CASE STUDY High vibration of De-dusting Fan and Motor As planned, yesterday the machine was stopped for further investigation and the followings noticed. Coupling issues We took one set of reading before stopping the machine and high axial vibration was noticed with 2X fundamental frequency for both fan and motor. Alignment was rechecked and no severe deviation observed. The coupling ,model 80SPLX 225-140, found over stretched in position and measurement revealed that the coupling assembly length is lesser by 3 mm than the design hub to hub distance 140 mm. Further inspection of the coupling element showed that the adapter ring got shifted radially from its normal position, forcing coupling bolts to touch the spacer holes where it is supposed to be free to transfer the torque through the shim pack as per this coupling design. Inspection of the coupling bushings confirmed that the clearance between the machined bolts and the bushings are higher than normal and due this higher clearance, the adapter ring got shifted during normal operation resulted high axial vibration. Overstretching and low coupling quality are suspected as the reasons for previous coupling failure also, when the coupling hub to hub distance was observed 144 mm against the coupling element length 137mm with an abnormal overstretch of 7mm. High axial vibration observed before stopping the machine for inspection 2X RPM frequency vibrations, due to coupling fault Structural vibrations The machine was stopped and one set of reading was taken for the motor vertical direction in monitor mode. Modulating vibration at 0.6X RPM ( 16.6 Hz)sub synchronous frequency was noticed with max. 3 mm/s amplitude at MOV at stopped condition. This frequency was observed during the normal running condition also along with the rotational speed frequency ( see the previous mail below). Subsequently solo run of the motor was carried out, no other fault frequencies observed except 0.6X RPM (16.6 Hz) dominancy with 3 mm/s amplitude induced by structural /pipe line vibrations. Further analysis showed that the structural vibration is transferred to the machine via the fan suction line, which is connected to many highly vibrating top floors through piping connections. There is a bellow in between the fan suction flange and the suction line. However, the amplitude of vibration on both sides of the bellow found same, confirms that the performance of the bellow is not adequate at present and the vibration is transferring from the line to the machine through this bellow without any change in amplitude.. Vibration analysis showed that no induced vibration is transferred to the machine from the first floor steel structure ( where the machine is mounted) which is isolated with resilient pads at the machine base frame. Motor solo run, dominancy at 0.6X RPM ( 16.6Hz), no other faults observed Suction pipe line vibration measured at 6th floor where it is connected to roll crusher .Dominancy at 16.5 Hz Base frame excitation An offline bump test was carried out for the base frame vertical plate below motor back foot and very high excitation of amplitudes with multiple frequencies are noticed. Further inspection showed that the stiffness of this vertical plate is very poor compared to other 3 vertical plates of the same base frame. One of the reasons for motor free end vertical high vibration could be the low stiffness of the vertical plate. Load run after corrections Alignment was corrected to 0.03 mm in axial and radial (Rim and face method), coupling dismantled and re assembled after centering( due to high clearances of coupling bushings) the spacer and adapter ring, suction line was cleaned with water wash, impeller washing carried out to remove deposits and load run was carried out. Overall vibrations are reduced but the motor vertical vibrations are slightly high, modulating with 0.6X rotational frequency generated from structural vibrations. The overall vibration measured at motor free end vertical is 6.3 mm/s, which is slightly high. Signature after alignment corrections, 0 .6X rotational frequency is still dominant Following recommendations are made based on the above observations and analysis , 1. Replace the coupling ( The existing one can twist in its position any time during normal operation , lead to high axial vibration) 2. Ensure the hub distance according to coupling length. ( Yesterday M/M could not do this due to motor bolt bound) 3. Arrest the suction line vibration. 4. Check and replace the suction bellow if required. 5. Stiffen the motor side vertical base plate. 6. Check and replace the base resilient pads if required. Regards Sasikumar Sr.Reliability Engineer FERTIL Mobile: 00971505112524 Tel: 009712 60 26673 Web site: www.fertil.com