer. However, all the technical staff had been moved offsite. Part of the role of an Engineering Authority should be to ensure that adequate resources at all levels are available to maintain integrity of operations. Specialist engineers allocated to the Engineering Authority are sometimes called “Technical Authorities”. Plant Integrity – plant handling light hydrocarbon condensates and high pressure gasses is vulnerable to extremely low temperatures in the event of an upset. Steel used in the fabrication of the process equipment must be specially made if it is to be able to retain its strength at much below 0°C. This is a safety critical aspect of plant operation that all supervisors and operators need to know. In this 172 INCIDENTS THAT DEFINE PROCESS SAFETY event, the only safe course of action would have been to shutdown the plant and allow the process equipment to warm up naturally. Criticism was also made in the Royal Commission report of the lack of regular monitoring of process operations by senior personnel in a high pressure hydrocarbon plant. Protective Systems – there was evidence that it was common for a large number of control room process alarms to be active at any one time. Many of these were considered to be “nuisance alarms”. There was no clear identification of safety critical alarms, which may explain why the operator failed to respond promptly to the loss of lean oil flow. Competent Personnel and Procedures – it is clear that supervisors and operators did not know the dangers of operating process equipment at extremely low temperatures. They also had not been trained nor had been exercised on the implications of loss of lean oil flow. As a result, the operator failed to inform his supervisor immediately after the lean pumps were lost. Even after the supervisor had returned, it took almost another hour before the supervisor ordered the shutdown of Gas Plant No: 1. Incident Investigation – process accidents were rarely the subject of an incident report unless they were accompanied by injury to people or damage to property, despite near miss reporting being a requirement of Esso’s safety management system. Emergency response – while there was no criticism of the emergency response made after the explosion and fire, there was clearly a major business interruption consequence of losing the Longford plant. Longford supplied almost all of the natural gas requirements of the State of Victoria. Business Continuity Planning on the part of both Esso and their customers would have reduced the impact from this incident. Performance Management of Integrity Management and Learning – an external assessment of the application of Esso’s OIMS at Longford had been carried out 6 months prior to the accident. The assessment report found that Esso had successfully applied the OIMS programme at the plant. However, the Royal Commission found that the observations made by the assessment team appeared inconsistent with the Commission’s own findings concerning the failure of Esso to implement it’s own systems particularly in relation to risk identification, analysis and management, training, operating procedures, documentation, data and communications. Assessments and audits need to be carried out by knowledgeable and experienced personnel who explore the full range of organisation and personnel to ensure that everybody understands 7. LACK OF HAZID (HAZard Identification) 173 health and safety management systems and the means by which they are implemented at site. Incidents of a Similar Nature Grangemouth Hydrocracker explosion: see detailed report in this book. Triple Fatality at Polymers plant, USA, Three employees were killed during the unbolting of a cover plate on a 750 gallon (2850 l) capacity polymer catch vessel during preparations to open the vessel for cleaning. The vessel had been cleaned three days previously and the plant, which produced partially aromatic polyamides, was then restarted for the next production run. Part of the pre-start up procedure is to test run the extruder that handles the final product, but this was not done. At the appropriate time in the start up sequence attempts were made to start up the extruder, but it was found that the screws would not turn. Preparations were then made to shut the unit down which requires flushing with solvent butanediol and water over an extended period. During the shutdown and flushing abnormal temperatures and pressure were observed at various points in the process, but eventually plans were made to open the polymer catch vessel to remove accumulated polymer. Lockout/tagout procedures were put in place and a maintenance technician assisted by process operators commenced removing the bolts attaching the cover plate to the catch vessel. After about 22 bolts (half of the total) had been removed from one side of the cover, the cover plate blew off, striking all three persons. Examination of the vessel internals showed that there was a layer of polymer 3 to 5 inches (75–125 mm) thick covering the entire internal surface, blocking all inlet and outlet connections. The investigation found