DETAIL OF CHANGES 1) Piling at AB11 & AB12 The combination of two pile group of 600 dia. and single pile 800 dia. were the original foundation system proposed for Academic Building 11 & 12 (Refer Dwg. RB 6199-CD-G-AB 12-PL-1 (Rev.00), RB 6199-CD-G- AB 11-PL-1 (Rev.00), 6199-CD-G-GN-PD-1 (Rev.00), RB 6199-CD-G-GN-PD-5 (Rev.00)). The quantity of rock socket were the concern during these time as cost of piling work are high due to the cost of rock coring. Majority of pile are having rock coring length about 12m. The length of rock socket during these time are based on SI report prepared by United Soil Sdn Bhd which indicated layer of Sandstone around 12m bgl. However actual rock coring length at site will be confirm based on the following criteria for the contractor to claim as rock coring which is:1) Change of Coring Tools, 2) Index Strength of rock sample, Is50 are more than 2MPa, for at least three (3) samples picked by the S.O Representative, and 3) Rock sample recovered are more than 70%. All criteria stated above must be achieved for the contractor to claim as coring in rock and for the designer to design as pile in rock. In order to minimize the rock socket depth for the piling, Value Engineering exercise has been done and we have work closely with JUBM in order to determine the most cost effective foundation system. After several option have been developed and proposed, it has been confirmed by JUBM that 900dia pile are the most economical and effective in term of reducing the pile socket length and thus reduce the foundation cost for AB 11&12. Majority of rock socket length required for 900dia. Pile are around 8m. Thus we revised the dwg based on single pile 900dia for all column (refer Dwg. RB 6199-CD-G-AB 12-PL- 1 (Rev.01), RB 6199-CD-G-AB 11-PL-1 (Rev.01), 6199-CD-G-GN-PD-1 (Rev.01), RB 6199-CD-G-GN-PD-5 (Rev.01)). Two (2) Preliminary Test Pile were conducted on May 2018 for TP-1 at AB11 area by the Sub Con of AZSB, Samalaju Sdn Bhd and Intrumentation contractor Strainstall Sdn Bhd. During the boring process for TP-1 pile, rock are encountered at 12m bgl. As the rock sample were extracted from the rock auger, we have found that the rock majority of them are completely weathered SHALE/SANDSTONE with Rock Quality Designation, RQD equal to 0%. After inspecting all the sample extracted, the rock are found to be not satisfying the rock coring criteria stated above thus the contractor can only claim it as boring in soil. The boring are continued until the desired pile toe level and all the rock found are still not satisfying the rock coring criteria as well, thus the designer have changed the design on site based on pile in soil for the TP-1 pile. The boring process shifted to preliminary test pile, TP-2 at AB12 are afterward, and rock encountered at 14mbgl. The rock sample extracted from the rock auger are similar and identical to TP-1 borehole and still not satisfying the rock criteria mentioned in the drawing, thus based on what we have discovered during the boring of TP-1 and TP-2 we decided that the pile are to be design as purely in soil as all of the rock encountered at site during boring process of TP-1 and TP-2 are not satisfying the rock criteria mentioned above. Based on the preliminary test pile result conducted, we found that the soil condition are better than expected. We found that the 900dia can be reduced to 800dia pile in order to reduce the concrete and steel bar volume up to 20% reduction from previous 900dia foundation system. Furthermore as no rock were satisfying rock socket criteria during test pile, the rock coring length are omitted. The column load also being reduced by the Structural Engineer thus reducing the required pile length in soil for majority of the pile. We revised our drawing and adopted 800dia single pile for all column except column at B-C/9 where two pile group 600dia pile were introduced in order to cater for the high loading due to canopy roof tied to the building(refer Dwg. RB 6199-CD-G-AB 12-PL-1 (Rev.02), RB 6199-CD-G-AB 11-PL-1 (Rev.02), 6199-CD-G-GN-PD-1 (Rev.03), RB 6199-CD-G-GN-PD-5 (Rev.03), RB 6199-CD-G-GN-PD-7 (Rev.00), RB 6199-CD-G-GN-PD-8 (Rev.00)). 2) Piling at Service Tunnel Originally the service tunnel were designed as pile raft without consideration of ground support (Totally relying on the pile friction). 600 dia. Bored Pile were adopted as a support of service tunnel scatter through the whole length of tunnel and column from toilet area are supported by isolated Four (4) and Two (2) 600dia. Bored Pile Group. (Total of 153 nos) (Refer Dwg. RB 6199-CD-G-ST-PL-1Rev.00). The quantity of rock socket were the concern during these time as cost of piling work are high due to the cost of rock coring. Majority of pile are having rock coring length about 7m for service tunnel area. The length of rock socket during these time are based on SI report prepared by United Soil Sdn Bhd which indicated layer of Sandstone around 12m bgl. However actual rock coring length at site will be confirm based on the following criteria for the contractor to claim as rock coring which is:1) Change of Coring Tools, 2) Index Strength of rock sample, Is50 are more than 2MPa, for at least three (3) samples picked by the S.O Representative, and 3) Rock sample recovered are more than 70%. All criteria stated above must be achieved for the contractor to claim as coring in rock and for the designer to design as pile in rock. In order to minimize the rock socket depth for the piling, Value Engineering exercise has been done and we have work closely with JUBM in order to determine the most cost effective foundation system. After several option have been developed and proposed, it has been confirmed by JUBM that 800 dia pile are the most economical as this system does not require the pile length to go deeper into rock layer thus omitting the rock socket cost for service tunnel. Nos of pile for that option also have reduced to 85 nos. compared to original design of 153nos. Based on these we revised the dwg based on 800dia bored pile pile raft system for service tunnel and column from toilet area are supported by isolated one (1) and Two (2) 800dia. Bored Pile Group. (refer Dwg. RB 6199-CD-G-ST-PL-1-Rev.01). Based on the preliminary test pile result conducted, we found that the soil condition are better than expected. After carefully studied we found that the ground can be used to support the service tunnel, only at the area where the column from the building connecting to the service tunnel wall which is supported by 600 dia bored pile as the column load there are very high and cant be supported by the ground. Thus Bored Pile nos can be reduced to 50 nos. Furthermore as no rock were satisfying rock socket criteria during test pile conducted at AB11 & AB12 (TP-1 & TP-2), the rock coring length are omitted (refer Dwg. RB 6199-CD-G-ST-PL-1-Rev.02).