Xcel Energy Smaller Scale Transmission Projects Northern MAPP Subregional Planning Group April 3, 2007 Srinivas Vemuri, Jason Standing, and Daniel Kline Small Project Information T-Corners Transformer Replacement Hyland Lake – Dean Lake 115 kV Upgrade Woodbury – Tanners Lake Upgrade Northeast Mankato 69 kV Plan South Shakopee Substation Ironwood Second Transformer Ironwood Bus Upgrade Lawrence Second Transformer Tracy Switching Station Capacitors Keegan Lake – Lebanon Hills Prescott 10 MVAR Cap Bank 3 T-Corners 115/69 kV Transformer Replacement Substation currently has two 115/69 kV transformers (#1 & #2) Tx #1 – 62.5 MVA Tx #2 – 112 MVA Summer 2011 – Loss of Transformer #2 will load #1 to 80 MVA (128%) Plan to replace existing 62.5 MVA bank with matching 112 MVA bank 4 T-Corners 115/69 kV Transformer Replacement T-Corners 52 Miles Eau Claire Metro Area 5 Ironwood Second Transformer Ironwood 88/34.5 kV Transformer currently rated at 25 MVA 78 MW generation at Bayfront Substation Loss of Bayfront 115/92 kV transformer sends Bayfront generation through 88 & 34.5 kV systems Severely overloads Ironwood – Bayfront 88 kV line Severely low voltages along Ironwood 34.5 kV system Add second Ironwood 88/34.5 kV transformer 6 Ironwood Second Transformer 7 Ironwood Terminal Equipment Upgrade Ironwood – Bayfront 115 kV conductor rated at 189 MVA (850 Amps) Ironwood 115 kV substation equipment with various ratintgs 200 Amp CT 300 Amp Wave Trap 380 Amp Bus 400 & 800 Amp Breakers, 600 Amp Switches Outage of Bayfront – Saxon Pump 88 kV line loads Ironwood 115 kV to 72 MVA (361 Amps) Outage of Bayfront 115/92 kV transformer loads Ironwood 115 kV to 87 MVA (437 Amps) Replace capacity-limiting terminal equipment 8 Lawrence Second 112 MVA Transformer This project is to add an additional 115/69 kV, 112 MVA transformer at the Lawrence Substation in Sioux Falls. This is needed due to the double-circuit outage of the 115 kV line out of Split Rock to Cheery Creek. In Summer 2011, loss of Split Rock-Cherry Creek and Split Rock-West Sioux Falls double-circuit outage results in a loading of 145.9 MVA (130.2%) of the 112 MVA transformer at Lawrence. 9 Lawrence Second 112 MVA Transformer 10 Tracy SW 12 MVAR CAP This project is to replace the existing 5.4 MVAR, 69 kV cap bank at the Tracy Switching Station with a new 12 MVAR cap bank. In Summer 2006, for loss of the Lyon County 69 kV source, the following buses have low voltage: Walnut Grove = 0.855 pu Tracy SS = 0.856 pu Lake Sarah = 0.860 pu Currie = 0.872 pu Slayton = 0.886 pu Hadley = 0.898 pu Lake Wilson = 0.905 pu 11 Tracy SW 12 MVAR CAP 12 Kegan Lake – Lebanon Hills 69 kV Line Upgrade Reconductor the 3 #8 CU section of the Kegan Lake – Lebanon Hills 69 kV line to at least 48 MVA. During 2011 summer peak conditions, the line overloads to 110.5% in the base case. 13 Kegan Lake – Lebanon Hills 69 kV Line Upgrade 14