that a HAZOP had been carried out only 2 years previously that had recognised the potential for polymer blockage of process pipework. However, during the HAZOP it had been assumed that existing safeguards were adequate, including: procedures in place for proper valve alignment, pressure relief valves and rupture discs fitted to protect against over pressure, and hot oil jacketing of pipework and equipment installed to help prevent blockage by polymer. What it had failed to recognise was the potential for all safeguards to fail from polymer formation. The HAZOP also did not address other aspects of design, specifically: drains, instrument tappings and 174 INCIDENTS THAT DEFINE PROCESS SAFETY lines, block valves, and relief valve position/protection. The catch vessel relief valve was located 7_ feet (2.3 metres) from the vessel and was full of polymer. The investigation also found that although early research work had identified the potential for decomposition products to be formed when polymer and solvent are subjected to elevated temperatures, this hazard had not been addressed in the operating and maintenance procedures. The pre-start up checks had not been completed, which resulted in the start up creating significant amounts of polymer before the condition of the extruder was discovered. Finally, the pattern of bolt removal is clearly against good practice and normal line breaking procedures. Texas City ISOM Explosion – particularly in respect of Performance Management and Learning. Some references to read more: • • • • • Arial photo of Esso plant, ABC Network Report of the Royal Commission into the accident at Esso Longford. Lessons from Longford, Andrew Hopkins, CCH Australia Ltd., ISBN 1 86468 422 4 The Journal of Occupational Health and Safety Australia and New Zealand, Volume 18(6), December 2002, Special Issue: Lessons from Longford: the trial by Andrew Hopkins BP Amoco Polymers, Inc. Augusta, Georgia, March 13, 2001 U.S. Chemical Safety And Hazard Investigation Board, Investigation Report No. 2001-03-I-G, Issue Date: June 2002 7. LACK OF HAZID (HAZard Identification) 175 EXPLOSION AT BP GRANGEMOUTH HYDROCRACKER, March 22, 1987 At 07:00 a violent explosion, heard up to 20 miles away (30 km), occurred at the Hydrocracker Unit that completely destroyed the LP (low pressure) separator. A crane driver who had just come onto the unit at the start of his working day was killed, but no other injuries occurred. A major fire with flames up to 300 ft (100 metres) in height followed the explosion that took over 6 hours to control. Pieces of the LP separator weighing up to 3 tonnes were scattered over a distance of over half a mile (1 km) away. Rebuilding took over 18 months and the total cost of the accident was in the region of $100 millions. BP were prosecuted under the UK Health and Safety at Work Act and fined £500,000 (c. $750,000). The Hydrocracker Unit had been shutdown on March 13 due to a major refinery shutdown that occurred as a result of the flare line incident. The opportunity was taken to repair a defective weld, and the unit recommissioned on March 21. At around 01:15 on Sunday, March 22, an automatic shutdown was initiated by a spurious high temperature being indicated in one of the reactor beds. After resolving the problem, the unit was held on gas circulation at 2100 psig (145 bar g) with the reactor beds at around 575°F (300°C) to await reintroduction of feed later in the morning. A shift change occurred at 06:00 accompanied by the usual handover, which included a description of minor problems with the recycle gas compressor and an instruction that the unit should remain on gas circulation pending the arrival of the day supervisor to oversee reintroduction of feed. The incoming shift crew then made their normal start of shift inspection rounds and returned to the mess room for breakfast just before 07:00. At 07:00 a violent explosion occurred, centred on the LP Separator, a horizontal cylindrical 176 INCIDENTS THAT DEFINE PROCESS SAFETY vessel 30 ft long and 10 ft in diameter (10_3 metres) which was constructed from 0.71 inch (18 mm) steel plate. Large pieces of this vessel up to 3 tonnes in weight were thrown up to 0.62 mile (1 km) away. The nucleonic level transmitter fitted to the vessel was never found. The investigation concluded that the explosion was caused by introduction of high pressure gas into the LP separator through the HP Separator level control valve, which had been opened manually. Other scenarios were examined in detail but discounted, including: hydrocarbon/oxygen combustion inside the LP Separator, opening of the manual bypass around the HP Separator level control valve, and spurious mechanical failure. There is no evidence or reason to believe that this explosion was the result of sabotage, rather that it was the result of an operational error made as attempts were being made to lower the liquid inventory within the HP Separator in preparation for start-up. 7. LACK OF HAZID (HAZard Identification) 177 Although the unit was on gas circulation, liquid feed and products were still being carried forward from equipment, the amounts reducing with time. In cold weather under no flow conditions, wax had been found to have solidified in the pipework between the HP and LP Separators. It appears that an operating practice had grown up to warm through the pipework and prove it was clear prior to start up by manually opening the HP Separator level control valve and observing the levels in the two vessels. The duty Boardman at the time of the accident had not been trained in or nor had he practiced this technique. During the investigation, an operator recalled an incident about 2 years previously when gas was heard to be passing between the HP and LP Separators with the relief valve lifting on the latter. However, no incident occurred as the control room operator closed the level control valve manually – no near miss report was made and, therefore, there was no investigation. The LP Separator was designed for 150 psig (10 bar g) and protected from overpressure by a single relief valve, designed to pass 12:25 tonnes/hour of gas at 160 psig (10.7 bar g). The design cases for this relief valve included blocked gas outlet and external fire situations, but not for high-pressure gas blow through from the HP Separator. The blow through case had been considered in the design with protection provided by two extra low level switches fitted, in parallel, to the HP Separator. Activation of either of these switches would trip shut the liquid level control valve. In addition to these two extra low level switches, the HP Separator was originally provided with a conventional float type level detector that provided both level indication and an audible alarm when the level fell to 20% of the operational range. The float chamber and extra low level switches were mounted on a common level bridle designed to minimise the numbers of nozzles in the shell of the large, high pressure, stress relieved HP Separator vessel. This arrangement had proved problematic since commissioning due to wax precipitation in the liquid phase within the HP Separator, particularly in cold weather and/or when problems were experienced with steam tracing. A second level indicator was provided of the nucleonic type that was not susceptible to process conditions. However, this could only be installed at the level bridle; the source strength required to detect the liquid level across the whole of the vessel would have been far too high to allow normal operator access due to the 4 inch (100 mm) wall thickness of the HP Separator itself. The same liquid level problems existed within the LP Separator, but nucleonic detection across the whole vessel was possible as the wall thickness was far lower at _ inch (18 mm). Audits prior to the accident had recognised that the LP Separator relief valve was not designed for the gas blow through case, confirming the safety critical nature of the HP Separator extra low-level switches. They also acknowledged the operational problems experienced in detection of the liquid level within that vessel. Recommendations were made to duplicate the level bridle and to provide 178 INCIDENTS THAT DEFINE PROCESS SAFETY independent tappings for the extra low level switches. These were never implemented. In 1980 a flare and relief study performed on the unit recognised the gas blow through case, but assumed that the extra low level switches would function correctly. However, after the accident it was found that both extra lowlevel switches were inoperative, one through being assembled incorrectly and the other due to blocked tappings. Even if the switches had operated properly the protection was still not available as the electrical supply to the trip solenoid on the HP Separator level control valve had been disconnected some years previously, possibly because of spurious activation. Many of the operators were aware of this and ignored spurious indications on the alarm console. Calculations carried out after the accident showed that a pressure of 725 psig (50 bar g) would be sufficient to burst the LP Separator, and that this would be achieved by gas blow through with the HP Separator level control valve open by more than 38%. Integrity Management Hazard Evaluation and Management – the Hydrocracker had been built in the late 1960’s well before HAZOP or any other form of process hazards analysis was used in design. Process units were built against a background of standards, many of which had been developed in the aftermath of major incidents. The design cases for the LP Separator relief valve, for example, fully conformed to the API Codes and Standards that existed at the time. Subsequent to the accident, BP carried out a world-wide study of all HP/LP interfaces to establish situations where there was insufficient downstream overpressure protection. A significant number were found that were urgently resolved. With the introduction of Process Safety Management, initial and regular HAZOP studies will identify such situations that have pre-existed or been allowed to creep in through an ineffective management of change programme. Major Accident Potential – when the Grangemouth Hydrocracker was built it was to “conventional” standards in respect of proximity of other process units and in the design of control buildings and workshops. It was very fortunate in this case that the control room and associated mess room and changing facilities, built in the centre of the unit, survived. The control room had been built with large, almost floor to ceiling, windows; the only protection being that they were fitted with wired glass. Had the explosion been of the partially confined vapour cloud type, the outcome could have been the complete destruction of the buildings with the death or serious injury of the entire operating crew of 9 persons. Management of Change – when the changes were made to the extra low level protection systems on the HP Separator, including the electrical disconnection of 7. LACK OF HAZID (HAZard Identification) 179 the trip solenoid on the liquid level control valve, there was no formal risk assessment process applied. Documentation of the changes was either nonexistent or, in one case, by hand written annotation on a drawing. A robust management of change programme will identify many types of change, with change to protective systems being one with the highest likely potential. Formal management of change reviews take time to organise, with further time required to implement action items. Sometimes, it is necessary to make changes at very short notice, such as when a protective system shows signs of becoming inactive during normal operations. The management of change programme must include the measures to be taken in such an event together with the roles and responsibilities of those at the scene, particularly outside of normal business hours. Engineering Authorities – it was noted in the investigation report that the refinery’s senior instrument engineer had commented on the electrical disconnection of the trip solenoid on the liquid level control valve in a 1985 memo – 2 years before the accident. However, nothing appears to have happened as a result of this observation. The inference is that there was no clear line of communication or responsibility for this aspect of plant safety. Plant Integrity – the Hydrocracker was the highest pressure process unit that had been installed in a BP UK refinery, with flange ratings and wall thicknesses of pressure vessels and pipework well in excess of anything that had been experienced before. The unit was also one of the largest of its kind in the world when it was commissioned, designed to process far heavier feedstock than previous smaller units in the USA had been designed for. It was also a process that was highly exothermic, with the potential for heating equipment well past its point of failure. Lessons from Hydrocracker disasters in the USA had been conditioned along the lines of extreme exotherms threatening mechanical integrity, and did not appear to include the hazards of gas breaking through the HP/LP interface although this has happened before. The initial operating period after commissioning was plagued with problems, particularly phase separation within the HP Separator (which also contained a water wash section to remove ammonia from the recycle gas), and the deposition of wax. Although the unit underwent several revamps and turnarounds, the emphasis appears to have been on achieving throughput and performance, rather than enhancing plant integrity. Protective Systems – the extra low level switches on the HP Separator were the ultimate protection afforded to the LP Separator. Had that protection been in the form of conventional pressure relief valves, they would have been tested at every turnaround and replaced or repaired if found defective. From all of the evidence coming out of the investigation into this incident, it is clear that the extra low level 180 INCIDENTS THAT DEFINE PROCESS SAFETY switches and HP Separator level control valve trip systems had never been tested since the original unit commissioning in 1972. Competent Personnel and Procedures – the control room operator was not experienced in blowing though the interconnecting pipework between the HP and LP Separators, but on the day before the accident he had been in the control room when a senior operator had blown through the line prior to that day’s start up. It appears that this practice was not contained in the operating procedures for the plant, nor was contained in the operator training package. Incident Investigation – it is clear that from the evidence of another operator that this was not the first time a blow through had occurred with the potential for a major accident. The near miss, 2 years previously, was not recorded and, accordingly, no investigation took place that could have resolved the problem and addressed the lack of protection. Operators are the people best placed to observe plant anomalies and report these for investigation and resolution. However, to be successful the organisational culture must be right and should reinforce this. Emergency Response – the fire reached major proportions and extinguishing/cooling fire water was applied at some 13,000 gallons per minute 3 (3500 m /h). Approximately 20,000 gallons (over 90 tonnes) of foam concentrate was used. The surface drainage system was unable to cope with these quantities, and extensive flooding occurred. Hydrocarbons released from the unit floated on the water, and although a foam blanket was applied a break in the foam allowed a flash fire to occur. Attendance by the Refinery Fire Brigade and the local authority Central Region Brigade was prompt and co-operation between them was excellent throughout the incident. The pre-arranged call-out procedure for contacting personnel worked well and key personnel arrived on the site between 10 and 25 minutes after the incident. The Major Incident procedure was activated with the nominated representatives meeting in the Police Station. It was considered that this served an important and helpful function in arranging, for example, additional supplies of foam concentrate and back-up equipment. Performance Management of Integrity Management and Learning – a number of external audits and reviews had identified the issue of plant safety, in particular the HP/LP interface issue. The engineering issues associated with modifying the HP Separator were immense, and potentially costly. This was a large, thick walled alloy steel pressure vessel weighing over 100 tonnes that had been stress relieved. Options were very limited on what could be done. However, nothing significant was done as a result of the audit and review findings. Audits and reviews are carried out with the aim of identifying unacceptable situations. They are carried out by specialists who can introduce experience and 7. LACK OF HAZID (HAZard Identification) 181 knowledge from outside the locality to an organisation. As such, they should be heeded with each recommendation and observation formally responded to by the recipient management, who are ultimately responsible for the safety of the plant. Incidents of a Similar Nature Hydrocracker Feed Drum Explosion, US refinery The feed drum on a Hydrocracker Unit exploded following a trip of the feed pumps. The manway door flew through 2 tanks, before coming to rest inside a third. A major fire resulted. The cause of incident was the piping of the minimum flow return line from the high pressure feed pumps back to the feed drum. Hydrocracker feed pumps normally discharge in the range 2,500–3,000 psig (170–200 bar g). They are unable to run against a closed head as friction of oil running between the small internal clearances would result in a rapid build up of heat followed by seizure. A minimum flow bypass is installed that automatically opens if the flow through the pump falls below a pre-set value. In the case of this unit, the minimum flow bypass was taken from downstream of the pump discharge non-return (check) and block valves and fed directly back to 182 INCIDENTS THAT DEFINE PROCESS SAFETY the feed drum. The relief valve on the feed drum, typically set at 100 psig (7 bar g) was sized only for failure of the low pressure purge gas controller and the external fire case. When the feed pumps tripped, operators were unable to intervene before the liquid feedstock had been pushed back from where it entered the reactors, which were under normal processing pressure of around 2,500 psig (170 bar g). A simple HAZOP would have identified a particularly dangerous situation. Subsequent Hydrocracker designs installed the minimum flow return line upstream of the pump non-return valves. Some references to read more: • The Fires and Explosion at BP Oil (Grangemouth) Refinery Ltd, a report of the investigations by the Health and Safety Executive into the fire and explosion at Grangemouth and Dalmeny, Scotland, March 13, March 22 and June 11, 1987, HSE Books 1989, ISBN: 0 1188 5493 3 7. LACK OF HAZID (HAZard Identification) 183 REACTIVE CHEMICALS Note: this section is composed of 3 separate incident descriptions to show that similar causes can lead to incidents in different situations: production, storage or transport. Road tanker explosion, Teeside Rohm & Haas plant, UK, January 3, 1976 On a Saturday afternoon, a parked road cistern containing approximately 14,500 kg (32,000 lbs) of water contaminated Glacial Acrylic Acid (GAA) violently ruptured, injuring three nearby plant workers and destroying equipment in the vicinity. Multiple small fires were started by falling ignited acrylic polymer and had to be extinguished by the Municipal Fire Brigade. General view of damage: in the foreground, the debris are what is left of a small temporary building, the road tanker was located in the background, in front of the piperack. A GAA batch was produced over New-Year night. For multiple reasons, the small batch was contaminated with water (0.58% for a 0.2% maximum specification), but it received the proper quantity of inhibitor. The off-specification GAA batch was loaded on the road tanker on the next Friday to take it to Seal Sands storage to be downgraded to CAA (Crude Acrylic Acid). Unfortunately, the time of delivery was past receiving hours and the storage facility sent the cistern back to the plant for the weekend. To avoid freezing of the GAA (that solidifies at 14°C (57°F)), operators connected the truck heating coil to a warm water supply (cold water was warmed from a conventional service tee with a mixture of steam and water: there was no way to check water or GAA temperatures). 15 hours after the tanker was connected to the warm water supply, operators noticed that thick white vapours were blowing out the loosened top lid of the road cistern. They shut off the steam water supply just before the explosion occurred. 184 INCIDENTS THAT DEFINE PROCESS SAFETY The investigations carried out concluded that the road cistern was overpressured by the rapid polymerization of the GAA (estimations were 300 psi (20 bars)). Portions of the GAA polymer that had reached auto-ignition temperature dispersed fires over a large area. However, some of the polymerized material showed no indication of any ignition, confirming that there was a non-uniform temperature distribution in the polymer mass in the cistern prior to the explosion. The most probable mechanism for initiation of the polymerization was attributed to a combination of local inhibitor deficiency and local overheating: • local inhibitor deficiency: the GAA at approximately 20°C (68°F)was loaded in the cold road tanker (around 6°C (43°F)). Therefore the first GAA to enter was probably cooled at or below its’ solidification temperature, at the bottom of the tanker, near the heating coil that was not in use at that time. Since the inhibitor is not soluble in the frozen monomer, the layer of material immediately adjacent to the coil was uninhibited: the inhibitor had migrated away from the solid GAA. This freezing of the GAA could also have been accomplished by a first circulation of only cold water at 6°C (43°F) in the heating coil when it was connected to the steam-water tee. • local overheating: because of the single point of entry of the heating coil in the cistern, the inlet temperature may well have been 60 or 70°C (140–158°F), so that the now thawed but uninhibited GAA reached the same temperature. Under this thermal stimulus, without inhibitor, polymerization started and slowly raised the temperature of the bulk of the GAA to a point where that even inhibitor presence could not prevent a runaway polymerization. Pesticide explosion during storage, Bartlo Packaging (BPS), Inc, May 8, 1997 A massive explosion and fire destroyed an agricultural chemical packaging building in West Helena, Arkansas. Three firefighters were killed by the blast and 17 others injured. Among other products, BPS was repackaging a pesticide (AZinphos Methyl — AZM 50W) produced by Micro Flow Company (MFC), from bulk to 1 lb bags. During the morning of May 8, 1997, a truck of 26 bulk bags of 1,600 pounds each of AZM 7. LACK OF HAZID (HAZard Identification) 185 50W pesticide was unloaded into a new BPS warehouse. Some bags of AZM were placed by forklift operators against a compressor header pipe located on a wall of the new warehouse. Repackaging operations required the use of two reciprocating air compressors. The compressors were located in the southern portion of the original building against which the new warehouse was built in 1995. The compressors discharge pipes went through the new warehouse addition north wall into a common header pipe. This header pipe (in red on drawing below) was fifteen feet (4.5 m) long and nearly six feet (1.8 m) above the concrete floor. The AZM bulk bags were stacked two-high. The top bags were listing so that they were in contact with the wall (and the pipe). After lunch break, a forklift operator noticed heavy smoke coming from the new warehouse. He couldn’t enter the building due to density of the smoke. He raised the alarm and told colleagues to evacuate. When firefighters arrived on scene, they first made sure that all employees were accounted for and they consulted MSDS with BPS management. As 4 firefighters were getting ready to enter the building, an explosion occurred, collapsing a wall (room 9 & 10 side on drawing above) on them and killing three. EPA/OSHA investigation determined that: 186 INCIDENTS THAT DEFINE PROCESS SAFETY • Some AZM bags were located against the hot compressor header pipe. Tests made on a similar installation showed that this pipe had a temperature above 300°F (149°C). • AZM thermally decomposed, releasing yellow smoke and flammable gases. Tests carried out after the incident showed that the product was decomposing rapidly above 212°F (100°C) and almost instantaneously above 338°F (170°C). MSDS for AZM didn’t indicate the potential for flammable gases release. • Flammable gases accumulated in the warehouse and were ignited resulting in an explosion, probably when the power was switched off by the local electricity Company at Fire Department request. The report also indicates that BPS did not have procedures to ensure segregation of incompatible materials and was relying only on MSDS from Manufacturers. Napp Technologies, Inc., Lodi, New Jersey When employee arrived on April 21, 1995 for the morning shift, they smelled a strong rotten egg odor and puffs of white smoke were seen coming out of a blender where sodium hydrosulfite, aluminium powder, potassium carbonate and benzaldehyde had been mixed the previous day to produce a batch of 3 approximately 1,000 gallons (3.8 m ) of gold precipitating agent. The plant was evacuated, but operators returned in the building to dump the batch, with some plant fire brigade members with fire hoses as back-up. At 07:47, a hissing noise was heard and a violent explosion occurred, killing 5 employees and injuring 4. During firefighting operations, water run-off was contaminated with fluorescein (a bright green dye) and other chemicals. Fish died up to 2 miles downstream. Sodium hydrosulfite and aluminium powder react with water in an exothermic reaction and their decomposition/oxidation can result in a deflagration. The EPA/ OSHA investigation team therefore concentrated on looking for water sources to the blender. The blender used for that batch was fitted with a dual mixer (in blue) / vacuum tube (in green) / feed line (purple pipe) that was connected to the shell of the blender by a graphite seal (in red under arrow on left hand side) cooled with water (see drawing below). 7. LACK OF HAZID (HAZard Identification) 187 The investigation team found that this seal had wear patterns that would have allowed small quantities of water to slowly leak into the blender, starting a series of exothermic reactions over a few hours. Early signs (unusual odors, bubbling, pressure build-up, etc.) that something was going wrong were not identified and employees attempted to correct the batch overnight when it should have taken less than one hour. Decomposition of sodium hydrosulfite produced sulfur dioxide, hydrogen sulfide and more water: the decomposition process, once started, was self-sustaining. The reaction generated sufficient heat to cause aluminium powder to react rapidly with the other ingredients and generate more heat. During the emergency attempt to off-load the blender of its reacting content, the materials ignited in contact with air and the explosion occurred. Integrity Management Hazard Evaluation and Management – the Rohm & Haas report on the GAA road cistern explosion concludes that “there are several anomalies and gaps in our knowledge. Further research and development work should be put in hand as soon as possible to study this on an urgent basis.” The EPA/OSHA report on BPS warehouse explosion states that “MFS (AZM Manufacturer) and BPS did not have a full understanding of the hazards associated with AZM”. The EPA/OSHA report on Napp blender explosion indicates that “and inadequate process hazard analysis was conducted and appropriate preventive actions were not taken”. Major Accident Potential – in all the examples above, the potential for a major incident was grossly underestimated or completely ignored. Even in Napp incident case, where the reactions of sodium hydrosulfite and aluminium powder 188 INCIDENTS THAT DEFINE PROCESS SAFETY with water were known by employees and numerous incidents data available (EPA/OSHA report lists dozens of these: however Napp did not appear to know about them), no-one raised concerns about the use of a blender that incorporated potential leak points of water (water cooled seal and cooling jacket). Management of Change – when the changes were made to build the new warehouse at BPS Inc., there was an opportunity to assess the potential hazards of a hot pipe in an area where hazardous chemicals were to be stored, and to develop procedures that address storage restrictions. Protective Systems – in the Rohm & Haas GAA incident, there was no possibility for operators to know what the water or GAA temperatures were. They could only check that the water coming out of the heating coil was warm or not by touching it. Even worse, a change in utility system pressures (either on the water or the steam side) could affect the adjustment initially made by the operator, without any alarm being triggered. Competent Personnel and Procedures – in all cases described above, the fact that the hazard analysis were incomplete or not done lead to operators using inadequate procedures and having no or not enough training on the potential problems that they may face. The Napp case is typical of operators attempting to get deviations corrected without understanding the full potential of the situation and without having clear instructions on when and how to trigger an adequate emergency shut-down. Emergency Response – in BPS warehouse explosion case, the EPA/OSHA report questions the strategy implemented by the Fire Department to prepare for entry into the building when no lives were threatened and too many unknown factors (which chemicals were involved, what were the combustion product hazards, etc.). On one side, an aggressive response is potentially placing firefighter lives at risk to save an insured building; on the other hand it may prevent escalation and sustain economic activity. Similarly, the decision to dump reactor content in Napp incident was ill-advised but there was no understanding that allowing contact with air could potentially lead to an explosion. Incidents of a Similar Nature Sadly, hundreds of similar chemical incidents reports are available. The following ones were chosen because they both clearly illustrate the need for good communications between researchers who may have identified particular hazards, and designers/operators. In these two incidents, hazards were clearly 7. LACK OF HAZID (HAZard Identification) 189 identified early on, but not included in the design, procedures and training, to catastrophic outcomes. Hydroxylamine plant explosions, US and Japan On February 19, 1999, a violent explosion destroyed the Concept Sciences Inc. plant in Pennsylvania. Five people were killed and another 14 injured. Operators were distilling an aqueous solution of hydroxylamine and potassium sulfate to produce the first batch of the new facility. Hydroxylamine is an oxygenated derivative of ammonia and is used in the semi-conductor manufacturing industry to clean circuits. It may ignite spontaneously if a large surface is exposed or on contact with sulfate, metals and oxidants. Hydroxylamine crystals and solutions can explosively decompose at high concentrations (above 70% per Concept Sciences Inc. MSDS). During the distillation process, high concentrations (above 86%) and temperatures were reached, allowing decomposition, possibly accelerated by contaminants. The Chemical Safety Board case study published on this incident indicates that Concept Sciences Inc. showed deficiencies in process knowledge/documentation and in process safety reviews for capital projects: despite knowing that above 70%, a solution of hydroxylamine could decompose explosively, this knowledge was not translated into the process design, as the new plant was designed to concentrate hydroxylamine up to 85%. A simple ‘what-if’ process hazard analysis was carried out, without considering factors that could lead to an explosion. A well-performed HAZOP would have identified particularly dangerous situations. On June 10, 2000, a similar explosion destroyed Nissin plant in Japan, killing 4 people and injuring 58 others: during a 5 hours temporary shut-down to replace oil in a vacuum pump, concentration of hydroxylamine solution was allowed to raise up to 85% when it detonated. 190 INCIDENTS THAT DEFINE PROCESS SAFETY Morton International, Inc. plant explosion – April 8, 1998, USA: During the manufacture of a batch of Yellow 96 Dye (petroleum fuel dying additive) by mixing ortho-nitrochlorobenzene (o-NCB) and 2-ethylexylamine (2-EHA) a runaway reaction occurred, overpressuring the r e a ctor vessel. Flammable materials were released and an explosion occurred, injuring 9 employees. The process to produce Yellow 96 Dye was designed to run at approximately 150°C (302°F), first by external heating, then by self-heating using the exothermic reaction: the reactor external envelope (‘jacket’) could receive steam (for initial heating) or cold water (to slow reaction rate). This 150°C temperature is very close to the decomposition temperature of the Dye, an exothermic reaction initiated at 195°C (383°F). This undesired reaction was identified by Morton researchers in the late 80s, but it seems that the Paterson plant, where the explosion occurred, was not aware of this hazard. 3 The plant produced 25 batches of that Dye in 1,000 gallons (3.8 m ) reactors: 20% of these showed some unexpected temperature rises, but these were not investigated. In 1996, a decision was made to manufacture the following batches in 3 2,000 gallons (7.6 m ) reactors, without a Management of Change review that may have shown that this change increased inventory and decreased by 10% the heat transfer area that was used to cool down the reaction. 50% of the following batches showed unexpected temperature rises, but again these were not investigated. On the day of the incident, operators loaded warmer products than usual and then left steam heating on for longer than usual. Once they saw the temperature in the reactor increasing rapidly, they tried to stop the reaction by introducing cold water in the jacket, but this was not enough. When rupture disks activated, the temperature was rising rapidly to 260°C (500°F). Operators started their escape just before the vessel ruptured. A large fireball went through the building roof and subsequent fire had to be extinguished by the fire brigade. Some references to read more: • “BPS Inc., West Helena Arkansas” EPA/OSHA chemical accident investigation report, EPA 550-R99-003, April 1999. 7. LACK OF HAZID (HAZard Identification) • • • • • 191 “Napp Technologies Inc., Lodi New Jersey” EPA/OSHA chemical accident investigation report, EPA 550-R97-002, October 1997. “Morton International Inc.”, Chemical Safety Board investigation report 1998-06-I-NJ. “The explosion at Concept Sciences: hazards of Hydroxilamine”, Chemical Safety Board case study 1999-13-C-PA, March 2002. “A checklist for inherently safer chemical reaction process design and operation”, Center for Chemical Process Safety, March 2004. “How to prevent runaway reactions” EPA/CEPPO, EPA 550-F99-004, August 1999.